Crash of a Convair C-131B Samaritan off Miami: 1 killed

Date & Time: Feb 8, 2019 at 1216 LT
Type of aircraft:
Operator:
Registration:
N145GT
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Nassau - Miami
MSN:
256
YOM:
1955
Flight number:
QAI504
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
23000
Captain / Total hours on type:
725.00
Copilot / Total flying hours:
650
Copilot / Total hours on type:
305
Aircraft flight hours:
12701
Circumstances:
According to the first officer, during the first cargo flight of the day, the left engine propeller control was not working properly and the captain indicated that they would shut down the airplane and contact maintenance if the left engine propeller control could not be reset before the return flight. For the return flight, the engines started normally, and both propellers were cycled. The captain and the first officer were able to reset the left propeller control, so the airplane departed with the first officer as the pilot flying. The takeoff and initial climb were normal; however, as the airplane climbed through 4,000 ft, the left engine propeller control stopped working and the power was stuck at 2,400 rpm. The captain tried to adjust the propeller control and inadvertently increased power to 2,700 rpm. The captain then took control of the airplane and tried to stabilize the power on both engines. He leveled the airplane at 4,500 ft, canceled the instrument flight rules flight plan, and flew via visual flight rules direct toward the destination airport. The first officer suggested that they return to the departure airport, but the captain elected to continue as planned (The destination airport was located about 160 nautical miles from the departure airport). The first officer's postaccident statements indicated that he did not challenge the captain's decision. When the flight began the descent to 1,500 ft, the right engine began to surge and lose power. The captain and the first officer performed the engine failure checklist, and the captain feathered the propeller and shut down the engine. Shortly afterward, the left engine began to surge and lose power. The captain told the first officer to declare an emergency. The airplane continued to descend, and the airplane impacted the water "violently," about 32 miles east of the destination airport. The captain was unresponsive after the impact and the first officer was unable to lift the captain from his seat. Because the cockpit was filling rapidly with water, the first officer grabbed the life raft and exited the airplane from where the tail section had separated from the empennage. The first officer did not know what caused both engines to lose power. The airplane was not recovered from the ocean, so examination and testing to determine the cause of the engine failures could not be performed. According to the operator, the flight crew should have landed as soon as practical after the first sign of a mechanical issue. Thus, the crew should have diverted to the closest airport when the left engine propeller control stopped working and not continued the flight toward the destination airport.
Probable cause:
The captain's decision to continue with the flight with a malfunctioning left engine propeller control and the subsequent loss of engine power on both engines for undetermined reasons, which resulted in ditching into the ocean. Contributing to the accident was the first officer's failure to challenge the captain's decision to continue with the flight.
Final Report:

Crash of a Convair C-131E Samaritan in Saint Johns: 4 killed

Date & Time: Feb 5, 1996 at 0950 LT
Type of aircraft:
Registration:
N131T
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Saint Johns – Brownsville – Chetumal
MSN:
338
YOM:
1956
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
18400
Captain / Total hours on type:
8.00
Aircraft flight hours:
18715
Circumstances:
Witnesses observed the aircraft departing from runway 14 with a rolling start. They said the aircraft rotated at the departure end of the runway and remained in ground effect with an excessive, nose high attitude. It then struck the airport perimeter fence, a barrier wall, and power lines. Power line wires were dragged through a residential area, resulting in additional damage. The airplane then crashed in a pasture and burned. Investigation revealed the airplane had been loaded to a gross weight (GW) of 50,870 lbs. Its maximum GW was limited to 48,000 lbs at sea level with the use of antidetonation injection (ADI) fluid and 40,900 lbs without ADI. Density altitude at the airport was 6200 feet. For conditions at the airport, maximum GW for takeoff with ADI and 15° of flaps was 43,205 lbs; without ADI and with 13 degrees of flaps, maximum GW was 38,909 lbs. The airplane flaps were found in the retracted position, but there was no performance data for takeoff with the flaps retracted. No ADI fluid was found in the line to the right engine, although it was intact; the ADI tank was destroyed; the ADI line to the left engine was damaged. The airplane was being flown under provision of a ferry permit, which did not provide for the cargo or the two passengers that were aboard. The first pilot (PIC) had accrued about 8 hours of flight experience in the make and model of airplane.
Probable cause:
Inadequate preflight planning and preparation by the first pilot (PIC), his failure to ensure the aircraft was properly loaded within limitations, his failure to use proper flaps for takeoff, his failure to use ADI assisted takeoff, and his resultant failure to attain sufficient airspeed to climb after takeoff. Factors relating to the accident were: the high density altitude, and the PIC's lack of experience in the make and model of airplane.
Final Report:

Crash of a Convair VC-131H Samaritan at Dothan AFB: 4 killed

Date & Time: Nov 15, 1985
Type of aircraft:
Operator:
Registration:
542817
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Dothan - Dothan
MSN:
221
YOM:
1955
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The crew (two pilots and two engineers) departed Dothan AFB for a local post maintenance test flight. Just after liftoff, the elevators jammed. The aircraft went out of control and crashed. All four occupants were killed.
Probable cause:
Elevators jammed on takeoff for unknown reasons.

Crash of a Convair C-131F Samaritan off Jacksonville NAS: 14 killed

Date & Time: Apr 30, 1983 at 1209 LT
Type of aircraft:
Operator:
Registration:
141010
Flight Type:
Survivors:
Yes
Schedule:
Jacksonville – Guantánamo
MSN:
293
YOM:
1955
Crew on board:
6
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
14
Circumstances:
After takeoff from Jacksonville-Towers Field NAS, while climbing, the left engine failed. The crew declared an emergency and was cleared to return. On final approach, the airplane crashed in the St Johns River about 125 yards short off shore. The aircraft came to rest in shallow waters and was destroyed. A passenger was rescued while 14 other occupants were killed.
Probable cause:
Failure of the left engine during initial climb or unknown reasons.

Crash of a Convair HC-131A Samaritan in Corpus Christi

Date & Time: Jan 18, 1982
Type of aircraft:
Operator:
Registration:
52-5786
Flight Type:
Survivors:
Yes
Schedule:
Corpus Christi - Corpus Christi
MSN:
53-6
YOM:
1954
Crew on board:
8
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was completing a local training flight at Corpus Christi Airport. Following an approach in reduced visibility due to foggy conditions, the airplane landed hard on runway 10R. Upon touchdown, the aircraft went out of control, veered off runway and came to rest. All eight crew members evacuated safely while the aircraft was damaged beyond repair.

Crash of a Convair C-131E Samaritan in Dillingham

Date & Time: Jun 4, 1981 at 1617 LT
Type of aircraft:
Registration:
N121CA
Flight Type:
Survivors:
Yes
Schedule:
Dillingham - Anchorage
MSN:
342
YOM:
1956
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9500
Captain / Total hours on type:
630.00
Circumstances:
After takeoff from Dillingham Airport, while on a company ferry flight to Anchorage, the right engine surged at meto power and the crew was forced to shut it down. The decision to return was taken and the crew followed a circuit pattern then started the descent. On final approach, the airplane descended into trees and crashed in a wooded area located few hundred yards short of runway 01. The aircraft was destroyed while all three occupants escaped with minor injuries.
Probable cause:
Engine malfunction during initial climb after exhaust stacks failed. The following contributing factors were reported:
- Material failure,
- Leak,
- Power indicators failure,
- Governors malfunction,
- Overheated, erratic,
- The pilot-in-command failed to follow approved procedures,
- Right engine fire warning light during takeoff,
- Engine surged at meto power,
- Exhaust stack broken,
- Bmep conduit overheated.
Final Report: