Crash of a Learjet 55 Longhorn in Livingston

Date & Time: Jan 11, 2024 at 0837 LT
Type of aircraft:
Operator:
Registration:
N558RA
Flight Type:
Survivors:
Yes
Schedule:
Pontiac - Livingston
MSN:
55-086
YOM:
1983
Flight number:
RAX698
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
31800
Captain / Total hours on type:
800.00
Copilot / Total flying hours:
1726
Copilot / Total hours on type:
9
Aircraft flight hours:
14135
Circumstances:
The pilot in command of the airplane reported that, while on an instrument GPS approach, they listened to the automated surface observing system several times and determined that they would be landing with a “light quartering tailwind” on an upsloping runway. Once clear of clouds and with the runway in sight, the pilot canceled the instrument flight rules clearance, announced their position over the airport’s common traffic advisory frequency and received a reply with a report of 1/4 inch of dry snow covering the runway, unplowed. During the landing roll, they applied brakes, extended spoilers, and thrust reversers. Initially the airplane slowed; however, about halfway down the runway, the airplane’s antiskid system was functioning continuously, and the airplane’s rate of deceleration decreased. The pilot was unsure if the thrust reversers deployed, and he cycled the thrust reversers and did not feel any effects. The pilot stated that, in his experience, the airplane’s thrust reversers do not feel very effective. The pilot considered aborting the landing, started to clean up the airplane but thought it was too late. The airplane overran the departure end of the runway, onto a grass covered area and into a deep ravine, resulting in substantial damage to the fuselage and both wings. The pilot reported that there were no preaccident mechanical failures or malfunctions with the airplane that would have precluded normal operation. The automated weather observation station located on the airport reported that, about 44 minutes before the accident, the wind was from 090° at 12 knots. The same automated station reported that, about 16 minutes after the accident, the wind was from 090° at 12 knots. The airplane landed on runway 22. The fixed based operator owner reported that, on the day of the accident, his review of the runway conditions at the airport appeared to be around an inch of snow on the runway surface. Additionally, plowing at the airport so far this year had been “abysmal.” Big windrows and ice chunks have been left; taxiway corners had been built up to the point there could be an occurrence should an airplane be taxiing by. Earlier this year, several departures were delayed due to the runway not being plowed. According to the chairman of the airport board, there is no formal process to conduct runway assessments. However, an airport board member lives in the area and routinely visits the airport to conduct runway assessments. The runway assessments and frequency of the observations are not documented but are conveyed verbally to the airport board via cell phone. To the best of his knowledge, there is no formal snow or ice removal plan. When the runway is required to be cleared, a board member will use county provided equipment to clear the runway. The frequency of the snow removal is not documented. The airport snow removal equipment is limited to clear substance to ½ inch of the runway surface. On the day of the accident, he was not aware of a Notice to Air Misson (NOTAM) issued for the conditions of the runway environment. According to the airplane manufacturer, the estimated landing distance on a dry runway was about 3,350 ft, with loose snow and no tailwind the estimated landing distance was about 6,700 ft, and on loose snow with tailwind, the estimated landing distance was 7,531 ft. According to the Federal Aviation Administration, the airport is not required to have a snow and ice control plan. However, the airport was provided federal funds (grant) to purchase/acquire a snowplow to maintain the airport surfaces during inclement weather conditions. There may be times where issues arise, and action is delayed. In that case it is expected that a NOTAM be issued as outlined in the grant agreement.
Probable cause:
The flight crew’s decision to land on a snow-covered runway with a tailwind, resulting in a runway excursion and subsequent impact with terrain. Contributing to the accident, was the failure of the airport authority to plow the runway.
Final Report:

Crash of a Learjet 55C Longhorn near Charallave: 6 killed

Date & Time: Jun 22, 2022 at 1937 LT
Type of aircraft:
Operator:
Registration:
YV3304
Flight Type:
Survivors:
No
Site:
Schedule:
Puerto Cabello – Charallave
MSN:
55-145
YOM:
1990
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
While approaching Charallave-Óscar Machado Zuloaga Airport, the crew encountered technical problems (apparently with the reversers) and declared an emergency. The captain initiated a go around procedure and completed a circuit south of the airport. During a second approach, the airplane deviated from the approach path to the south and continued until it impacted the top of a hill located 8 km south of the airport. The aircraft was destroyed by impact forces and a post crash fire and all six occupants were killed, among them Christian Toni, President of the Estudiantes de Mérida football club.

Crash of a Learjet 55 Longhorn in Monmouth

Date & Time: Feb 25, 2020 at 2356 LT
Type of aircraft:
Registration:
N135LR
Survivors:
Yes
Schedule:
Richmond – Monmouth
MSN:
55-068
YOM:
1982
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
18288
Captain / Total hours on type:
2909.00
Copilot / Total flying hours:
14759
Copilot / Total hours on type:
1978
Aircraft flight hours:
12792
Circumstances:
The pilot reported that he and the copilot were conducting an instrument approach to the runway in a business jet. He noted that the weather conditions included fog and mist. After touching down about 1,500 ft down the 7,300-ft-long runway, he engaged the thrust reversers and applied the brakes gradually because the runway was "slippery." As the airplane approached the end of the runway, he applied full braking, but the airplane departed the end of the runway and impacted a ditch, which resulted in the forward landing gear breaking and the airplane nosing down. The copilot corroborated the pilot's statement. The fuselage was substantially damaged. The pilot reported that there were no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation.
Probable cause:
The flight crew's failure to stop the airplane on the available runway, which was wet and resulted in the airplane impacting a ditch.
Final Report: