Crash of a Piper PA-46-350P Malibu Mirage in Cranfield

Date & Time: Apr 29, 2021 at 1425 LT
Operator:
Registration:
G-HYZA
Flight Type:
Survivors:
Yes
Schedule:
Cranfield - Cranfield
MSN:
46-36130
YOM:
1997
Flight number:
86
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
34620
Captain / Total hours on type:
1588.00
Circumstances:
On the morning of the accident flight, G-HYZA was flown for approximately 16 minutes on test flight 85. The flight test team debriefed the results and prepared the aircraft for flight 86. The plan for this flight was for the HV battery to be switched off at the end of the downwind leg then, if able, to fly three or more circuits at 1,000 ft aal using the HFC only to provide electrical power. The flight test team discussed experimenting with combinations of higher airspeeds and propeller rpm that would reduce the aircraft angle of attack and improve the mass flow of air through the radiator which provided cooling for the HFC. This was considered as a potential strategy to manage a slow rise in temperature in the HFC which they had observed in previous flights when flying on that power source alone. The test card for flight 86 was not amended to reflect this intention. At 1406 hrs, following a normal start using both the HV battery and HFC to provide electrical power, the HV was switched off to preserve its electrical capacity. The aircraft taxied to the holding point and was cleared to line up on Runway 03. The weather was fair with good visibility and light winds from 010°. The aircraft entered the runway and backtracked to the threshold where the pilot commenced a run-up of the propulsion system to ensure the HFC could achieve thermal stability within the flight test parameters. Once the temperatures in the HFC were stable, the pilot switched on the HV battery to bring both power sources online and commenced the takeoff run. As the aircraft accelerated and the power lever was advanced, the observer operated the high temperature override switch to maintain the temperature of the HFC within the operating limits. After takeoff, the pilot turned onto the crosswind leg and climbed to the circuit height of 1,000 ft agl. During the downwind leg of the right-hand circuit, the pilot stated the power was set to 95 kW, the propeller to 2,500 rpm and the airspeed to 100 kt. Once stabilized at these parameters, which were at variance with the flight test card conditions, the observer confirmed that the HFC operating temperatures were within limits. He then instructed the pilot to reduce power to 90 kW to assess the effect on the airspeed, which reduced to approximately 95 kt. The pilot increased the power to 95 kW to regain the target speed. The pilot set the power by reference to his display unit which was located below the throttle quadrant. When he looked up from this task, he recognized that the aircraft was in a late downwind position. He turned onto base leg and commented that they were losing speed in the turn. The observer suggested that they could increase power to 120 kW to regain the lost airspeed, then reduce power before turning off the HV battery to re-establish the test conditions. He also suggested a reduction in propeller rpm. The pilot increased power to 120 kW but did not reduce the propeller rpm. As he started to turn onto final, the pilot briefed that once he had established straight and level flight he would reduce the power slightly and turn off the HV battery leaving the electrical motors powered by the HFC. He called final on the radio and was cleared by ATC to fly through at circuit height. Approaching the runway threshold at approximately 940 ft agl, the pilot reduced power to 90 kW, set the airspeed to 90 kt then selected the HV battery to off. Immediately, all electrical drive to the propeller was lost. The pilot and observer made several unsuccessful attempts to reset the system to restore power from the HFC with the observer stating the action to be taken and the pilot making the switch selection. The observer instructed the pilot to select the HV battery to on to reconnect the alternative power source. HV power was not restored so the observer instructed the pilot to attempt a system reset with the HFC in the off position. Electrical power was still not restored and at 440 ft agl the observer declared “the voltage is too high”, to which the pilot replied, “we’ve got to do something quick”. The observer called for a further reset attempt and adjusted the power lever. The aircraft had now travelled the length of the runway and was at approximately 320 ft aal when the observer reported that power could not be restored. The pilot transmitted a MAYDAY call and initiated a turn to the left to position for a landing on Runway 21. Almost immediately he recognized that he did not have sufficient height to complete the manoeuvre so lowered the landing gear and selected full flap for a forced landing in a field that was now directly ahead on a north-westerly heading. The aircraft touched down at approximately 87 kt ground speed on a level grass field. The pilot applied the brakes, and the aircraft continued its movement until it struck, and passed through, a hedge during which the left wing broke away. The nosewheel and left main wheel entered a ditch and the aircraft came to an abrupt stop. The pilot and observer were uninjured and exited the aircraft through the upper half of the cabin door. The airport fire service arrived quickly at the scene. The observer returned to the aircraft and vented the hydrogen tank to atmosphere and disconnected the HV battery to make the aircraft safe.
Probable cause:
The loss of power occurred during an interruption of the power supply when, as part of the test procedure, the battery was selected off with the intention of leaving the electrical motors solely powered by the hydrogen fuel cell. During this interruption the windmilling propeller generated a voltage high enough to operate the inverter protection system, which locked out the power to the motors. The pilot and observer were unable to reset the system and restore electrical power.
Final Report:

Crash of a Learjet 35A in Belo Horizonte: 1 killed

Date & Time: Apr 20, 2021 at 1452 LT
Type of aircraft:
Registration:
PR-MLA
Flight Type:
Survivors:
Yes
Schedule:
Belo Horizonte - Belo Horizonte
MSN:
35-072
YOM:
1976
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3432
Captain / Total hours on type:
41.00
Copilot / Total flying hours:
3034
Copilot / Total hours on type:
2211
Circumstances:
The airplane departed Belo Horizonte-Pampulha-Carlos Drummond de Andrade Airport at 1420LT on a local training fight. On board were two pilots and one passenger. After 30 minutes of flight over the area, the crew returned to the airport and initiated the approach to runway 13 to complete a touch and go manoeuvre. On final approach, the crew forgot to lower the gear, causing the airplane to land on its belly. It slid for few hundred metres, overran, went through the perimeter fence (striking concrete poles) and came to rest against trees, broken in two. The copilot aged 76 was killed while both other occupants were injured.
Probable cause:
Contributing factors:
- Attention – undetermined.
It is possible that the aircraft’s encounter with a kite led to a delayed and imprecise response to operational cues, which may have resulted in a breakdown in the alert and distraction management system, specifically regarding landing gear extension.
- Attitude – undetermined.
Conducting the flight with an unqualified pilot reflected the adoption of inappropriate attitudes such as complacency, overconfidence, and disregard for the requirements established in RBACs 91 and 61, which may have contributed to this accident.
- Crew Resource Management – a contributor.
Inefficient use of the human resources available for the aircraft operation led to inadequate task management among the crew. The PIC never questioned the aircraft’s readiness for landing, and the pilot occupying the right seat failed to monitor the aircraft configuration or assertively advise on the landing gear position for touchdown.
- Perception – a contributor.
During the approach, the aural warning indicating that the landing gear was still retracted was activated and could be heard on the CVR audio. However, the pilots took no corrective action, evidencing impaired ability to recognize and interpret internal environmental cues, which led to reduced situational awareness and culminated in a gear up landing.
- Limited pilot’s experience – undetermined.
Considering the PIC’s operational background, developed almost entirely in rotary wing aviation, it is possible that his limited experience with fixed-wing aircraft had not yet enabled him to acquire the full range of skills and knowledge necessary for the safe operation of Learjet 35 flights.
Final Report:

Crash of a Learjet 25B in Toluca

Date & Time: Apr 18, 2021 at 1527 LT
Type of aircraft:
Operator:
Registration:
XB-PIZ
Survivors:
Yes
Schedule:
Cancún - Toluca
MSN:
25-193
YOM:
1975
Location:
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Following an uneventful flight from Cancún, the crew encountered technical problems with the undercarriage while on approach to Toluca-Licenciado Adolfo López Mateos. Decision was taken to complete a belly landing on runway 15/33. The airplane slid for few dozen metres before coming to rest, bursting into flames. All 9 occupants evacuated safely and the aircraft was damaged beyond repair.

Crash of a Beechcraft 200 Super King Air in Nairobi

Date & Time: Mar 26, 2021 at 1630 LT
Operator:
Registration:
5Y-NJS
Flight Type:
Survivors:
Yes
Schedule:
Nairobi – Kisumu – Eldoret – Nairobi
MSN:
BB-837
YOM:
1981
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6589
Captain / Total hours on type:
4600.00
Aircraft flight hours:
12177
Circumstances:
The aircraft, registered 5Y-NJS operated by Westwind Aviation Ltd crashed at Ngong Racecourse. The flight with two onboard was on a private mission to Kisumu, Eldoret and back to Nairobi. The aircraft departed Wilson Airport (HKNW) at 0420Z and landed at Kisumu Airport (HKKI) at 0502Z. It then departed HKKI to HKEL at 1142Z and landed at 1200Z where it picked one passenger. The flight then departed HKEL to HKNW with three onboard at 1247Z with an estimated flight time of 40 minutes. According to the preliminary information obtained from the Captain, the aircraft attained flight level 250 42NM from Eldoret VOR. The flight was then cleared to fly direct to GV VOR by Nairobi Area Control Centre. During descend to flight level 100 they encountered bad weather whereby the wings developed heavy icing. The Captain deployed deicing systems on the wings but the problem persisted. The situation prompted the Captain to request Wilson Control to descend to “Monstry fix” for landing at HKNW which was approved. As the flight continued descending the left engine went off. The Captain requested Wilson Tower for assistance. After 30 seconds, the right engine also went off. The Captain elected to make an emergency landing at Ngong Racecourse. On landing along, the left wing collided with trees and broke-off and separated together with the left engine and the left main landing gear. The turned clockwise through 180° and faced the opposite direction. All three onboard escaped unhurt but the aircraft was destroyed.

Crash of a Boeing 737-4Y0 in Jakarta

Date & Time: Mar 20, 2021 at 1126 LT
Type of aircraft:
Operator:
Registration:
PK-YSF
Flight Type:
Survivors:
Yes
Schedule:
Jakarta - Makassar
MSN:
23869/1639
YOM:
1988
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6228
Captain / Total hours on type:
5208.00
Copilot / Total flying hours:
1255
Copilot / Total hours on type:
1084
Aircraft flight hours:
55982
Aircraft flight cycles:
65005
Circumstances:
On 20 March 2021, a Boeing 737-400F, registered PK-YSF, was being operated by Trigana Air Service on a non-schedule cargo flight from Halim Perdanakusuma International Airport (WIHH), Jakarta, Indonesia with intended destination of Sultan Hasanuddin International Airport (WAAA), South Sulawesi, Indonesia. On board in this flight was two pilots, one engineer and one Flight Operation Officer (FOO). According to the weight and balance sheet, the flight carried 16,672 kgs of general cargo, takeoff fuel of 11,100 kg and the takeoff weight was 60,695 kg (133,835 lbs). The Pilot in Command (PIC) acted as Pilot Flying (PF) and the Second in Command (SIC) acted as Pilot Monitoring (PM). At 0328 UTC (1028 LT), the PM requested clearance to Halim Tower controller (the controller) to pushback and start the engines. At 1031 LT, the PM requested to the controller for taxi clearance. There was no report of aircraft system abnormality prior to the aircraft departure. At 1047 LT, the controller issued clearance to the PK-YSF pilot to enter and to backtrack Runway 24. At 1051 LT, the PM reported ready for departure to the controller. The controller issued takeoff clearance with additional departure clearance that after takeoff, turn left to heading 180° and initially climb to altitude of 3,000 feet. The PM acknowledged the clearance. The takeoff was conducted with reduced takeoff thrust by assumed temperature of 40°C and the aircraft became airborne at 10:52:57 LT. At 1055 LT, the controller advised the pilot to report when established on heading 180°. The PM reported that they were experiencing right engine failure and requested to fly to AL NDB . The controller advised the PM to turn left heading 060° and to climb to 2,500 feet. Furthermore, the controller asked the pilot intention whether to hold over AL NDB or direct for landing approach. The PM replied that they would hold over AL NDB and added the information that no fire was detected. The controller issued clearance to fly to AL NDB at altitude of 2,500 feet. The controller assumed that PK-YSF would return to Halim and advised the Airport Rescue and Fire-Fighting (ARFF) personnel that PK-YSF experienced right engine failure and would return to Halim. At 1058 LT, the controller requested the information of time required for holding over AL NDB and was replied by the PM that holding would require about 15 minutes. Furthermore, the controller requested whether the pilot able to hold at a point about 15 to 20 Nm from AL NDB and was replied by the PM that they did not objection to the proposal. The controller instructed the pilot to maintain outbound heading up to 15 Nm, at altitude of 2,500 feet. This was intended by the controller to manage the departure and arrival aircraft to and from Halim. At 1116 LT, the PM reported that they were ready to turn left for approach. The controller advised the pilot to turn left and to intercept localizer of the Instrument Landing System (ILS) Runway 24. At 1125 LT, the PM reported to the controller that the Runway was in sight. The controller advised that the wind was from 060° at velocity of 6 knots, QNH 1,007 mbs and issued landing clearance. The aircraft touched down on the touchdown zone and shortly after, both wheels of the right main landing gear detached. The controller noticed spark appeared from the aircraft and pressed the crash bell. At 1127 LT, the controller informed pilots of the other aircraft that the runway blocked by the landing aircraft and identified fire on one of the engines. Few seconds later, the PM called the controller whether any fire and was replied by the controller that fire was visible on the left side of the aircraft.

Crash of a Cessna 208B Grand Caravan in Marsabit: 2 killed

Date & Time: Mar 20, 2021 at 1000 LT
Type of aircraft:
Operator:
Registration:
5Y-JKN
Flight Type:
Survivors:
No
Site:
Schedule:
Nairobi – Marsabit
MSN:
208B-0688
YOM:
1998
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
4235
Captain / Total hours on type:
2329.00
Copilot / Total flying hours:
344
Copilot / Total hours on type:
104
Aircraft flight hours:
16343
Circumstances:
The report describes the accident to C208B type of aircraft, registration 5Y-JKN with two crew on onboard that occurred on Marsabit Hill on 20th March 2021 in which the aircraft crashed killing two crew onboard. The aircraft with 2200lbs fuel onboard was chartered to ferry Marsabit County Officials to a peace keeping mission at Illeret 156 nautical miles North West of Marsabit town. Preliminary information revealed that the aircraft departed Wilson Airport at 08.20am (0520Z) and arrived within the vicinity of Marsabit town at around 10.00a.m (0700Z). It collided with Kofia Mbaya Hill - Marsabit terrain while attempting to approach Marsabit airstrip. The aircraft first impacted the terrain with its nose-wheel and the main landing gears leaving parts of the fuselage and iron box with its content kept in the lower baggage compartment on the sport. It then ballooned and missed a house before it flipped upside down and impacted the ground and came to rest facing opposite direction. It left a trail of aircraft parts along its path before it came to rest. The nosewheel and its assembly separated and fell off and was found next to the house 110m from its first point of impact. There was no fire after impact but all the occupants received fatal injuries.
Probable cause:
The probable cause of the accident was a continued descend into terrain without forward visibility in thick fog.
The following contributing factors were identified:
- Location of the airstrip which is surrounded by high hills,
- Inadequate flight planning and crew resource management.
Final Report:

Crash of an Antonov AN-26 in Almaty: 4 killed

Date & Time: Mar 13, 2021 at 1722 LT
Type of aircraft:
Registration:
02 white
Flight Type:
Survivors:
Yes
Schedule:
Nursultan - Almaty
MSN:
72 01
YOM:
1978
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
Following an uneventful flight from Nursultan Nazarbayev Airport on behalf of the National Security Committee of the Republic of Kazakhstan, the crew was approaching Almaty Airport runway 23R in marginal weather conditions with a ceiling at 300 feet and a visibility limited to 5 km in freezing drizzle. On short final, the aircraft struck the ground and crashed 600 metres short of runway, bursting into flames. Two crew members were rescued while four others were killed.
Those killed were:
Major Gabit Esimdaevich Barlykbayev,
Captain Doszhan Galymbekovich Baimuratov,
1st Lt Mukhtar Hadzhimukanovich Sagimbayev,
Sgt Vasilkov Evgeny Borisovich.

Crash of a Embraer EMB-120ER Brasília in Detroit

Date & Time: Mar 7, 2021 at 0008 LT
Type of aircraft:
Operator:
Registration:
N233SW
Flight Type:
Survivors:
Yes
Schedule:
Detroit - Akron
MSN:
120-307
YOM:
1995
Flight number:
BYA233
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The twin engine airplane departed Detroit-Willow Run (Ypsilanti) Airport at 2337LT on March 6 on a cargo service to Akron-Canton Airport, carrying two pilots and a load of various goods. After takeoff, the crew encountered technical problems and declared an emergency. He completed two low passes in front of the tower, apparently due to gear problems. Eventually, the aircraft belly landed at 0008LT and came to rest on runway 05R. Both pilots evacuated safely and the aircraft was damaged beyond repair.

Crash of a Beechcraft 350 Super King Air in Abuja: 7 killed

Date & Time: Feb 21, 2021 at 1148 LT
Operator:
Registration:
NAF201
Flight Type:
Survivors:
No
Schedule:
Abuja - Minna
MSN:
FL-585
YOM:
2008
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
7
Circumstances:
After takeoff from Abuja-Nnamdi Azikiwe Airport, while climbing, the crew informed ATC about an engine failure and was cleared for an immediate return. On final approach to runway 22, the aircraft went out of control and crashed in an open field, bursting into flames. The aircraft was destroyed and all 7 occupants were killed, among them two pilots, four ATOS specialists (Airborne Tactical Observation System) and one technician.

Crash of a Cessna 402B in Asunción: 7 killed

Date & Time: Feb 9, 2021 at 1430 LT
Type of aircraft:
Operator:
Registration:
0221
Flight Type:
Survivors:
Yes
Schedule:
Fuerte Olimpo – Asunción
MSN:
402B-1360
YOM:
1978
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
7
Circumstances:
On final approach to Asunción-Silvio Pettirossi Airport, the twin engine aircraft crashed on a parking place and burst into flames. A passenger was seriously injured while seven other occupants were killed.