Crash of a Boeing 737-222 in Charlotte

Date & Time: Oct 25, 1986 at 2008 LT
Type of aircraft:
Operator:
Registration:
N752N
Survivors:
Yes
Schedule:
Newark - Charlotte - Myrtle Beach
MSN:
19073
YOM:
1968
Flight number:
PI467
Crew on board:
5
Crew fatalities:
Pax on board:
114
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10000
Captain / Total hours on type:
2500.00
Copilot / Total flying hours:
4100
Copilot / Total hours on type:
500
Aircraft flight hours:
41714
Aircraft flight cycles:
59033
Circumstances:
During arrival, Piedmont flight 467 was vectored for an ILS runway 36R approach. At 2001 cdt (approximately 7 minutes before landing), all arriving flights were advised the weather was (in part): 400 feet overcast, visibility 2 miles with light rain and fog, wind from 090° at 8 knots. Runway 05/32 was out of-svc at that time. Flight 467 was vectored for right turns (from north and west) onto final approach. At 2002:42, the ATC final controller told another flight (same frequency) that there was a 20 to 25 knots right crosswind on final approach. When flight 467 was cleared for landing at 2005:36, the surface wind was reported from 100° at 4 knots. The aircraft was not configured for landing until just before touchdown and the copilot did not alert the captain of the deviation. The aircraft landed approximately 3,200 feet from the threshold and the captain was unable to stop on the wet runway. After departing the runway, the aircraft hit an ILS antenna and a culvert, then went thru a fence and stopped beside railroad tracks. Reportedly, the captain added 20 knots to approach speed for possible wind shear and delayed spoiler option after touchdown. There was evidence of hydroplaning and poor frictional quality on last 1,500 feet of runway. Three passengers received back injuries; both pilots and one flight attendant had minor injuries.
Probable cause:
The captain's failure to stabilize the approach and his failure to discontinue the approach to a landing that was conducted at an excessive speed beyond the normal touchdown point on a wet runway. Contributing to the accident was the captain's failure to optimally use the airplane decelerative devices. Also contributing to the accident was the lack of effective crew coordination during the approach. Contributing to the severity of the accident was the poor frictional quality of the last 1,500 feet of the runway and the obstruction presented by a concrete culvert located 318 feet beyond the departure end of the runway.
Final Report:

Crash of a Cessna 441 Conquest II in DuPage: 1 killed

Date & Time: Oct 23, 1986 at 0851 LT
Type of aircraft:
Operator:
Registration:
N241FW
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
DuPage – Cleveland
MSN:
441-0241
YOM:
1982
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
10200
Aircraft flight hours:
1615
Circumstances:
The pilot (a part time employee of the owner) was ferrying the aircraft for maintenance. Witnesses, who saw the pilot before take- off, noted that his speech was slurred and that he seemed angry because a tug would not start. One witness characterized him as being 'very mad' and said his face was 'flushed red.' The aircraft was observed to takeoff in a high nose-up attitude and climb about 500 to 1,000 feet before turning to the southwest and leveling. Subsequently, the plane turned back toward the airport, then it crashed and burned approximately 1-1/2 mile ssw of the airport while on a heading of northeast. Impact occurred while the aircraft was descending in a slightly left wing low attitude. The wreckage was scattered over an area that was approximately 600 feet long and about 45 feet wide at the widest point. According to witnesses, the engines were operating normally when the aircraft crashed. No preimpact mechanical problem was found. A toxicology check of the pilot's liver tissue fluid showed an alcohol level of 2,26‰. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: in flight collision with terrain/water
Phase of operation: takeoff - initial climb
Findings
1. (c) judgment - poor - pilot in command
2. (c) impairment (alcohol) - pilot in command
3. Ifr procedure - initiated
4. (f) weather condition - low ceiling
5. (f) weather condition - fog
6. Climb - delayed
7. (c) altitude - not maintained - pilot in command
8. (c) descent - not corrected - pilot in command
9. (f) psychological condition - pilot in command
Final Report:

Crash of a Lockheed C-141B Starlifter at Travis AFB

Date & Time: Oct 15, 1986
Type of aircraft:
Operator:
Registration:
65-0246
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
300-6097
YOM:
1965
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
28675
Circumstances:
On approach to Travis AFB, the crew was advised of a bomb threat at the passenger terminal. In night-time conditions, he had to park the aircraft which was normally reserved for tow-in parking. The captain complained about this to the marshaller, but he was told to taxi the aircraft to the parking spot. Wingwalkers were present by each wing. While completing a sharp turn to the right, the left wing struck a light pole, rupturing the n°1 fuel tank. Fuel leaked down the light pole and ignited after contacting a high voltage junction box located at the base of the pole. An intensive fire erupted, destroyed the left part of the aircraft. All occupants evacuated safely and were unhurt.

Crash of a Mitsubishi MU-2B-20 Marquise in Denver

Date & Time: Oct 12, 1986 at 1051 LT
Type of aircraft:
Registration:
N3MU
Flight Type:
Survivors:
Yes
Schedule:
Grand Junction – Denver – Chicago
MSN:
143
YOM:
1969
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4186
Captain / Total hours on type:
38.00
Aircraft flight hours:
5780
Circumstances:
Aircraft had been repossessed and was being ferried from Grand Junction, CO, to Chicago, IL, with en route stop at Denver, CO. After takeoff from Denver, landing gear would not retract. Pilot made several attempts without success. He elected to return to Denver. Pilot said that on final approach the right engine began surging and the left engine would not increase power. Aircraft made hard landing on runway, breaking left wing. Investigation revealed both speed levers would not function because engine prop governors and underspeed fuel governor reset arms, splined onto underspeed fuel governor shafts, were positioned on opposite side of speed lever actuating arms. Landing gear functioned normally during swing tests. It was later learned that right main tire had blown on takeoff 3 days earlier and required repair. Maintenance personnel opened the landing gear circuit breakers to preclude inadvertent gear retraction. Pilot said he checked circuit breakers when gear failed to retract. Both occupants escaped uninjured.
Probable cause:
Occurrence #1: airframe/component/system failure/malfunction
Phase of operation: takeoff - initial climb
Findings
1. (f) electrical system,circuit breaker - not engaged
2. (f) maintenance - inadequate - company maintenance personnel
3. (c) aircraft preflight - inadequate - pilot in command
4. (f) lack of familiarity with aircraft - pilot in command
5. (f) landing gear - inoperative
6. Gear retraction - attempted - pilot in command
7. (f) lack of familiarity with aircraft - copilot/second pilot
8. (c) electrical system, circuit breaker - open
9. (f) landing gear, gear indicating system - false indication
----------
Occurrence #2: loss of engine power (partial) - nonmechanical
Phase of operation: approach - vfr pattern - final approach
Findings
10. Precautionary landing - performed - pilot in command
11. (c) checklist - not followed - pilot in command
12. (c) propeller governor control, linkage - incorrect
13. (c) maintenance - not corrected - company maintenance personnel
14. (c) maintenance, service of aircraft/equipment - inadequate - other maintenance personnel
----------
Occurrence #3: hard landing
Phase of operation: landing - flare/touchdown
Findings
15. (c) airspeed (vref) - below - pilot in command
16. (c) diverted attention - pilot in command
17. (c) stall - inadvertent - pilot in command
Final Report:

Crash of a Lockheed L-382G-23C Hercules at Kelly AFB: 3 killed

Date & Time: Oct 4, 1986 at 0410 LT
Type of aircraft:
Operator:
Registration:
N15ST
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Kelly AFB - Robins AFB
MSN:
4391
YOM:
1970
Flight number:
SJ015
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
7000
Captain / Total hours on type:
1400.00
Copilot / Total flying hours:
4100
Copilot / Total hours on type:
107
Aircraft flight hours:
45622
Aircraft flight cycles:
20472
Circumstances:
Southern Air Transport’s LOGAIR 15 flight, a Lockheed L-382G, was cleared for takeoff from Kelly Air Force Base, Texas, on an instrument flight plan to Robins Air Force Base, Georgia, at about 0405 on October 4, 1986. Visual meteorological conditions prevailed. There were three flightcrew members aboard the military contracted domestic cargo flight operating under 14 CFR Part 121. All communications with the air traffic control tower were routine. Radar recorded that the airplane reached an altitude of about 700 feet above ground level. Witnesses reported an abnormally steep climb attitude. followed by a turn and/or bank to the left, after which the airplane continued to roll to the left and struck the ramp area at about a 90° angle to the departure runway in a near-inverted attitude between two hangars and exploded. A severe ground fire ensued. All three flightcrew members were killed.
Probable cause:
The probable cause of this accident was the use by the carrier of a non approved device designed to raise the elevator during loading operations which was not properly stowed by the flightcrew and which lodged in the Controls, preventing the flightcrew from controlling the airplane during takeoff.
Final Report:

Crash of a Piper PA-60 Aerostar (Ted Smith 600) in Tallahassee: 1 killed

Date & Time: Oct 2, 1986 at 1845 LT
Registration:
N217HM
Flight Type:
Survivors:
No
Schedule:
Tampa – Tallahassee
MSN:
60-0236-098
YOM:
1976
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3500
Circumstances:
Witnesses stated seeing the aircraft enter a left downwind approach to runway 16, turn base to final normally then veer to the left of the runway in a nose high attitude and disappear behind a line of trees and crash approximately 500 feet east of runway 16. Post crash examination of the aircraft revealed the left engine was not producing power at the time of impact. Further examination revealed that the left engine fuel servo fuel mixture and idle speed settings were misadjusted. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: loss of engine power
Phase of operation: approach - vfr pattern - final approach
Findings
1. (f) fuel system, fuel control - other
----------
Occurrence #2: loss of control - in flight
Phase of operation: approach - vfr pattern - final approach
Findings
2. (f) in-flight planning/decision - poor - pilot in command
3. (c) directional control - not maintained - pilot in command
----------
Occurrence #3: in flight collision with object
Phase of operation: descent - uncontrolled
Findings
4. Object - tree(s)
Final Report:

Crash of a Rockwell Sabreliner 75A in Liberal

Date & Time: Sep 29, 1986 at 1204 LT
Type of aircraft:
Operator:
Registration:
N64
Flight Type:
Survivors:
Yes
Schedule:
Oklahoma City - Liberal
MSN:
380-35
YOM:
1975
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8448
Captain / Total hours on type:
1540.00
Aircraft flight hours:
7327
Circumstances:
The right main landing gear downlock pin retracted just before or during touchdown. The airplane touched down 21 feet short of the runway. It traveled that 21 feet, traveled the full length of the 6999- foot runway, then traveled another one-fourth of a mile and stopped on a golf course. No pre-touchdown mechanical, hydraulic or electrical problems could be found. All four occupants escaped uninjured.
Probable cause:
Occurrence #1: gear collapsed
Phase of operation: landing - flare/touchdown
Findings
1. (c) procedures/directives - not followed - pilot in command
2. (c) gear retraction - inadvertent - copilot/second pilot
----------
Occurrence #2: loss of control - on ground/water
Phase of operation: landing - roll
----------
Occurrence #3: on ground/water encounter with terrain/water
Phase of operation: landing - roll
Findings
3. (f) terrain condition - ditch
----------
Occurrence #4: on ground/water collision with object
Phase of operation: landing - roll
Findings
4. (f) object - fence
----------
Occurrence #5: on ground/water encounter with terrain/water
Phase of operation: landing - roll
Findings
5. (f) terrain condition - water, glassy
Final Report:

Crash of a Beechcraft E18S in Chicago: 1 killed

Date & Time: Sep 28, 1986 at 2254 LT
Type of aircraft:
Operator:
Registration:
N101VE
Flight Type:
Survivors:
No
Site:
Schedule:
Chicago - Covington
MSN:
BA-190
YOM:
1956
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
6400
Captain / Total hours on type:
2059.00
Aircraft flight hours:
17743
Circumstances:
The aircraft had departed on runway 13. He was then directed to climb to 6,000 feet. Thirty seconds later he advised he had engine trouble and was returning to the airport. Shortly thereafter he advised he could not maintain altitude. The aircraft, one mile southeast of the airport, struck the roofs of two family type residences. Then struck two garages, ground impacted and struck the rear area of a third residence. An intense fire followed. Left engine had impeller failure. Propeller was pitched between low and high rpm. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: loss of engine power (total) - mech failure/malf
Phase of operation: climb - to cruise
Findings
1. (f) eng assembly, blower/impeller/integral supercharger - failure, total
2. (f) lubricating system - lack of
----------
Occurrence #2: airframe/component/system failure/malfunction
Phase of operation: descent - emergency
Findings
3. (c) propeller system/accessories, feathering system - incorrect
4. Propeller feathering - attempted - pilot in command
5. (c) propeller system/accessories, feathering system - movement restricted
----------
Occurrence #3: forced landing
Phase of operation: descent - emergency
----------
Occurrence #4: in flight collision with object
Phase of operation: descent - emergency
Findings
6. (c) object - residence
----------
Occurrence #5: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in Culpeper: 1 killed

Date & Time: Sep 28, 1986 at 0500 LT
Registration:
N59942
Flight Phase:
Flight Type:
Survivors:
No
MSN:
31-7552094
YOM:
1975
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
500
Aircraft flight hours:
4139
Circumstances:
The aircraft, which was stolen from the airport, collided with the ground in a steep angle approximately one mile south of the airport. Instrument meteorological conditions existed with local visibility less than one mile as reported by persons near the accident site. The pilot was not instrument or multi engine rated. The pilot was denied a medical certificate about two weeks prior to the accident due to uncontrolled hypertension and diabetes. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: takeoff - initial climb
Findings
1. (f) weather condition - fog
2. (f) weather condition - low ceiling
3. (c) vfr flight into imc - attempted - pilot in command
4. (f) overconfidence in personal ability - pilot in command
5. (c) aircraft handling - not maintained - pilot in command
6. (f) lack of total instrument time - pilot in command
7. (c) spatial disorientation - pilot in command
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of a Cessna 340A near Crawford: 5 killed

Date & Time: Sep 25, 1986 at 1740 LT
Type of aircraft:
Registration:
N6663G
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Gunnison – Grand Junction
MSN:
340A-0693
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
2241
Captain / Total hours on type:
1420.00
Aircraft flight hours:
1560
Circumstances:
The pilot took off on a VFR flight with no flight plan filed or weather briefing. He encountered a weather squall line en route with low ceilings, fog, mixed rain and snow. While he was attempting to maneuver VFR through the weather at a low altitude above the ground, the aircraft entered clouds and impacted terrain at 7,500 feet msl in mountainous terrain. All five occupants were killed.
Probable cause:
Occurrence #1: in flight encounter with weather
Phase of operation: maneuvering
Findings
1. (f) weather condition - low ceiling
2. (f) weather condition - fog
3. (f) weather condition - rain
4. (f) weather condition - snow
5. (f) terrain condition - mountainous/hilly
6. (c) preflight planning/preparation - inadequate - pilot in command
7. (c) hazardous weather advisory - not obtained - pilot in command
8. (c) vfr flight into imc - inadvertent - pilot in command
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: maneuvering
Findings
9. (c) in-flight planning/decision - improper - pilot in command
10. (c) proper altitude - not maintained - pilot in command
Final Report: