Crash of a Beechcraft C-45H Expeditor in New Hudson

Date & Time: Jan 24, 1995 at 1620 LT
Type of aircraft:
Registration:
N618K
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
New Hudson - Port Huron
MSN:
AF-759
YOM:
1954
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4386
Captain / Total hours on type:
52.00
Copilot / Total flying hours:
1050
Copilot / Total hours on type:
60
Aircraft flight hours:
1928
Circumstances:
The pilot-in-command stated that shortly after takeoff, when the airplane was about 150 feet above the ground over a stand of trees, the left engine lost power. The pilots made a hard forced landing in a field, skidded and came to a stop against a farm building. The power loss occurred over a wooded area. Postaccident examination revealed the left engine driven fuel pump shaft had failed. Airplane records indicated the most recent maintenance occurred in november 1991. The airplane had flown 148 hours since that date.
Probable cause:
The owner/pilot's inadequate maintenance practices which resulted in a loss of engine power shortly after takeoff and the pilot's inadequate emergency procedure after the power loss occurred. Related factors are trees, diminished airspeed and abrupt touchdown.
Final Report:

Crash of a Cessna 208B Super Cargomaster in Lubbock

Date & Time: Jan 18, 1995 at 0903 LT
Type of aircraft:
Operator:
Registration:
N9461R
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Lubbock - Midland
MSN:
208B-0076
YOM:
1988
Flight number:
MRA817
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2542
Captain / Total hours on type:
514.00
Aircraft flight hours:
3984
Circumstances:
During the night before the accident, freezing rain followed later by snow, fell on the ramp where the airplane was parked. A witness reported that while assisting the pilot in removing snow from the airplane, he noted that 80% of the wing was covered with a coarse layer of ice, from 1/16 to 3/16 in thickness, that was not removed before flight. After the accident, a fireman from the city of lubbock fire department noted ice on the wing approximately 1/16th of an inch thick that had a rough texture that looked as if deposited by freezing rain. The pilot reported that shortly after take off she heard a power decrease and felt surges in the aircraft. The pilot then looked for a place to land. A detailed examination of the engine revealed no mechanical deficiencies.
Probable cause:
The pilot's failure to remove ice from the airframe prior to takeoff. Factors were freezing rain the night before and the pilots' incomplete preflight inspection.
Final Report:

Crash of a Cessna 208B Super Cargomaster in Pleasanton: 1 killed

Date & Time: Jan 12, 1995 at 1747 LT
Type of aircraft:
Operator:
Registration:
N754FE
Flight Type:
Survivors:
No
Site:
Schedule:
Visalia - Oakland
MSN:
208B-0249
YOM:
1991
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
25500
Captain / Total hours on type:
516.00
Aircraft flight hours:
2073
Circumstances:
A Cessna 208B struck a ridge line about 14 miles from the destination airport. The pilot reported to atc he had the airport in sight from 7,000 feet msl more than 30 miles away. A weather reporting station located 5 miles east of the accident site was reporting two cloud layers; a scattered layer at 1,500 feet agl, and a broken layer at 5,000 feet agl. The airplane was descending after the pilot was cleared for a visual approach. The airplane collided with a tree and the ground in a wings level attitude at an elevation of 1,500 feet msl. There was no evidence of mechanical failure or malfunction found with the airplane.
Probable cause:
Failure of the pilot-in-command to maintain visual contact with terrain and sufficient altitude for terrain clearance. Factors in the accident were the pilot's decision to initiate a descent 14 miles from the airport, and weather, specifically cloud conditions and darkness.
Final Report:

Crash of a Cessna 414 Chancellor in Augusta: 4 killed

Date & Time: Jan 12, 1995 at 0904 LT
Type of aircraft:
Registration:
N13SE
Flight Phase:
Survivors:
No
Schedule:
Swainsboro - Columbia
MSN:
414-0437
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
1312
Captain / Total hours on type:
23.00
Aircraft flight hours:
4526
Circumstances:
While climbing through 6,300 feet, the pilot reported the complete loss of power on the right engine. Approx 4 min later, and after the pilot had established an emergency descent for a landing, he reported that the left engine had also lost power. The airplane impacted a driveway and skidded into a building. Examination revealed that the right engine failed due to shifting of the engine case halves. Review of the engine maintenance records indicated that several cylinders had been replaced in recent months; the cylinder through bolts are used to torque the engine case. A reason for the loss of power on the left engine was not determined.
Probable cause:
The loss of power on the left engine for undetermined reasons. A factor was the failure of the right engine due to maintenance personnel's failure to properly torque the cylinder through bolts.
Final Report:

Crash of a Cessna 208B Super Cargomaster in Flagstaff: 1 killed

Date & Time: Jan 11, 1995 at 1805 LT
Type of aircraft:
Operator:
Registration:
N746FE
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Flagstaff - Phoenix
MSN:
208-0236
YOM:
1990
Flight number:
FDX7551
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
10000
Captain / Total hours on type:
2000.00
Aircraft flight hours:
2439
Circumstances:
A witness located near the departure end of the runway saw the airplane initially climb in a normal manner, then stay below the clouds and make a shallow bank 180-degree left turn and descend below a tree line. Tower tapes revealed that the pilot twice transmitted that he was "coming back" to the airport during which the background sound of the "fuel selector off" warning horn was heard. The pilot then informed the controller "I've got to get back", and no warning horn was heard. The airplane collided with trees and came to rest about 6,500 feet sse of the runway's end. Prior to departure, the airplane was refueled with 40 gals of jet a (20 gals per tank), which increased the total fuel load to 148 gals. The flight manual required that the fuel balance between the left and right tanks be kept within 200 pounds, and suggested turning off one fuel selector to correct unbalance situations. The condition of one fuel selector turned off will cause the "fuel selector off" warning horn to sound. Exam of the aircraft revealed no evidence of preimpact failures. Prop blade butt signatures indicated it was operating in the governing range, and engine power was being produced at impact.
Probable cause:
The pilot's failure to properly configure the aircraft fuel system prior to takeoff, and his failure maintain an adequate terrain clearance altitude while maneuvering to return to the airport. Factors in the accident were the dark night lighting conditions, low ceilings, restricted visibility conditions, and the pilot's diverted attention which resulted from activation of the airplane's fuel selector warning horn system.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in Brownsville

Date & Time: Jan 9, 1995 at 1622 LT
Registration:
N50WT
Flight Type:
Survivors:
Yes
Schedule:
Cancún – El Paso
MSN:
31-7952018
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
87
Circumstances:
During an international cross country flight the private pilot, certificated single engine land, experienced a dual engine power loss as he was being vectored to the Brownsville Airport. Following the accident the aircraft was examined by a Federal Aviation Administration inspector who found that there was fuel in the left fuel tank and that the fuel selector was in the right tank position. The pilot had reported, prior to loss of engine power, that he had low fuel indications in the right tank and that he needed a vector to Brownsville. The aircraft was landed in rough and uneven terrain, resulting in damage to the structure and wings, approximately 1/2 mile short of the runway.
Probable cause:
The fuel starvation loss of engine power due to the pilot's improper use of the fuel tank selector. Factors were the pilot's qualification and the lack of suitable terrain for landing.
Final Report:

Crash of a Beechcraft A60 Duke in Hurley: 3 killed

Date & Time: Jan 5, 1995 at 1835 LT
Type of aircraft:
Registration:
N3LP
Survivors:
No
MSN:
P-242
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
2746
Captain / Total hours on type:
209.00
Circumstances:
During climb to cruise the pilot reported a power loss on one engine and received vectors for a return to the departure airport. The pilot was subsequently cleared for the VOR-A approach and reported intercepting the inbound radial. The impact site was right of the inbound radial and short of the extended runway centerline. Weather at the airport was VFR. Post impact fire damaged the airplane. The left engine propeller was in the feather position. Visual and metallurgical examination confirmed the turbocharger shaft separated due to fatigue. The shaft contained chromium. The aircraft overhaul manual states that 'chrome plating...restoration of the shaft...are not permitted.' Metallographics revealed a microstructure of grey iron (automotive application) in the center housing. The turbocharger was overhauled and installed on the left engine in october 1989. All three occupants were killed.
Probable cause:
The pilot's failure to maintain airspeed during a single engine approach resulting in an inadvertent stall. Factors were a fatigue separation of a shaft in the left engine turbocharger due to use of a Federal Aviation Administration approved overhaul procedure that was not consistent with the manufacturer's overhaul procedure, and the resultant loss of power to the left engine.
Final Report:

Crash of a Beechcraft C90 King Air in Royal: 2 killed

Date & Time: Jan 3, 1995 at 1817 LT
Type of aircraft:
Registration:
N101GA
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Hot Springs - Pueblo
MSN:
LJ-11
YOM:
1965
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
4000
Captain / Total hours on type:
185.00
Aircraft flight hours:
7507
Circumstances:
The pilot obtained a weather briefing, filed an IFR flight plan, and took off at night on a flight from Hot Springs, Arkansas, to Pueblo, Colorado. About one minute later, he advised air traffic control that he needed to return to Hot Springs. He then contacted the airplane operator and said the heater was not working. The operator suggested that he return for repairs. The pilot was then heard to say, 'oh, shoot!' No further radio transmissions were received from the flight. The airplane cut a 400 foot swath through trees, and the wreckage path measured 940 feet. With exception of a heater problem, no pre impact mechanical failure was evident. Both occupants were killed.
Probable cause:
The pilot inadvertently allowed the airplane to descend and collide with trees, after he became diverted by an inoperative cabin heater. Darkness was a related factor.
Final Report:

Crash of a Piper PA-46-350P Malibu in Rochester: 3 killed

Date & Time: Dec 22, 1994 at 1152 LT
Registration:
N133MA
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Rochester - Guntersville
MSN:
46-22133
YOM:
1993
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
2500
Captain / Total hours on type:
96.00
Aircraft flight hours:
106
Circumstances:
The airplane departed on runway 31 in instrument meteorological conditions (IMC) and turned right to a heading of 090°. Radar contact (arts tag) was acquired about 1 to 2 miles north of the airport. Reportedly, the arts tag would typically be acquired as the airplane climbed through an altitude of about 700 feet agl. Subsequently, the airplane crashed about 2 miles north of the airport. A witness reported hearing a loud engine noise before the plane crashed. The wreckage path was oriented along a westerly heading and over an area of about 380 feet. There was evidence of an in-flight breakup. An outboard portion of the right wing was found about 150 feet from the main impact crater. An examination revealed the right wing had failed near the production seam. The right spar exhibited features 'typical of an upward bending overstress separation.' Examination revealed no other evidence of preimpact aircraft or engine malfunction. The airplane's gross weight was estimated to be about 4,696 pounds; its max limit was 4,300 pounds. The pilot's logbook indicated that he had flown only 2 instrument approaches in the previous 14 months. All three occupants were killed.
Probable cause:
Failure of the pilot to maintain control of the airplane, while climbing in instrument meteorological conditions (IMC) after takeoff. Factors related to the accident were: fog, low ceiling, the pilot's lack of recent instrument experience, and the excessive gross weight of the airplane.
Final Report:

Crash of a Learjet 35A in Fresno: 4 killed

Date & Time: Dec 14, 1994 at 1146 LT
Type of aircraft:
Operator:
Registration:
N521PA
Flight Type:
Survivors:
No
Schedule:
Fresno - Fresno
MSN:
35-239
YOM:
1979
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
7109
Captain / Total hours on type:
2747.00
Aircraft flight hours:
6673
Aircraft flight cycles:
5254
Circumstances:
At about 1146 pst, Learjet 35A, N521PA, operating as a public use aircraft, crashed in Fresno, CA. Operating with call sign Dart 21, the flightcrew had declared an emergency inbound to Fresno Air Terminal due to engine fire indications. They flew the airplane toward a right base for their requested runway, but the airplane continued past the airport. The flightcrew was heard on tower frequency attempting to diagnose the emergency conditions and control the airplane until it crashed, with landing gear down, on an avenue in fresno. Both pilots were fatally injured. Twenty-one persons on the ground were injured, and 12 apartment units in 2 buildings were destroyed or substantially damaged by impact or fire. Investigation revealed that special mission wiring was not installed properly, leading to a lack of overload current protection. The in-flight fire most likely originated with a short of the special mission power supply wires in an area unprotected by current limiters. The fire resulted in false engine fire warning indications to the pilots that led them to a shutdown of the left engine. An intense fire burned through the aft engine support beam, damaging the airplane structure and systems in the aft fuselage and may have precluded a successful emergency landing.
Probable cause:
The accident was the consequence of the following factors:
- Improperly installed electrical wiring for special mission operations that led to an in-flight fire that caused airplane systems and structural damage and subsequent airplane control difficulties,
- Improper maintenance and inspection procedures followed by the operator,
- Inadequate oversight and approval of the maintenance and inspection practice by the operator in the installation of the special mission systems.
Final Report: