Crash of a Lockheed C-130H3 Hercules at Al Taji AFB

Date & Time: Jun 8, 2020 at 2205 LT
Type of aircraft:
Operator:
Registration:
94-6706
Flight Type:
Survivors:
Yes
Schedule:
Ali Al Salem AFB - Al Taji AAF
MSN:
5398
YOM:
1995
Country:
Region:
Crew on board:
7
Crew fatalities:
Pax on board:
19
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total hours on type:
1700.00
Copilot / Total hours on type:
506
Circumstances:
On 8 June 2020, at approximately 2205 hours local time (L), the mishap aircraft (MA), a C-130H (tail number (T/N) 94-6706), was involved in a mishap during a routine mobility airlift mission from Ali Al Salem Air Base, Kuwait, into Al Taji (Camp Taji), Iraq, when it failed to come to a stop during landing, overran the runway, and impacted a concrete barrier. All 26 mishap crew (MC) members and passengers survived the mishap, with relatively minor injuries to two of the individuals. The MA was damaged beyond repair, and was valued at $35,900,000. The MA was from the 165th Airlift Wing (165 AW), Georgia Air National Guard (ANG), was manned with Wyoming ANG crew members deployed from the 153d Airlift Wing (153 AW), in Cheyenne, Wyoming, and assigned to the 386th Air Expeditionary Wing (386 AEW) at Ali Al Salem Air Base, Kuwait. The mishap occurred at the end of the first planned leg of the MC’s mission on 8 June 2020. The MC departed Ali Al Salem Air Base, Kuwait, at approximately 2053L, with an uneventful start, taxi, takeoff, and cruise to Camp Taji. During descent into Camp Taji, the MC prepared the MA for a nighttime landing, using night vision devices. During this time, the MC turned the MA earlier than their planned turn point, did not descend to lower altitudes in accordance with their planned descent, and allowed the airspeed to exceed recommended maximum speeds for the configuration the plane was in. During the landing, the MA continued to be above the planned glideslope and maintained excessive airspeed, with a nose-down attitude until touchdown. The MA proceeded to “porpoise” or oscillate down the runway from the point of touchdown until the MA was slowed sufficiently by use of reverse thrust from the engines to allow the MA to settle onto the wheels, which in turn allowed for the brakes to engage. The MA, despite slowing somewhat, had less than 1,000 feet of runway remaining by that point, and thus overran the runway and did not come to a complete stop until it impacted a 12-foot-high concrete barrier, approximately 600 feet past the runway.
Probable cause:
The Accident Investigation Board (AIB) President found by a preponderance of the evidence that the causes of the mishap were the MA’s excess airspeed above recommended landing velocity, which caused the MA to maintain lift (flight) and did not provide sufficient weight on wheels (WOW) to allow braking action to occur. Additionally, the AIB President found, by a preponderance of the evidence, the MC’s failure to adequately assess risk, failure to follow proper procedures, and their poor communication were all substantially contributing factors to the mishap.
Final Report:

Crash of a BAe 125-700A in Sartaneja

Date & Time: May 28, 2020
Type of aircraft:
Operator:
Registration:
N720PT
Flight Type:
Survivors:
Yes
MSN:
257032
YOM:
1978
Country:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The airplane landed on an illegal airstrip, lost its nose gear and hit obstacles before coming to rest. No one was found on site. The aircraft was damaged beyond repair.

Crash of an Airbus A320-214 in Karachi: 98 killed

Date & Time: May 22, 2020 at 1439 LT
Type of aircraft:
Operator:
Registration:
AP-BLD
Survivors:
Yes
Site:
Schedule:
Lahore - Karachi
MSN:
2274
YOM:
2004
Flight number:
PK8303
Country:
Region:
Crew on board:
8
Crew fatalities:
Pax on board:
91
Pax fatalities:
Other fatalities:
Total fatalities:
98
Aircraft flight hours:
47124
Aircraft flight cycles:
25866
Circumstances:
On 22 May 2020 at 13:05 hrs PST, the Pakistan International Airlines aircraft Airbus A320-214, registration number AP-BLD, took off from Lahore (Allama Iqbal International Airport – AIIAP) Pakistan to perform a regular commercial passenger flight (PK8303) to Karachi (Jinnah International Airport – JIAP) Pakistan, with 8 crew members (01 Captain, 01 First Officer, and 06 flight attendants) and 91 passengers on board. At 14:35 hrs the aircraft performed an ILS approach for runway 25L and touched down without landing gears, resting on the engines. Both engines scrubbed the runway at high speed. Flight crew initiated a go-around and informed “Karachi Approach” that they intend to make a second approach. About four minutes later, during downwind leg, at an altitude of around 2000 ft, flight crew declared an emergency and stated that both engines had failed. The aircraft started losing altitude. It crashed in a populated area, short of runway 25L by about 1340 meters. An immediate subsequent post impact fire initiated. Out of 99 souls on-board, 97 were fatally injured and 02 passengers survived. On ground 04 persons were injured however 01 out of these reportedly expired later at a hospital.

Below, the preliminary report published by the Pakistan AAIB.
Final Report:

Crash of a Cessna 402C in Hampton

Date & Time: May 9, 2020 at 1513 LT
Type of aircraft:
Operator:
Registration:
N4661N
Survivors:
Yes
Schedule:
Peachtree City - Peachtree City
MSN:
402C-0019
YOM:
1979
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7330
Captain / Total hours on type:
11.00
Copilot / Total flying hours:
1096
Copilot / Total hours on type:
5
Aircraft flight hours:
17081
Circumstances:
According the commercial pilot and a flight instructor rated check pilot, they were conducting their first long-duration, aerial observation flight in the multiengine airplane, which was recently acquired by the operator. They departed with full fuel tanks, competed the 5-hour aerial observation portion of the flight, and began to return to the destination airport. About 15 miles from the airport, the left engine fuel warning light illuminated. Within a few seconds, the right engine stopped producing power. They attempted to restart the engine and turned the airplane toward an alternate airport that was closer. The pilots then turned on the electric fuel pump, the right engine began surging, and soon after the left engine stopped producing power. They turned both electric fuel pumps to the low setting, both engines continued to surge, and the pilots continued toward the alternate airport. When they were about 3 miles from the airport, both engines lost total power, and they elected to land on a highway. When they were a few feet above the ground, power returned briefly to the left engine, which resulted in the airplane climbing and beginning to roll. The commercial pilot pulled the yoke aft to avoid a highway sign, which resulted in an aerodynamic stall, and subsequent impact with trees and terrain. The airplane sustained substantial damage to the wings and fuselage. Although both pilots reported the fuel gauges indicated 20 gallons of fuel remaining on each side when the engines stopped producing power, the flight instructor noted that there was no fuel in the airplane at the time of the accident. In addition, according to a Federal Aviation Administration inspector who responded to the accident site, both fuel tanks were breached and there was no evidence of fuel spillage.
Probable cause:
A dual total loss of engine power as a result of fuel exhaustion.
Final Report:

Crash of a Learjet 35A in Esquel: 3 killed

Date & Time: May 5, 2020 at 2238 LT
Type of aircraft:
Operator:
Registration:
LV-BXU
Flight Type:
Survivors:
Yes
Schedule:
San Fernando – Esquel
MSN:
35-462
YOM:
1982
Location:
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
1498
Copilot / Total flying hours:
2612
Aircraft flight hours:
11711
Aircraft flight cycles:
10473
Circumstances:
The airplane departed San Fernando Airport on an ambulance flight to Esquel, carrying a doctor, a nurse and two pilots. On approach to Esquel-Brigadier General Antonio Parodi Airport at night, the crew encountered poor visibility (200 metres) and the visual contact with the runway was lost intermittently. Nevertheless, the crew continued the approach and at decision height, the captain decided to continue the descent. After crossing Runway 23 threshold at a height of 78 feet, the pilot-in-command initiated a go-around procedure and turned to the left. The airplane continued in a left hand turn, causing the left wing tip fuel tank to struck the ground. Out of control, the airplane crashed on a small embankment located about 400 metres to the left of the runway centerline, coming to rest upside down and bursting into flames. Both passengers were killed and both pilots were seriously injured. Two days later, the copilot died from injuries sustained.
Probable cause:
It was determined that the accident was the consequence of a controlled flight into terrain (CFIT) and the airplane did not suffer any technical anomalies.
The following contributing factors were identified:
- The crew failed to check the approach charts according to SOP's,
- The approach was initiated and continued in conditions that were below weather minimums,
- Visibility data transmitted by Tower to the crew were inaccurate, leading to confusion on the part of the pilots and their decision-making,
- Both engines were at full power upon impact as the crew was initiating a go-around procedure.
Final Report:

Crash of an Embraer EMB-120RT Brasília in Bardale: 5 killed

Date & Time: May 4, 2020 at 1545 LT
Type of aircraft:
Operator:
Registration:
5Y-AXO
Flight Type:
Survivors:
No
Schedule:
Mogadiscio – Baidoa – Bardale
MSN:
120-259
YOM:
1992
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
On approach to Bardale Airstrip, the twin engine aircraft struck the ground and crashed 5 km from the airport, bursting into flames. The aircraft was totally destroyed and all five occupants were killed. The crew was enroute from Mogadiscio to Bardale with an en route stop in Baidao, carrying medical supplies and mosquito nets.
Probable cause:
When the aircraft was arriving at Bardale FOB, the usual direction is east-west, but the aircraft was flying from west-east to land over the base camp. Even though the troops did not shoot it down, the aircraft crashed on the ground and was apparently not ready not land. The troops concluded that the aircraft was suspected to be a suicide and trying to find the target to make suicide in the base camp because of the movement of the aircraft. Due to lack of communication and awareness, the aircraft was shot down and all five occupants (3 Kenyan and 2 Somali citizens) died. The incident was performed by a non-AMISOM troops of Ethiopia, which will require mutual collaborative investigation team from Somalia, Ethiopia and Kenya for determine the truth.
Final Report:

Crash of a Pilatus PC-12/47 in Mesquite

Date & Time: Apr 23, 2020 at 1600 LT
Type of aircraft:
Operator:
Registration:
N477SS
Flight Type:
Survivors:
Yes
Schedule:
Dallas – Muscle Shoals
MSN:
813
YOM:
2007
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2283
Captain / Total hours on type:
1137.00
Aircraft flight hours:
7018
Circumstances:
Shortly after takeoff the pilot reported to the air traffic controller that he was losing engine power. The pilot then said he was going to divert to a nearby airport and accepted headings to the airport. The pilot then reported the loss of engine power had stabilized, so he wanted to return to his departure airfield. A few moments later the pilot reported that he was losing engine power again and he needed to go back to his diversion airport. The controller reported that another airport was at the pilot’s 11 o’clock position and about 3 miles. The pilot elected to divert to that airport. The airplane was at 4,500 ft and too close to the airport, so the pilot flew a 360° turn to set up for a left base. During the turn outbound, the engine lost all power, and the pilot was not able to reach the runway. The airplane impacted a field, short of the airport. The airplane’s wings separated in the accident and a small postcrash fire developed. A review of the airplane’s maintenance records revealed maintenance was performed on the day of the accident flight to correct reported difficulty moving the Power Control Lever (PCL) into reverse position. The control cables were inspected from the pilot’s control quadrant to the engine, engine controls, and propeller governor. A static rigging check of the PCL was performed with no anomalies noted. Severe binding was observed on the beta control cable (propeller reversing cable). The cable assembly was removed from the engine, cleaned, reinstalled, and rigged in accordance with manufacturer guidance. During a post-accident examination of the engine and propeller assembly, the beta control cable was found mis-rigged and the propeller blades were found in the feathered position. The beta valve plunger was extended beyond the chamfer face of the propeller governor, consistent with a position that would shut off oil flow from the governor oil pump to the constant speed unit (CSU). A wire could be inserted through both the forward and aft beta control cable clevis inspection holes that function as check points for proper thread engagement. The forward beta control cable clevis adjustment nut was rotated full aft. The swaging ball end on the forward end of the beta control cable was not properly secured between the clevis rod end and the push-pull control terminal and was free to rotate within the assembly. Before takeoff, the beta valve was in an operational position that allowed oil flow to the CSU, resulting in normal propeller control. Vibration due to engine operation and beta valve return spring force most likely caused the improperly secured swaging ball to rotate (i.e. “unthread”) forward on the beta control cable. The resulting lengthening of the reversing cable assembly allowed the beta valve to stroke forward and shut off oil flow to the propeller CSU. Without propeller servo oil flow to maintain propeller control, the propeller faded to the high pitch/feather position due to normal leakage in the transfer bearing. The reported loss of power is consistent with a loss of thrust due to the beta control cable being mis-rigged during the most recent maintenance work.
Probable cause:
The loss of engine power due to a mis-rigged beta control cable (propeller reversing cable), which resulted in a loss of thrust inflight.
Final Report:

Crash of a BAe 125-F400B in Caballo Blanco

Date & Time: Mar 22, 2020
Type of aircraft:
Operator:
Registration:
XB-PNK
Flight Type:
Survivors:
Yes
MSN:
25227
YOM:
1970
Country:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Probably engaged in an illegal contraband flight, the crew attempted to land on a road when the aircraft crashed against a vehicle parked in a sugarcane field and awaiting for the it, bursting into flames. No one was found on site. The airplane was damaged beyond repair. The registration XN-PNK is false, the older one was XB-OUF.

Crash of a Hawker 800XP in Scottsdale

Date & Time: Mar 14, 2020 at 1600 LT
Type of aircraft:
Operator:
Registration:
N100AG
Flight Type:
Survivors:
Yes
Schedule:
Rogers – Scottsdale
MSN:
258747
YOM:
2005
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9150
Captain / Total hours on type:
650.00
Copilot / Total flying hours:
10556
Copilot / Total hours on type:
52
Aircraft flight hours:
4823
Circumstances:
The pilot stated that, upon landing, the airplane touched down on the runway centerline with light and variable wind conditions. The pilot recalled that the touchdown felt normal but that, during the landing roll, the airplane began to veer to the right. The pilot added full left rudder, but the airplane continued to veer off the runway surface and encountered large rocks located between the runway and taxiway. A postaccident operational check of the nosewheel steering system revealed no mechanical malfunctions or anomalies that would have precluded normal operation. The left nosewheel tire was not adequately inflated and was worn to the point at which the cord was exposed; the right nosewheel tire was within tolerances. Also, one-third of the rim was absent on the left nosewheel tire outer wheel half. The available evidence precluded a determination of whether the imbalance between the nosewheel tires contributed to the control problem on the runway. It could also not be determined if the left nosewheel tire damage occurred before the touchdown or as a result of the accident sequence.
Probable cause:
The pilot’s inability to maintain directional control during landing for undetermined reasons, which resulted in a runway excursion.
Final Report:

Crash of a Cessna 525 CJ1 in Porlamar

Date & Time: Mar 13, 2020 at 1700 LT
Type of aircraft:
Operator:
Registration:
YV3452
Flight Type:
Survivors:
Yes
Schedule:
Porlamar – Caracas
MSN:
525-0084
YOM:
1994
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew departed Porlamar-Del Caribe-General en Jefe Santiago Mariño Airport on a ferry flight to Caracas-Oscar Machado Zuloaga Airport. After takeoff, while climbing, the crew encountered unknown technical problems and was cleared to return for an emergency landing. After touchdown, the aircraft was unable to stop within the remaining distance. It overran, lost its undercarriage and came to rest, bursting into flames. Both pilots were seriously injured and suffered burns. The aircraft was partially destroyed by fire.