Crash of a Rockwell Grand Commander 680 in Newburgh: 2 killed

Date & Time: Sep 16, 1980 at 1411 LT
Operator:
Registration:
N1520K
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Newburgh - Hudson
MSN:
680-0730-32
YOM:
1959
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
182
Circumstances:
After takeoff from Newburgh-Stewart Airport, while in initial climb, the twin engine airplane banked right then stalled and crashed, bursting into flames. Both occupants were killed.
Probable cause:
Complete engine failure during initial climb due to improper maintenance. The following contributing factors were reported:
- Improper maintenance on part of the owner personnel,
- The pilot failed to maintain flying speed,
- Forced landing off airport on land,
- Champion RHB32E plugs installed, not approved,
- Cowl fasteners missing.
Final Report:

Crash of a Beechcraft E90 King Air off New York: 2 killed

Date & Time: Mar 10, 1980 at 2303 LT
Type of aircraft:
Registration:
N4GN
Flight Type:
Survivors:
No
Schedule:
Fort Lauderdale - New York
MSN:
LW-38
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1750
Captain / Total hours on type:
225.00
Circumstances:
The pilot started the approach to New York-LaGuardia Airport by night and poor weather conditions due to a low ceiling, rain falls and thunderstorm activity. He initiated a go-around and started a second approach few minutes later. On final, the twin engine airplane crashed in the East River few hundred yards offshore. The aircraft was lost and both occupants were killed.
Probable cause:
Control collision with water during a missed approach due to improper IFR operation. The following contributing factors were reported:
- Airways facilities personnel: inadequately maintained approach facilities,
- Airport facilities: instrument landing system,
- Low ceiling,
- Rain,
- Thunderstorm activity,
- Hail,
- LOC alignment out of tolerance.
Final Report:

Crash of a Rockwell Grand Commander 680FL in Rexville: 3 killed

Date & Time: Aug 23, 1979 at 0931 LT
Registration:
N5003E
Flight Phase:
Survivors:
No
Schedule:
Albany - Lancaster
MSN:
680-1737-144
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
3100
Circumstances:
The airplane departed Albany on an air pollution monitoring program flight to Lancaster, carrying two passengers and one pilot. En route, while cruising in marginal weather conditions, the pilot encountered severe turbulences when control was lost. The airplane crashed in Rexville, killing all three occupants.
Probable cause:
Uncontrolled collision with ground during normal cruise due to inadequate preflight preparation. The following contributing factors were reported:
- The pilot continued flight into known areas of severe turbulences,
- Turbulences associated with clouds and thunderstorms.
Final Report:

Crash of a Rockwell Aero Commander 560A in Pavilion: 1 killed

Date & Time: Jul 21, 1979 at 0905 LT
Operator:
Registration:
N2748B
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Pavilion - Pavilion
MSN:
560-0248
YOM:
1955
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4405
Captain / Total hours on type:
217.00
Circumstances:
The pilot, sole on board, was taking part to a local air show when, flying at low height, the airplane banked right and crashed following the failure of the right engine. The aircraft was destroyed and the pilot was killed.
Probable cause:
Engine failure and subsequent stall after the left engine failed due to valve assemblies failure. The following contributing factors were reported:
- Material failure,
- The pilot failed to maintain flying speed,
- High vegetation,
- Forced landing off airport on land,
- Exhaust valve, second cylinder on right engine failed.
Final Report:

Crash of a Beechcraft E18S in Newburgh

Date & Time: Apr 4, 1979 at 2315 LT
Type of aircraft:
Registration:
N149PA
Flight Type:
Survivors:
Yes
Schedule:
Boston - Newburgh
MSN:
BA-412
YOM:
1959
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3897
Captain / Total hours on type:
99.00
Circumstances:
While descending to Newburgh-Stewart Airport by night and marginal weather conditions, the pilot informed ATC about icing conditions but was vectored for a holding pattern due to heavy traffic. On short final, the twin engine airplane stalled and crashed about 1,600 feet short of runway threshold. The pilot, sole on board, was seriously injured.
Probable cause:
Stall on approach due to improper in-flight decisions. The following contributing factors were reported:
- Airframe ice,
- Icing conditions including sleet, freezing rain,
- Visibility three miles or less,
- Fog,
- Pilot informed of icing at holding altitude prior to his entering holding.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain near Lake Placid: 3 killed

Date & Time: Dec 25, 1978 at 1918 LT
Registration:
N114TA
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Detroit - Saranac Lake
MSN:
31-7405461
YOM:
1974
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
2741
Circumstances:
The twin engine airplane departed Detroit-Wayne County Airport at the end of the afternoon on a flight to Saranac Lake-Adirondack Airport, NY. While descending by night and limited visibility due to snow falls, at an altitude of 3,100 feet, the airplane struck tree tops and crashed in a wooded area located on Mt Nye, in The Adirondack Mountain Range, about six miles south of Lake Placid. As the airplane failed to arrive, SAR operations were initiated but eventually abandoned after few days as no trace of the aircraft nor the three occupant was found. Walkers found the wreckage on 29 April 1979, about 16 miles southeast of Saranac Lake Airport.
Probable cause:
Controlled flight into terrain following improper IFR operation. The following contributing factors were reported:
- Low ceiling,
- Snow,
- Visibility one mile or less,
- Fog.
Final Report:

Crash of a Rockwell Shrike Commander 500S in Hammondsport: 3 killed

Date & Time: Sep 11, 1978 at 1925 LT
Registration:
N40MA
Survivors:
Yes
Schedule:
Raleigh - Hammondsport
MSN:
500-3234
YOM:
1975
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
6300
Circumstances:
While on approach to Hammondsport-Taylor-Van Gelder Airstrip in excellent weather conditions, the pilot failed to realize his altitude was too low when the airplane struck a mountain and crashed few miles from Hammondsport. Two passengers were rescued while three other occupants were killed.
Probable cause:
Stall on final approach after the pilot misjudged distance and altitude and failed to maintain flying speed. The following contributing factors were reported:
- Obstructions to vision,
- Sunglare,
- Haze,
- Aircraft was approaching toward rising terrain.
Final Report:

Crash of a Beechcraft E18S in Albany

Date & Time: Sep 1, 1978 at 2046 LT
Type of aircraft:
Operator:
Registration:
N58H
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Albany – Windsor Locks
MSN:
BA-250
YOM:
1957
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4618
Captain / Total hours on type:
214.00
Circumstances:
After takeoff from Albany Airport, while in initial climb, the left engine failed. The airplane lost height then struck the ground and crashed near the airport. The pilot, sole on board, was slightly injured and the aircraft was destroyed.
Probable cause:
Engine failure during initial climb for undetermined reasons. The following contributing factors were reported:
- Failed to follow approved procedures,
- Improper emergency procedures,
- Forced landing off airport on land,
- Failed engine not feathered.
Final Report:

Crash of a Piper PA-31-310 Navajo in East Hampton

Date & Time: Aug 7, 1978 at 0033 LT
Type of aircraft:
Operator:
Registration:
N9093Y
Flight Type:
Survivors:
Yes
Schedule:
Elmira - East Hampton
MSN:
31-128
YOM:
1968
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2507
Captain / Total hours on type:
150.00
Circumstances:
The crew was approaching East Hampton Airport and encountered marginal weather conditions with limited visibility to 3/4 of mile due to the night and ground fog. While in a missed approach configuration, the crew lost control of the airplane that stalled and crashed few miles from the airfield. Both occupants were injured and the aircraft was destroyed.
Probable cause:
Stall during a missed approach after the crew failed to maintain flying speed. The following contributing factors were reported:
- Fog,
- Sky obscured,
- Visibility 3/4 mile or less,
- Pilot transitioned from visual reference to instrument reference,
- Encountered ground fog after MDA.
Final Report:

Crash of a BAc 111-203AE in Rochester

Date & Time: Jul 9, 1978 at 1730 LT
Type of aircraft:
Operator:
Registration:
N1550
Survivors:
Yes
Schedule:
Boston - Rochester - Montreal
MSN:
44
YOM:
1965
Flight number:
AL453
Crew on board:
4
Crew fatalities:
Pax on board:
73
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
13461
Captain / Total hours on type:
7008.00
Copilot / Total flying hours:
8746
Copilot / Total hours on type:
4687
Aircraft flight hours:
33693
Aircraft flight cycles:
48215
Circumstances:
The pilot-in-command adopted a wrong approach configuration and passed over the runway 28 threshold at an excessive speed of 184 knots (61 knots above the Vref) in a nose down attitude. The nose gear landed first at a speed of 163 knots (40-45 knots above normal touchdown speed) 2,540 feet past the runway threshold (runway 28 is 5,500 feet long). Unable to stop within the remaining distance, the airplane overran, struck a drainage ditch, lost its undercarriage and came to rest 728 past the runway end. All 77 occupants were evacuated safely, one of them was slightly injured.
Probable cause:
The captain's lack of awareness of airspeed, vertical speed, and aircraft performance throughout an ILS approach and landing in visual meteorological conditions which resulted in his landing the aircraft at an excessively high speed and with insufficient runway remaining for stopping the aircraft, but with sufficient aircraft performance capability to reject the landing well after touchdown. Contributing to the accident was the first officer's failure to provide required callouts which might have alerted the captain to the airspeed and sink rate deviations. The Safety Board was unable to determine the reasons for the captain's lack of awareness or the first officer's failure to provide required callouts.
Final Report: