Crash of a Rockwell Grand Commander 690 off Chicago: 4 killed

Date & Time: Apr 23, 1977 at 1550 LT
Registration:
N847
Flight Phase:
Survivors:
No
Schedule:
Chicago - Harrisburg
MSN:
690-11140
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
6707
Captain / Total hours on type:
1200.00
Circumstances:
After takeoff from Chicago-Merrill C. Meigs Airport, while climbing, the airplane collided with a flock of seagulls. An engine lost power and the airplane lost speed and height. The pilot elected to return when the airplane stalled and crashed into Lake Michigan. The aircraft was destroyed and all four occupants were killed.
Probable cause:
Stall and spin after the airplane collided with a flock of seagulls. The following contributing factors were reported:
- Exercised poor judgment,
- Bird ingestion,
- Failed to maintain flying speed,
- Airport supervisory personnel,
- Improper emergency procedures,
- Pilot advised of seagulls on runway,
- Ineffective bird removal technique,
- Failed to retract flaps.
Final Report:

Crash of a Beechcraft 200 Super King Air in Ruddock: 5 killed

Date & Time: Apr 18, 1977 at 2207 LT
Operator:
Registration:
N256TM
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
New Orleans - New Orleans
MSN:
BB-96
YOM:
1976
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
2900
Captain / Total hours on type:
580.00
Circumstances:
The twin engine airplane departed New Orleans-Moisant in the evening for a local test flight. In unknown circumstances, it went out of control and crashed in water near Ruddock, about 16,7 miles northwest of Moisant Airport. The aircraft was destroyed and all five occupants were killed.
Probable cause:
The exact cause of the accident could not be determined. Unauthorized flight.
Final Report:

Ground accident of a Cessna 207 Skywagon in Wausau

Date & Time: Apr 15, 1977 at 0850 LT
Operator:
Registration:
N1567U
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Wausau - Milwaukee
MSN:
207-0167
YOM:
1970
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
566
Captain / Total hours on type:
550.00
Circumstances:
While parked at Wausau Airport, the engine was started when the airplane departed its parking place, rolled for few yards and eventually collided with a tree. The pilot who was not on board was uninjured while the aircraft was damaged beyond repair.
Probable cause:
Ground collision with tree after the pilot started the engine without proper ground assistance. The following contributing factors were reported:
- The pilot rotated propeller by hand,
- The pilot failed to turn magnetos off,
- The pilot failed to set brakes prior to start the engine.
Final Report:

Crash of a Nord 262A-27 in Reading: 3 killed

Date & Time: Apr 9, 1977 at 1356 LT
Type of aircraft:
Operator:
Registration:
N7886A
Flight Type:
Survivors:
No
Schedule:
Philadelphia - Reading
MSN:
47
YOM:
1968
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
The crew was completing a ferry flight from Philadelphia to Reading. 54 seconds after being cleared for an approach to runway 31 at Reading-General Spaatz Airport, while flying at an altitude of 4,500 feet, the twin engine airplane collided with a Cessna 195 registered N4377N and owned by the Hagerstown Cash Register Company. His pilot was performing a private flight from Lincoln Park to York, Pennsylvania. Following the collision, both aircraft went out of control, entered a dive and crashed. All four occupants on both aircraft were killed.
Probable cause:
Inflight collision while descending to Reading Airport after the pilot-in-command failed to see and avoid other aircraft. The following contributing factors were reported:
- Pilot of other aircraft,
- Not under radar contact,
- No control area.
Final Report:

Crash of a Convair CV-240-0 in Hyannis

Date & Time: Apr 9, 1977 at 1315 LT
Type of aircraft:
Registration:
N10AV
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Hyannis - Hyannis
MSN:
8
YOM:
1947
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
15774
Captain / Total hours on type:
600.00
Circumstances:
The airplane departed Hyannis-Barnstable Airport for a local private flight. While flying at an altitude of about 500 feet, the right engine failed. Due to populated area around his position, the captain decided to attempt an emergency landing on a beach. Upon landing, the airplane struck huge boulders and crashed. All five occupants were injured and the airplane was damaged beyond repair.
Probable cause:
Engine failure caused by ice in fuel. The following contributing factors were reported:
- Collision with objects,
- Inadequate preflight preparation,
- Mismanagement of fuel,
- Ice in fuel,
- Forced landing off airport on land,
- Ice in right fuel tank, crossfeed on,
- Boost pumps on tank valves both on.
Final Report:

Crash of a Mitsubishi MU-2B-30 Marquise in New York: 7 killed

Date & Time: Apr 5, 1977 at 1431 LT
Type of aircraft:
Registration:
N888RJ
Flight Type:
Survivors:
Yes
Schedule:
Somerset - LaGuardia
MSN:
542
YOM:
1971
Crew on board:
1
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
13500
Circumstances:
While approaching LaGuardia Airport in poor weather conditions (low ceiling and fog), both engines failed. The pilot lost control of the airplane that crashed at Pelham Bay Park, Bronx, about five miles north of the airport. A passenger was seriously injured while seven other occupants were killed.
Probable cause:
Double engine failure on approach due to fuel exhaustion. The following contributing factors were reported:
- Inadequate preflight preparation,
- Mismanagement of fuel,
- Fuel exhaustion,
- Low ceiling,
- Fog,
- Fuel quantity gauge - erratic.
Final Report:

Crash of a Mitsubishi MU-2-25 Marquise in Detroit

Date & Time: Apr 4, 1977 at 2004 LT
Type of aircraft:
Operator:
Registration:
N321MA
Survivors:
Yes
Schedule:
Boston - Detroit
MSN:
276
YOM:
1973
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2993
Captain / Total hours on type:
144.00
Circumstances:
On final approach to Detroit-Willow Run Airport, the crew encountered poor weather conditions and decided to make a go-around for unknown reasons. Shortly later, the twin engine crashed near the airport. Both occupants were seriously injured and the aircraft was destroyed.
Probable cause:
Collision with ground during a missed approach due to improper maintenance. The following contributing factors were reported:
- Flight control systems: elevator tab control system, frayed and binding,
- Low ceiling,
- Fog,
- Maintenance conducted on elevator trim tab bracket a day prior to the accident.
Final Report:

Crash of a Douglas DC-9-31 in New Hope: 72 killed

Date & Time: Apr 4, 1977 at 1619 LT
Type of aircraft:
Operator:
Registration:
N1335U
Flight Phase:
Survivors:
Yes
Site:
Schedule:
Muscle Shoals - Huntsville - Atlanta
MSN:
47393
YOM:
1970
Flight number:
SO242
Crew on board:
4
Crew fatalities:
Pax on board:
81
Pax fatalities:
Other fatalities:
Total fatalities:
72
Captain / Total flying hours:
19380
Captain / Total hours on type:
3205.00
Copilot / Total flying hours:
3878
Copilot / Total hours on type:
235
Aircraft flight hours:
15405
Circumstances:
Southern Airways Flight 242, a DC-9-31, operated as a scheduled passenger flight from Muscle Shoals, Alabama, to Atlanta, Georgia, with an intermediate stop at Huntsville, Alabama. Flight 242 departed Muscle Shoals at 15:21 and landed at Huntsville about 15:44. About 15:54, Flight 242 departed Huntsville on an instrument flight rules (IFR) flight plan for the Hartsfield-Atlanta International Airport; there were 81 passengers and 4 crew members aboard. The flight's route was direct to the Rome VOR and then a Rome runway 26 profile descent to Atlanta. Its estimated time en route was 25 min and its requested en route altitude was 17,000 ft. At 15:56, the controller told Flight 242 that his radarscope was showing heavy precipitation and that the echos were about 5 nmi ahead of the flight. At 15:57:36, the controller said, "...you're in what appears to be about the heaviest part of it now, what are your flight conditions." Flight 242 replied, "...we're getting a little light turbulence and...I'd say moderate rain." At 15:57:47, the controller acknowledged Flight 242's report and told the flight to contact Memphis Center. The Memphis Center controller advised the flight that a SIGMET was current for the area. He then told Flight 242 to contact Atlanta Center. At 16:03:20, Flight 242 switched to another sector of Atlanta Center, established communications on the new frequency and reported being level at FL170. As the aircraft entered an area of rain, the flight crew began discussing the weather depicted on their radar. Based on information from the airborne radar, the captain initially decided that the storms just west of the Rome VOR were too severe to penetrate. Shortly after his initial assessment of the storm system, the captain decided to penetrate the storm area near the Rome VOR. At 16:06:41 Atlanta Center cleared Flight 242 to descend to and maintain 14,000 ft. Shortly afterwards the aircraft entered an area of heavy hail or rain, which continued for at least one minute. The ingestion of intense rain and hail into the engines caused the rotational speed of both engines to decrease below the engine-driven electrical generator operating speeds, and resulted in normal electrical power interruption for 36 seconds. The flight crew likely advanced one or both thrust levers, restoring its generator to operation and provide normal electrical power. After establishing contact with Atlanta Center again, the flight was told to maintain 15,000 ft. At 16:09:15, Flight 242 reported to Atlanta Center, "Okay...we just got our windshield busted and... we'll try to get it back up to 15, we're 14." After reported that the left engine had flamed out, the flight was cleared to descend to 13,000 ft. Meanwhile both engines' high-pressure compressors began to stall severely due to ingestion of massive quantities of water. The severe compressor stalls produced an overpressure surge which deflected the compressor blades forward in the sixth stage of the low-pressure compressors; these blades clashed against the fifth-stage stator vanes and broke pieces from the blades and vanes. Pieces of blades and stator vanes were then ingested into the high-pressure compressors and damaged them severely. Continued high thrust settings following the severe damage to the high-pressure compressors probably caused severe overheating in the turbine sections of both engines, and the engines ceased to function. Shortly before normal electrical power was again, the flight crew radioed that both engines had failed. Atlanta Center told the crew to contact approach control for vectors to Dobbins Air Force Base. Power was then lost for 2 min 4 sec until the APU-driven generator restored electrical power. After establishing contact with Atlanta Approach Control the flight was told they were 20 miles from Dobbins. As the flight was descending, the captain began to doubt their ability to reach Dobbins. Cartersville was closer at 15 miles, so the controller gave vectors for Cartersville. Unable to make it to Cartersville, the crew began looking for a clear field or highway for an emergency landing. At 16:18:02, Flight 242's last transmission to Approach Control was recorded: "... we're putting it on the highway, we're down to nothing." The aircraft's outboard left wing section first contacted two trees near State Spur Highway 92 south-southwest of the community of New Hope. About 0.8 miles farther north-northeast, the left wing again contacted a tree alongside the highway within the community of New Hope. The left and right wings continued to strike trees and utility poles on both sides of the highway, and 570 ft after striking the first tree in New Hope, the aircraft's left main gear contacted the highway to the left of the centerline. Almost simultaneously, the outer structure of the left wing struck an embankment, and the aircraft veered to the left and off the highway. The aircraft traveled another 1,260 ft before it came to rest. As it traveled, the aircraft struck road signs, utility poles, fences, trees, shrubs, gasoline pumps at a gas station-store, five automobiles, and a truck. Of the 85 persons aboard Flight 242, 62 were killed, 21 were seriously injured, and 1 was slightly injured. Additionally, eight persons on the ground were killed. Within a month of the accident, one of the surviving passengers and one person on the ground both died of their injuries.
Probable cause:
Total and unique loss of thrust from both engines while the aircraft was penetrating an area of severe thunderstorms. The loss of thrust was caused by the ingestion of massive amounts of water and hail which, in combination with thrust lever movement, induced severe stalling in and major damage to the engine compressors. Major contributing factors include the failure of the company's dispatching system to provide the flight crew with up-to-date severe weather information pertaining to the aircraft's intended route of flight, the captain's reliance on airborne weather radar for penetration of thunderstorm areas, and limitations in the FAA's ATC system which precluded the timely dissemination of real-time hazardous weather information to the flight crew.
Final Report:

Crash of a Rockwell T-39D Sabreliner near San Diego: 5 killed

Date & Time: Apr 4, 1977
Type of aircraft:
Operator:
Registration:
150545
Flight Phase:
Survivors:
No
MSN:
277-4
YOM:
1963
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
Crashed in unknown circumstances 30 miles east of San Diego while completing a reconnaissance mission. All five crew members were killed.