Crash of a Bristol 170 Freighter Mk 31M in Enstone

Date & Time: Jul 18, 1996 at 1135 LT
Type of aircraft:
Registration:
C-FDFC
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Enstone - Bristol
MSN:
13218
YOM:
1954
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
11000
Captain / Total hours on type:
1300.00
Copilot / Total hours on type:
60
Circumstances:
The weather at the departure airfield consisted of a light and variable wind, good visibility and a temperature of 20ºC. At the start of the take-off run the aircraft, which was being flown by the copilot, who is also an experienced pilot with some 60 hours on type, began to swing to the right. Corrective action caused it to swing to the left but, after further correction,the aircraft continued accelerating and swing to the right. The Bristol Freighter is well known for its tendency to swing on takeoff. The commander joined the co-pilot on the controls and attempted to assist in correcting the right-hand swing. It became apparent to the pilots that they would be unable to prevent the aircraft running over the edge of the runway and, as there were people standing by the edge and a small control tower building behind them, they applied full up-elevator in an effort to avoid a collision. Because of the low airspeed at which this occurred, the aircraft stalled and the left wing tip hit the ground. This caused the aircraft to turn so that it was then travelling sideways which resulted in the landing gear collapsing as it touched the runway. The aircraft then slid off the runway onto the grass. There was no fire and the only injuries were sustained by three of the aircraft passengers.
Final Report:

Crash of a De Havilland DHC-5D Buffalo in Nairobi: 5 killed

Date & Time: Jul 17, 1996
Type of aircraft:
Operator:
Registration:
JW9022
Flight Phase:
Flight Type:
Survivors:
No
MSN:
94
YOM:
1979
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
Crashed on takeoff for unknown reasons, killing all five crew members.

Crash of a De Havilland DHC-4 Caribou in Kalemie

Date & Time: Jul 17, 1996
Type of aircraft:
Registration:
9Q-CUB
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
212
YOM:
1964
Location:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was completing a humanitarian flight when the aircraft crashed in unknown circumstances shortly after takeoff. Both pilots were injured.

Crash of a Boeing E-3A Sentry in Preveza

Date & Time: Jul 14, 1996
Type of aircraft:
Registration:
LX-N90457
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Preveza - Geilenkirchen
MSN:
22852
YOM:
1984
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
11
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft was completing a flight from Preveza to the Geilenkirchen NATO Air Base in Germany. During the takeoff roll at Preveza-Aktion Airport, after V1 speed, the pilot-in-command heard a loud noise. Thinking this was the consequence of a bird strike, he decided to abandon the takeoff procedure and started an emergency braking manoeuvre. Unable to stop within the remaining distance, the aircraft overran, struck a dyke and came to rest partially submerged in the sea. All 16 occupants escaped uninjured.
Probable cause:
Investigations revealed there were no indications of a possible bird strike during takeoff.

Crash of a Piper PA-46-310P Malibu in Hartford

Date & Time: Jul 12, 1996 at 1115 LT
Registration:
N234DM
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Hartford – Block Island
MSN:
46-8408043
YOM:
1984
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4918
Captain / Total hours on type:
488.00
Circumstances:
The pilot reported that he performed a rolling takeoff from the 2315 ft runway. He said that as soon as the airplane broke ground on the takeoff roll, he experienced a loss of engine power. The pilot said that he retracted the gear to help clear a 42 ft dike at the departure end of the runway. Also, he reported that after clearing the dike, he turned gradually to the left, and the left wing stalled. Two witnesses reported hearing loud, steady sounds from the airplane's engine and propeller. They said they saw the airplane in a high nose-up attitude, and watched the airplane descend behind the dike. The engine could be heard until the airplane contacted the river. During an operational check after the accident, the engine performed at recommended levels. According to performance data provided by the FAA, at the given takeoff weight, with a zero degree flap setting, the airplane required 2850 feet of runway to clear a 50 ft obstacle. The charts were based on full power before brake release.
Probable cause:
The pilot's inadequate preflight planning/preparation, and his failure to attain the proper liftoff airspeed, which resulted in a stall and collision with the terrain (river).
Final Report:

Crash of an Avro 748-402-2B in Ambon

Date & Time: Jul 11, 1996 at 0900 LT
Type of aircraft:
Operator:
Registration:
PK-IHN
Flight Phase:
Survivors:
Yes
Schedule:
Ambon - Manado
MSN:
1794
YOM:
1983
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
43
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
During the takeoff roll at Ambon-Pattimura Airport, just before Vr, one of the engine failed. The captain abandoned the takeoff procedure and initiated an emergency braking manoeuvre. Unable to stop with the remaining distance (the runway surface was wet), the aircraft overran and came to rest 180 metres further against a dyke. All 48 occupants evacuated safely while the aircraft was damaged beyond repair.

Crash of a Beechcraft 65 Queen Air in Campbellsville

Date & Time: Jun 30, 1996 at 1240 LT
Type of aircraft:
Registration:
N3870C
Flight Phase:
Survivors:
Yes
MSN:
LC-212
YOM:
1966
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3500
Captain / Total hours on type:
100.00
Aircraft flight hours:
2549
Circumstances:
According to an FAA inspector, the airplane '...was unable to get airborne...' during the takeoff roll. He stated that after travelling the full length of the 4,997-foot runway, the airplane ran off the departure end of runway 5 and continued approximately 2,257 feet through an open field, a fence, a corn field and into a depression where it impacted terrain and came to rest. The pilot reported that during the takeoff roll he discovered that he had not removed the gust lock from the control column and that his attempts to remove it were unsuccessful. The pilot stated that the aircraft '...went off the end of the runway through a fence and impacted an earthen berm that collapsed the gear [and] blade strikes that stopped the engines.'
Probable cause:
The pilot's inadequate preflight preparation, his failure to remove the control lock, and his failure to abort the takeoff.
Final Report:

Crash of a Douglas DC-3A-S1C3G in Conroe

Date & Time: Jun 20, 1996 at 1408 LT
Type of aircraft:
Registration:
N23WT
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Conroe - Conroe
MSN:
11650
YOM:
1943
Location:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
16500
Captain / Total hours on type:
707.00
Aircraft flight hours:
51307
Circumstances:
During initial takeoff climb the copilot who was manipulating the controls called for METO (maximum except takeoff) power. After the pilot-in-command set METO power, the left engine lost power. The PIC took the controls from the copilot and called for him to feather the left propeller. The copilot did not hear the call to feather the left propeller. Maintaining an indicated airspeed of 90 knots and wings level attitude, the airplane descended into trees and impacted a rural residential paved street. The cockpit area and main fuselage were consumed by a post crash fire. Examination of the throttle quadrant revealed the propeller control levers were forward, the mixture control levers were autorich, the throttle for the right engine was forward, and the throttle for the left engine was at idle. According to a FAA operations inspector maintaining 90 knots with the propeller not feathered would result in the aircraft descending. The pilot and copilot had not completed a proficiency check or flight check for the DC3 type aircraft within the previous 24 months. Examination of the left engine did not disclose any preexisting anomalies.
Probable cause:
The flight instructor's failure to use the single engine best angle of climb airspeed resulting in a loss of control of the aircraft. Factors were the loss of power to the left engine for undetermined reasons, the flight instructor not being qualified to be pilot-in-command in the DC3, his lack of recent experience in the DC3, and the lack of suitable terrain for the forced landing.
Final Report:

Crash of a PZL-Mielec AN-2TP in Georgetown

Date & Time: Jun 20, 1996 at 0950 LT
Type of aircraft:
Operator:
Registration:
N67AN
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Georgetown - Georgetown
MSN:
1G88-13
YOM:
1967
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7000
Captain / Total hours on type:
50.00
Circumstances:
During departure climb, the airplane experienced a loss of engine power. Emergency procedures were executed and a forced approach/landing was initiated to a field. While on the approach, the pilot observed a ditch running across the proposed landing pathway. He turned the airplane right to parallel the ditch. During the landing roll, the pilot attempted to avoid a building by intentionally ground looping the airplane. During this avoidance maneuver, the left wing struck the building. Examination of the airplane revealed that the engine had seized due to an internal failure. The reason for the engine's internal failure was not determined.
Probable cause:
Engine seizure for undetermined reasons. A factor was the lack of suitable terrain for the forced landing.
Final Report:

Crash of a Douglas DC-10-30 in Fukuoka: 3 killed

Date & Time: Jun 13, 1996 at 1208 LT
Type of aircraft:
Operator:
Registration:
PK-GIE
Flight Phase:
Survivors:
Yes
Schedule:
Fukuoka – Denpasar – Jakarta
MSN:
46685
YOM:
1979
Flight number:
GA865
Country:
Region:
Crew on board:
15
Crew fatalities:
Pax on board:
260
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
10263
Captain / Total hours on type:
2641.00
Copilot / Total flying hours:
3910
Copilot / Total hours on type:
1437
Aircraft flight hours:
46325
Circumstances:
During the takeoff roll at Fukuoka-Itazuke Airport runway 16, at a speed of 158 knots, the captain started the rotation. During initial climb, at a height of about 3 metres, the right engine suffered a loss of power after a fan blade located on the 1st stage of the high pressure compressor disk separated. The N1 dropped to 23,7% and five seconds later, the flight engineer informed the crew about the failure of the engine n°1. The captain decided to abort the takeoff and landed back on runway. The aircraft contacted ground with a vertical acceleration of 2,1 g then thrust reversers were deployed and ground spoilers were extended. Unable to stop within the remaining distance, the aircraft overran, crossed a road, skidded for about 620 metres before coming to rest in an open field, bursting into flames. Three passengers were killed.
Probable cause:
Although the CAS was well in excess of V1 and the aircraft had already lifted off from the runway, the takeoff was aborted. Consequently the aircraft departed the end of the runway, came to rest and caught fire. It is estimated that contributing to the rejection of the takeoff under this circumstance was the fact that the CAP's judgement in the event of the engine failure was inadequate. Investigation revealed that the turbine blade that failed, had operated for 30913 hours and 6182 cycles. General Electric had advised customers to discard blades after about 6000 cycles.
Final Report: