Crash of a Lockheed P-2H Neptune at Otis AFB

Date & Time: Dec 3, 1967
Type of aircraft:
Operator:
Registration:
148350
Flight Type:
Survivors:
Yes
MSN:
726-7235
YOM:
1958
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed on landing at Otis AFB and came to rest in flames. There were no casualties but the aircraft was destroyed by fire.

Crash of a Rockwell Aero Commander 680FL in North Platte

Date & Time: Dec 2, 1967 at 2040 LT
Operator:
Registration:
N747NT
Flight Phase:
Survivors:
Yes
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1940
Captain / Total hours on type:
10.00
Circumstances:
Shortly after a night takeoff from North Platte-Lee Bird Airport, while in initial climb, both engines failed simultaneously. The pilot informed ground about his situation and decided to return to the airport for an emergency landing. Few second later, he realized he could not make it so he ditched the airplane into lake Maloney located 7 miles southwest of the airport. While the aircraft was destroyed, the pilot was seriously injured.
Probable cause:
Poor preflight preparation on part of the pilot who failed to secure the fuel cap after he proceed to the aircraft refueling prior to takeoff. This caused the fuel to leak between the parking and takeoff and during initial climb, both engines failed simultaneously due to fuel starvation.
Final Report:

Crash of a Learjet 23 in Orlando: 3 killed

Date & Time: Nov 29, 1967 at 2318 LT
Type of aircraft:
Registration:
N690LJ
Survivors:
No
Schedule:
Jacksonville – Miami
MSN:
23-078
YOM:
1965
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
3000
Captain / Total hours on type:
700.00
Circumstances:
On a leg from Jacksonville to Miami, the crew encountered technical problems and decided to divert to Orlando-Herndon Airport. While on a night approach, the airplane became uncontrollable and crashed onto a house located short of runway threshold. The aircraft was destroyed and all three occupants were killed while no one on the ground was injured.
Probable cause:
It was determined that the loss of control on final was the consequence of an insufficient speed as the pilot failed to maintain flying speed. A failure of a fuel pump forced the crew to modify his route and this was the result of a faulty maintenance and servicing.

Crash of a Vickers 745D Viscount in Raleigh

Date & Time: Nov 28, 1967 at 2100 LT
Type of aircraft:
Operator:
Registration:
N7465
Survivors:
Yes
MSN:
231
YOM:
1957
Crew on board:
4
Crew fatalities:
Pax on board:
39
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8862
Captain / Total hours on type:
3982.00
Circumstances:
After touchdown at Raleigh-Durham Airport by night, the nosewheel collapsed. The airplane slid on the runway for several yards until it came to rest. All 43 occupants escaped uninjured while the aircraft was later considered as damaged beyond repair.
Probable cause:
Failure of the nosewheel steering system upon touchdown due to fatigue fracture. A valve body on the nosewheel steering jack twin valve failed, causing oscillations.
Final Report:

Crash of a Cessna 401 in Whitefield: 1 killed

Date & Time: Nov 26, 1967 at 1250 LT
Type of aircraft:
Registration:
N3280Q
Flight Phase:
Survivors:
No
MSN:
401-0080
YOM:
1967
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4600
Captain / Total hours on type:
9.00
Circumstances:
While in cruising altitude, the twin engine aircraft went out of control, entered a dive and crashed in an isolated area located in the region of Whitefield. The wreckage was found two days later. The aircraft was totally destroyed and the pilot, sole on board, was killed.
Probable cause:
The exact cause of the accident could not be determined with certainty. However, the phenomena observed at autopsy considered the results of impact injuries.
Final Report:

Crash of a Beechcraft C-45H Expeditor in Sanger: 3 killed

Date & Time: Nov 25, 1967 at 0405 LT
Type of aircraft:
Registration:
N9450Z
Flight Type:
Survivors:
No
MSN:
AF-247
YOM:
1952
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
2200
Captain / Total hours on type:
1400.00
Circumstances:
On a night approach to Sanger Airport, the copilot informed ground about an engine failure. The crew was unable to maintain a safe altitude when the airplane stalled and crashed few miles short of runway. All three occupants were killed. At the time of the accident, the airplane was approximately 827 lbs above gross weight.
Probable cause:
Powerplant failure for undetermined reason. Inadequate preflight preparation on part of the flying crew and improperly loaded aircraft (weight and/or CofG).
Final Report:

Crash of a Beechcraft Queen Air A80 in Concan

Date & Time: Nov 22, 1967 at 1700 LT
Type of aircraft:
Operator:
Registration:
N899Q
Flight Type:
Survivors:
Yes
MSN:
LD-46
YOM:
1962
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3050
Captain / Total hours on type:
380.00
Circumstances:
On final approach to Concan-Angermiller Airport, the twin engine aircraft struck power cables, stalled and crashed in flames in an open field short of runway. The aircraft was destroyed and all five occupants were injured.
Probable cause:
The pilot failed to see and avoid unmarked TV cable.
Final Report:

Crash of a Convair CV-880-22-1 in Cincinnati: 70 killed

Date & Time: Nov 20, 1967 at 2057 LT
Type of aircraft:
Operator:
Registration:
N821TW
Survivors:
Yes
Schedule:
Los Angeles - Cincinnati - Pittsburgh - Boston
MSN:
22-00-27
YOM:
1961
Flight number:
TW128
Crew on board:
7
Crew fatalities:
Pax on board:
75
Pax fatalities:
Other fatalities:
Total fatalities:
70
Captain / Total flying hours:
12895
Captain / Total hours on type:
1389.00
Copilot / Total flying hours:
2647
Copilot / Total hours on type:
447
Aircraft flight hours:
18850
Circumstances:
Flight 128 was a scheduled domestic flight from Los Angeles International Airport, California, to Boston, Massachusetts, with intermediate stops at Cincinnati, Ohio and Pittsburgh, Pennsylvania. The departure from Los Angeles was delayed due to an equipment change but the aircraft was airworthy at the time of departure. The only carry- over discrepancy was an inoperative generator which had no bearing on this accident. The flight took off from Los Angeles at 1737 hours Eastern Standard Time. The descent into the Cincinnati area from cruising altitude was delayed due to conflicting traffic and was initiated closer to the destination than normal. It required the crew to conduct the descent with a higher than normal rate toward the initial approach fix. The crew discussed the technique they were going to use to increase the rate of descent, and evidence revealed that they were relaxed, unworried and operating within the established operating limits of the aircraft. As the flight reported leaving 15 500 ft remarks were made in the cockpit about the rapidity of the descent and the hope, apparently with reference to the underlying cloud conditions, that it would be a thin layer. The crew checked the anti-icing equipment and conversations after that time indicated that they were not aware of any discrepancies regarding that system. Control of the flight was normal until the flight was turned over to the approach controller who failed to provide the crew with the current altimeter setting of 30.07 in Hg instead of 30.06 previously given to the crew. However, shortly after the crew intercepted a transmission to another aircraft containing the current altimeter setting of 30.07 they set and cross-checked that setting on their altimeters. Throughout the descent, the co-pilot called out the appropriate warnings to the pilot-in-command as the aircraft approached assigned altitudes and apparently performed all of his assigned duties without prompting by the pilot-in-command. Crew coordination was very good during that portion of the flight. The weather conditions in the Cincinnati area were such that the crew should have established visual contact with the ground by the time they reached 3 000 to 4 000 ft. As the flight approached the final fix, approximately 7 minutes before the accident, the crew was given the latest reported weather which indicated that the ceiling was approximately 1 000 ft and the visibility was 13 miles in snow and haze. Approximately 1 minute later they were reminded that the ILS glide slope was out of service, as well as the middle marker beacon and the approach lights. The crew acknowledged receipt of this information and planned their approach to the proper minimum altitude of 1 290 ft AMSL, 400 ft above the ground, to allow for these outages. From this point in the approach to the outer marker, the aircraft altitudes and headings were in general agreement with altitudes reported by the crew and the headings they were instructed to fly. Operation of the aircraft was normal and the proper configuration was established for the approach to the outer marker in accordance with the company's operating instructions. The crew reported over the outer marker at 2056 hours and were cleared to land on runway 18 and advised that the wind was 090°/8 kt and the RVR more than 6 000 ft (see Fig. 22-1). The co-pilot reported to the pilot-in-command that they were past the marker and that there was no glide slope. The pilot-in-command acknowledged this and stated ". . . We gotta go down to, ah, four hundred, that would be, ah." At this point, the co-pilot supplied the information "twelve ninety" and the pilot-in-command repeated "twelve ninety." The flight had arrived at the outer marker with the landing gear down, the flaps set at 40' down at an altitude of approximately 2 340 it and at an airspeed of approximately 200 kt. (The prescribed minimum altitude over the outer marker beacon, 4 miles from the threshold, was 1 973 ft AMSL). After the aircraft passed the outer marker, a rate of descent of 1 800 ft/min was established at an airspeed of about 190 kt. The rate of descent was greater than that recommended by the company for an instrument approach and remained nearly constant until approximately 20 sec before the first recorded sound of impact. At that time the rate increased to approximately 3 000 ft/min coincident with a request for 50° flaps, and a decrease in thrust, and then decreased to about 1 800 ft/min until about 5 sec before the initial contact. Prior to initial contact, the aircraft was rotated to a virtually level attitude, the rate of descent was decreasing, the airspeed was about 191 kt, and the indicated altitude was about 900 ft AMSL. The aircraft first struck small tree limbs at an elevation of approximately 875 ft AMSL, 9 357 it short of the approach end of runway 18 and 429 it right of the extended runway centre line. After several more impacts with trees and the ground, the aircraft came to rest approximately 6 878 it from the runway and 442 ft right of the extended runway centre line and burst into flames. A stewardess who survived the accident stated that the first noticeable impact felt like a hard landing. None of the survivors recalled any increase of engine power or felt any rotation of the aircraft. The accident occurred at 2057 hours during darkness in an area where snow was falling. Five crew members and 65 passengers were killed while 12 other occupants were seriously injured.
Probable cause:
The Board determined that the probable cause of this accident was an attempt by the crew to conduct a night, visual, no-glide-slope approach during deteriorating weather conditions without adequate altimeter cross reference. The approach was conducted using visual reference to partially lighted irregular terrain which may have been conducive to producing an illusionary sense of adequate terrain clearance.
Final Report:

Crash of a Boeing 707-131 in Cincinnati: 1 killed

Date & Time: Nov 6, 1967 at 1841 LT
Type of aircraft:
Operator:
Registration:
N742TW
Flight Phase:
Survivors:
Yes
Schedule:
New York – Cincinnati – Los Angeles
MSN:
17669
YOM:
1959
Flight number:
TW159
Crew on board:
7
Crew fatalities:
Pax on board:
29
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
18753
Captain / Total hours on type:
6204.00
Copilot / Total flying hours:
1629
Copilot / Total hours on type:
830
Aircraft flight hours:
26319
Circumstances:
TWA Flight 159 was a scheduled domestic flight from New York to Los Angeles with an intermediate stop at the Greater Cincinnati Airport. It departed the ramp at Cincinnati at 1833 hours Eastern Standard Time. As it was approaching runway 27L for take-off, Delta Air Lines, Inc., DC-9, N-3317L, operating as Flight DAL 379, was landing. As DAL 379 was completing its landing roll, the crew requested and received clearance for a 180° turnaround on the runway in order to return to the intersection of runway 18-36 which they had just passed. After turning through approximately 90°, the nosewheel slipped off the paved surface and the aircraft moved straight ahead off the runway during which time it became mired. The throttles were retarded to idle, and power was not increased again. At 1839:05 hours as DAL 379 was in the process of clearing the runway, TWA 159 was cleared for take-off. The local controller testified that before TWA 159 began moving, he observed that DAL 379 had stopped. He stated that although DAL 379 appeared to be clear of the runway, he requested confirmation from the crew who replied, "Yeah, we're in the dirt, though." Following this report the controller stated "TWA 159 he's clear of the runway, cleared for take-off, company jet on final behind you." Take- off performance had been computed as V1 132 knots, VR 140 knots, V2 150 knots. In fact DAL 379 was stopped on a heading of 004' and located 4 600 ft from the threshold of runway 27L with its aft-most point being approximately 7 ft north of the runway edge, the aft-most exterior lights located on the wing tip and the upper and lower anti-collision lights being approximately 45 ft from the runway edge. The crew of TWA 159 did not have DAL 379 in sight when they commenced the take-off roll. The co-pilot was performing the take-off and the pilot-in-command drew his attention to DAL 379 as the aircraft appeared in their landing lights they could see that it was off the runway by Some 5-7 ft. As TWA 159 passed abeam of DAL 379 the co-pilot experienced a movement of the flight controls and the aircraft yawed. Simultaneously there was a loud bang from the right side of the aircraft. The last airspeed he had observed was 120 knots and assuming that the aircraft was at or near V1, and that a collision had occurred, he elected to abort the take-off . He stated that he closed the power levers, placed them in full reverse, applied maximum braking, and called for the spoilers which the pilot-in-command operated. Directional control was maintained but the aircraft ran off the end of the runway, rolled across the terrain for approximately 225 ft, to the brow of a hill, and became airborne momentarily. It next contacted the ground approximately 67 ft further down the embankment, the main landing gear was torn off and the nosewheel was displaced rearward, forcing the cabin floor upward by approximately 15 in. The aircraft slid down the embankment and came to rest on a road approximately 421 ft from the end of the runway. The accident occurred at approximately 1841 hours, in darkness. A passenger was killed, another was seriously injured, five others were slightly injured. The aircraft was written off.
Probable cause:
The Board determined that the probable cause of the accident was the inability of the TWA crew to abort successfully their take-off at the speed attained prior to the attempted abort. The abort was understandably initiated because of the co-pilot's belief that his plane had collided with a Delta aircraft stopped just off the runway. A contributing factor was the action of the Delta crew in advising the tower that their plane was clear of the runway without carefully ascertaining the facts, and when in fact their aircraft was not at a safe distance under the circumstance of another aircraft taking off on that runway.
Final Report:

Crash of a Rockwell Aero Commander 560 in Calhoun: 2 killed

Date & Time: Nov 4, 1967 at 0815 LT
Operator:
Registration:
N2677B
Flight Phase:
Flight Type:
Survivors:
No
MSN:
560-177
YOM:
1954
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
4169
Captain / Total hours on type:
1293.00
Circumstances:
While in cruising altitude, on a positioning flight, the landing gear were lowered and the flaps were positioned to a full down angle. The twin engine airplane entered an uncontrolled descent until it crashed near Calhoun. Both occupants were killed.
Probable cause:
The exact cause of the loss of control could not be determined with certainty.
Final Report: