Crash of a Convair CV-340-38 in Elma

Date & Time: Mar 21, 1978 at 0145 LT
Type of aircraft:
Registration:
N4807C
Survivors:
Yes
Schedule:
Saint Louis - Minneapolis
MSN:
84
YOM:
1953
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9000
Captain / Total hours on type:
5500.00
Circumstances:
En route from Saint Louis to Minneapolis, while cruising at an altitude of 6,000 feet, the right engine caught fire. The copilot declared an emergency and was cleared to divert to Elma Airport. Shortly later, the right engine detached. The crew completed an emergency descent but made a forced landing off airport on land. All four occupants evacuated safely while the aircraft was considered as damaged beyond repair.
Probable cause:
Engine failure in flight due to master and connecting rods failure. The following contributing factors were reported:
- Material failure,
- Fire in engine,
- Oil exhaustion - engine lubrication system,
- Separation in flight,
- Complete engine failure,
- Force landing off airport on land,
- Engine separated from aircraft in flight due to fire damage.
Final Report:

Crash of a Beechcraft 65-90 King Air in Houston: 2 killed

Date & Time: Mar 19, 1978 at 0132 LT
Type of aircraft:
Registration:
N2MF
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Houston - Houston
MSN:
LJ-96
YOM:
1966
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
2271
Captain / Total hours on type:
117.00
Circumstances:
While flying around Houston Airport by night, the pilot lost control of the airplane that entered a dive and crashed in flames in a field. The aircraft was destroyed and both occupants were killed.
Probable cause:
Stall and spiral after the pilot failed to maintain flying speed. The following contributing factors were reported:
- Powerplant - propeller system: governor, erratic.
Final Report:

Crash of a Piper PA-31-310 Navajo in Leesburg: 1 killed

Date & Time: Mar 16, 1978 at 0345 LT
Type of aircraft:
Registration:
N7488L
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Leesburg - Leesburg
MSN:
31-7300911
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
500
Circumstances:
While flying in marginal weather conditions, the twin engine airplane entered an uncontrolled descent and crashed near Leesburg-Flying Baron Estates Airport. The passenger was killed and the pilot was seriously injured.
Probable cause:
Uncontrolled descent and subsequent uncontrolled collision with ground after the pilot initiated flight in adverse weather conditions. The following contributing factors were reported:
- The pilot suffered a spatial disorientation,
- Fog,
- Visibility half a mile or less.
Final Report:

Crash of a Beechcraft D18S in Pontiac: 2 killed

Date & Time: Mar 14, 1978 at 0413 LT
Type of aircraft:
Registration:
N427Q
Flight Type:
Survivors:
No
Schedule:
Flint - Pontiac
MSN:
A-336
YOM:
1947
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
5443
Captain / Total hours on type:
421.00
Circumstances:
The twin engine airplane was completing a cargo flight from Flint to Pontiac. While descending to Pontiac-Oakland County Airport by night, the pilot encountered bad weather conditions when on final, the airplane went out of control and crashed in White Lake, about three miles west of the airport. The aircraft was destroyed and both occupants were killed.
Probable cause:
Uncontrolled descent on finale approach due to windshear. The following contributing factors were reported:
- Turbulences associated with clouds and thunderstorm activity,
- Visibility two miles or less,
- Fog,
- IFR conditions,
- Local residents reported tornado like winds in area.
Final Report:

Crash of a Rockwell Hawk Commander 681 in Greenup: 3 killed

Date & Time: Mar 8, 1978 at 1008 LT
Operator:
Registration:
N5NP
Survivors:
No
Schedule:
Milwaukee – Manchester – Huntington
MSN:
680-6042
YOM:
1970
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
9154
Captain / Total hours on type:
1395.00
Circumstances:
En route, the crew encountered engine problems and was cleared to divert to Ashland Airport. While descending in marginal weather conditions (low ceiling, fog and icing conditions), the crew lost control of the airplane that crashed in a field located in Greenup, west of the airport. The aircraft was destroyed and all three occupants were killed. At the time of the accident, weather conditions were below minimums.
Probable cause:
Uncontrolled collision with ground on final approach following a powerplant failure for undetermined reasons. The following contributing factors were reported:
- Failed to follow approved procedures,
- Improper emergency procedures,
- Low ceiling,
- Fog,
- Icing conditions including sleet, freezing rain,
- Partial loss of power on one engine,
- Forced landing off airport on land,
- Visibility half a mile or less,
- Weather conditions below minimums.
Final Report:

Crash of a Cessna 411 in Chilcoot: 4 killed

Date & Time: Mar 3, 1978 at 1940 LT
Type of aircraft:
Registration:
N3212R
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
San Jose - Truckee
MSN:
411-0212
YOM:
1966
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
151
Captain / Total hours on type:
69.00
Circumstances:
While flying in poor weather conditions, the pilot lost control of the airplane that entered an uncontrolled descent and crashed in flames in an uninhabited area located in the region of Chilcoot. The aircraft was destroyed and all four occupants were killed.
Probable cause:
Uncontrolled descent and subsequent uncontrolled collision with ground after the pilot initiated flight in adverse weather conditions and suffered a spatial disorientation. The following contributing factors were reported:
- Low ceiling,
- IFR flight conditions,
- VFR flight not recommended.
Final Report:

Crash of a Beechcraft G18S in Rockingham

Date & Time: Mar 2, 1978 at 2020 LT
Type of aircraft:
Registration:
N180P
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Rockingham - Pontiac
MSN:
BA-478
YOM:
1959
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6500
Captain / Total hours on type:
2825.00
Circumstances:
Shortly after a night takeoff from Rockingham-Hamlet Airport, the twin engine airplane struck wires and crashed in flames in a snow covered field. The pilot, sole on board, was seriously injured.
Probable cause:
Collision with wires during initial climb due to inadequate preflight preparation on part of the pilot-in-command. The following contributing factors were reported:
- Failed to abort takeoff,
- Selected unsuitable terrain,
- Disregard of good operating practice,
- Airport conditions: snow on runway,
- Launched from snow covered runway with half inch of snow on wings.
Final Report:

Crash of a Douglas DC-10-10 in Los Angeles: 2 killed

Date & Time: Mar 1, 1978 at 0925 LT
Type of aircraft:
Operator:
Registration:
N68045
Flight Phase:
Survivors:
Yes
Schedule:
Los Angeles - Honolulu
MSN:
46904
YOM:
1972
Flight number:
CO603
Crew on board:
14
Crew fatalities:
Pax on board:
186
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
29000
Captain / Total hours on type:
2911.00
Copilot / Total flying hours:
10000
Copilot / Total hours on type:
1249
Aircraft flight hours:
21358
Circumstances:
On March 1, 1978, Continental Air Lines, Inc., Flight 603, a McDonnell Douglas DC-10-10 (N68045), was a scheduled flight from Los Angeles International Airport, California, to Honolulu, Hawaii. At 0857:18, Flight 603 called Los Angeles clearance delivery and was cleared for the route of flight which was to have been flown. About 2 min later, the flight received permission from Los Angeles ground control to push back from the gate. At 0901:37, Flight 603 was cleared by ground control to taxi to runway 6R. The runway was wet, but there was no standing water. At 0922:29, Los Angeles local control cleared Flight 603 to taxi into position on runway 6R and hold. At 0923:17, local control cleared Flight 603 for takeoff; however, the flightcrew did not acknowledge the instructions and did not comply with them. At 0923:57, local acknowledged the instructions. The captain stated that he delayed control, again, cleared the flight for takeoff. This time the flightcrew acknowledgment of the takeoff clearance because he believed that he had initially been given the clearance too soon after a heavy jet aircraft had made its takeoff. The flightcrew stated that acceleration was normal and that all engine instruments were in the normal range for takeoff. As the airspeed approached the V1 speed of 156 kns, the captain heard a loud "metallic bang" which was followed immediately by "a kind of quivering of the plane." The flightcrew noticed that the left wing dropped slightly. A rejected takeoff was begun immediately; however, according to the digital flight data recorder (DFDR), the airspeed continued to increase to about 159 kns as the rejected takeoff procedures were begun. The captain stated that he applied full brake pressure while simultaneously bringing the thrust levers back to idle power. Reverse thrust levers were actuated and full reverse thrust was used. The flightcrew stated that they noted good reverse thrust. First, the aircraft moved to the left of the runway centerline and appeared tb the flightcrew to be decelerating normally. With about of deceleration had decreased, and they believed that the aircraft would 2,000 ft of runway remaining, the flightcrew became aware that the rate not be able to stop on the runway surface. The captain stated that he maintained maximum brake pedal force and full reverse thrust as he steered the aircraft to the right of the runway centerline in an effort "to go beside the stanchions holding the runway lights" immediately off of the departure end of runway 6R. He stated further that he encountered no problems with directional control of the aircraft throughout the rejected takeoff maneuver. The aircraft departed the right corner of the departure end of runway 6R. About 100 ft beyond the runway, the left main landing gear broke through the nonload-bearing tar-macadam (tarmac) surface and failed rearward. Fire erupted immediately from this area. The aircraft dropped onto the left wing and the No. 1 (left) engine and rotated to the left as it continued its slide along the surface. It stopped between two of the approach light stanchions for runway 24L about 664 ft from the departure end of runway 6R and about 40 ft to the right of the runway 6R extended centerline; it came to rest on a heading of 008°, in an 11° left wing low, 1.3° noseup attitude. When the aircraft came to a stop, the evacuation was begun immediately. Two passengers were killed while all other occupants were evacuated, some of them with serious injuries.
Probable cause:
The National Transportation Safety Board determined that the probable cause of the accident was the sequential failure of two tires on the left main landing gear and the resultant failure of another tire on the same landing gear at a critical time during the takeoff roll. These failures resulted in the captain's decision to reject the takeoff. Contributing to the accident was the cumulative effect of the partial loss of aircraft braking because of the failed tires and the reduced braking friction achievable on the wet runway surface which increased the accelerate-stop distance to a value greater than the available runway length. These factors prevented the captain from stopping the aircraft within the runway confines. The failure of the left main landing gear and the consequent rupture of the left wing fuel tanks resulted in an intense fire which added to the severity of the accident.
Final Report:

Crash of a Rockwell Aero Commander 500A near Solvang: 7 killed

Date & Time: Feb 28, 1978 at 1030 LT
Registration:
N6143X
Flight Phase:
Survivors:
No
Site:
Schedule:
Visalia – Santa Maria – Santa Barbara
MSN:
500-931-26
YOM:
1960
Crew on board:
3
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
17770
Captain / Total hours on type:
2440.00
Circumstances:
While cruising under VFR mode, the crew encountered limited visibility due to low ceiling and ground fog when the airplane struck the slope of a mountain located near Solvang. The aircraft was destroyed upon impact and all seven occupants were killed.
Probable cause:
Controlled flight into terrain after the crew continued VFR flight into adverse weather conditions. The following contributing factors were reported:
- Low ceiling,
- Ground fog.
Final Report:

Crash of an Evangel 4500 in Merrill Pass: 3 killed

Date & Time: Feb 27, 1978 at 1325 LT
Type of aircraft:
Operator:
Registration:
N4508L
Flight Phase:
Survivors:
No
Site:
Schedule:
Dillingham – Stony River – Anchorage
MSN:
8
YOM:
1974
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
5500
Captain / Total hours on type:
1203.00
Circumstances:
While cruising under VFR mode in adverse weather conditions, the pilot suffered a spatial disorientation when the airplane struck the slope of a mountain located near Merrill Pass. The aircraft was destroyed upon impact and all three occupants were killed. The wreckage was located a day later.
Probable cause:
Uncontrolled descent and subsequent uncontrolled collision with ground due to inadequate preflight preparation. The following contributing factors were reported:
- Continued VFR flight into adverse weather conditions,
- Spatial disorientation,
- Low ceiling,
- Rain,
- Pilot checked weather data himself,
- Zero visibility.
Final Report: