Crash of a Beechcraft G18S in Cleveland

Date & Time: Oct 11, 1978 at 2045 LT
Type of aircraft:
Registration:
N11Z
Flight Type:
Survivors:
Yes
Schedule:
Bowling Green - Cleveland
MSN:
BA-510
YOM:
1960
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2673
Captain / Total hours on type:
267.00
Circumstances:
The airplane landed hard on its belly after the pilot forgot to lower the landing gear on approach. Upon touchdown, he decided to initiate a go-around manoeuvre when the cargo shifted as it was not properly secured. The airplane stalled and crashed in flames. The aircraft was damaged beyond repair and the pilot, sole on board, was seriously injured.
Probable cause:
Hard and wheels-up landing following an improper level off. The following contributing factors were reported:
- Inadequate preflight preparation,
- cargo shifted as improperly secured,
- No cargo net or rope found in the cabin,
- First flight in this model.
Final Report:

Crash of a Piper PA-31P-425 Pressurized Navajo in Lexington: 5 killed

Date & Time: Oct 3, 1978 at 2145 LT
Type of aircraft:
Operator:
Registration:
N338J
Flight Phase:
Survivors:
No
Schedule:
Lexington - Fort Smith
MSN:
31P-051
YOM:
1971
Crew on board:
3
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
11226
Circumstances:
Following a night takeoff from Lexington-Blue Grass Airport, the twin engine airplane encountered difficulties to gain height. It struck tree tops, stalled and crashed in flames in a wooded area. The aircraft was destroyed and all five occupants were killed.
Probable cause:
Collision with trees and subsequent crash during climb following an engine failure caused by a crankshaft failure. The following contributing factors were reported:
- Material failure,
- Failed to follow approved procedures,
- Improper emergency procedures,
- Rain,
- Fog,
- Forced landing off airport on land,
- Visibility less than a mile,
- Both propeller blade angles found at 30° settings,
- Flaps found extended.
Final Report:

Crash of a Boeing 727-200 in San Diego: 142 killed

Date & Time: Sep 25, 1978 at 0902 LT
Type of aircraft:
Operator:
Registration:
N533PS
Survivors:
No
Site:
Schedule:
Sacramento - Los Angeles - San Diego
MSN:
19688/589
YOM:
1968
Flight number:
PS182
Crew on board:
7
Crew fatalities:
Pax on board:
128
Pax fatalities:
Other fatalities:
Total fatalities:
142
Captain / Total flying hours:
14382
Captain / Total hours on type:
10482.00
Copilot / Total flying hours:
10049
Copilot / Total hours on type:
5800
Aircraft flight hours:
24088
Aircraft flight cycles:
36557
Circumstances:
The crew was completing flight PS182 from Sacramento to San Diego with an intermediate stop in Los Angeles. While descending to San Diego-Lindbergh Field runway 27, the crew was informed about the presence of a Cessna 172M registered N7711G and operated by the Gibbs Flight Center. The single engine airplane just departed San Diego Airport for a local training mission with one student pilot and one instructor on board. At 0901:47, at an altitude of 2,600 feet and 3 NM northeast of San Diego Airport, both airplane collided. Out of control, they dove into the ground and crashed into several houses and the 805 highway located between the districts of Altadena and City Heights. Both aircraft disintegrated on impact and all 137 occupants in both aircraft were killed as well as seven people on the ground. Nine other people on the ground were seriously injured as dozen houses were destroyed.
Probable cause:
The failure of the flight crew of Flight 182 to comply with the provisions of a maintain-visual-separation clearance, including the requirement to inform the controller when visual contact was lost; and the air traffic control procedures in effect which authorized the controllers to use visual separation procedures in a terminal area environment when the capability was available to provide either lateral or vertical separation to either aircraft. Contributing to the accident were:
- The failure of the controller to advise Flight 182 of the direction of movement of the Cessna;
- The failure of the pilot of the Cessna to maintain his assigned heading;
- The improper resolution by the controller of the conflict alert.
Final Report:

Crash of a Grumman G-159 Gulfstream GI in Houston

Date & Time: Sep 24, 1978 at 1447 LT
Type of aircraft:
Operator:
Registration:
N91G
Survivors:
Yes
Schedule:
Ponca City - Houston
MSN:
37
YOM:
1960
Crew on board:
2
Crew fatalities:
Pax on board:
18
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10284
Captain / Total hours on type:
955.00
Circumstances:
On approach to Houston-William P. Hobby Airport, a low oil pressure in the right engine gearbox forced the crew to shut down the engine and to feather its propeller. For unknown reason, the propeller was not properly feathered and the airplane was approaching too low and too fast. After touchdown, as the airplane already rolled half of the landing distance (7,600 feet), the captain decided to initiate a go-around. After liftoff, fire was observed coming out from the tail exhaust pipe while the left engine lost power. The crew attempted an emergency landing and completed a belly landing in an open field near the airport. All 20 occupants were rescued, among them a passenger was seriously injured. The aircraft was written off.
Probable cause:
Wheels-up landing following a go-around after the crew failed to follow approved procedures. The following contributing factors were reported:
- Improper emergency procedures,
- Poorly planned approach,
- Failure of both engines,
- Forced landing off airport on land,
- Right engine shut down in flight due to low oil pressure,
- Right propeller not fully feathered,
- Left engine not able full accelerate.
Final Report:

Crash of a Rockwell Aero Commander 500 in Laredo: 7 killed

Date & Time: Sep 23, 1978 at 2340 LT
Registration:
N6244B
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Fort Worth - San Antonio - Laredo
MSN:
500-652-13
YOM:
1958
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
310
Captain / Total hours on type:
142.00
Circumstances:
While approaching Laredo area by night, the pilot encountered marginal weather conditions with low ceiling and limited visibility. He completed several turns when the airplane entered a dive and crashed. The airplane was totally destroyed upon impact and all seven occupants were killed.
Probable cause:
Uncontrolled descent after the pilot initiated flight in adverse weather conditions. The following contributing factors were reported:
- The pilot became lost/disoriented,
- Spatial disorientation,
- Low ceiling,
- Haze,
- Dark night,
- VFR flight not recommended,
- During last 11 minutes of flight, heading changed thru 630°.
Final Report:

Crash of a Lockheed P-3B-75-LO Orion in Poland: 8 killed

Date & Time: Sep 22, 1978 at 1215 LT
Type of aircraft:
Operator:
Registration:
152757
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Brunswick - Trenton
MSN:
185-5199
YOM:
1966
Location:
Crew on board:
8
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
8
Circumstances:
The four engine airplane departed Brunswick NAS, Maine, at 1205LT on a flight to Trenton, Ontario, where it was dispatched to an airshow. While climbing, the crew encountered poor weather conditions with stormy weather when the engine n°1 went in whirl mode and detached. 11 feet of the left wing separated and struck the left horizontal stabilizer that was torn off as well. Out of control, the airplane entered a dive and partially disintegrated before crashing near Poland. All eight occupants were killed.
Crew:
Lt Cdr Francis William Dupont Jr.,
Lt Jg Donald Edward Merz,
Lt Jg George D. Nuttelman,
Lt Jg Ernest A. Smith,
Aw2 James Allen Piepkorn,
Awan Paul G. Schulz,
Ad3 Robert Lewis Phillips Jr.,
Adc Larry Miller.
Probable cause:
It was determined that the engine went into a whirl mode which corresponds to a low frequency vibration in the engine mounts that can cause the separation of the engine in flight. It is believed that weather turbulences may affect the proper functioning of the engine.

Crash of a Piper PA-31-310 Navajo in Bristol

Date & Time: Sep 19, 1978 at 0907 LT
Type of aircraft:
Registration:
N7700L
Flight Type:
Survivors:
Yes
Schedule:
Johnson City - Bristol
MSN:
31-501
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1826
Captain / Total hours on type:
158.00
Circumstances:
On final approach to runway 23 at Bristol-Tri-Cities Airport, both engines stopped simultaneously. The pilot attempted an emergency landing and the airplane belly landed in a field located 2,600 feet short of runway. The pilot, sole on board, was uninjured while the aircraft was damaged beyond repair.
Probable cause:
Wheels-up landing on final approach following a double engine failure caused by a fuel exhaustion. The following contributing factors were reported:
- Mismanagement of fuel,
- Inattentive to fuel supply,
- Fuel exhaustion,
- Forced landing off airport on land.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in Granville: 2 killed

Date & Time: Sep 18, 1978 at 1042 LT
Registration:
N63731
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Westfield - Pontiac
MSN:
31-7752054
YOM:
1977
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
6500
Circumstances:
While cruising in marginal weather conditions on a cargo flight from Westfield-Barnes to Pontiac, the twin engine airplane struck the slope of a mountain located in Granville, Massachusetts. The burnt wreckage was found 500 feet below the summit and both occupants were killed.
Probable cause:
Controlled flight into terrain after the pilot continued VFR flight in adverse weather conditions. The following contributing factors were reported:
- Unwarranted low flying,
- Low ceiling,
- Rain,
- Fog.
Final Report:

Crash of a Cessna 411 off Kodiak: 3 killed

Date & Time: Sep 17, 1978
Type of aircraft:
Registration:
N1EC
Flight Phase:
Survivors:
No
Schedule:
King Salmon - Kodiak
MSN:
411-0094
YOM:
1965
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
2200
Captain / Total hours on type:
90.00
Circumstances:
While approaching Kodiak on a taxi flight from King Salmon, the twin engine airplane crashed in unknown circumstances in the Shelikof Strait located off Kodiak. SAR operations were conducted and eventually suspended after few days as no trace of the aircraft nor the three occupants was found.
Probable cause:
Due to lack of evidences as the aircraft was not recovered, the cause of the accident could not be determined.
Final Report:

Crash of a De Havilland DHC-2 Beaver near Whittier: 6 killed

Date & Time: Sep 13, 1978 at 1130 LT
Type of aircraft:
Operator:
Registration:
N37741
Flight Phase:
Survivors:
No
Schedule:
Anchorage - Whittier
MSN:
269
YOM:
1952
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
3125
Captain / Total hours on type:
106.00
Circumstances:
En route from Anchorage to Whittier, weather conditions worsened while the pilot was flying into a canyon. The single engine airplane lost height then crashed in a river bed. All six occupants were killed.
Probable cause:
Loss of control after the pilot continued VFR flight in adverse weather conditions. The following contributing factors were reported:
- Improper in-flight decisions,
- Sudden windshift,
- Downdrafts, updrafts,
- Flew into blind canyon,
- Aircraft came to rest in water,
- Float equipped,
- No antenna for ELT.
Final Report: