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Crash of a Piper PA-61P Aerostar (Ted Smith 601P) in Moscow: 1 killed

Date & Time: Apr 23, 2002 at 1343 LT
Operator:
Registration:
N101LT
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Lamar - Liberal
MSN:
61-0760-8063377
YOM:
1980
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
17725
Aircraft flight hours:
2442
Circumstances:
The airplane was destroyed during an attempted forced landing following an in-flight fire in cruise flight. The pilot was reported to be flying the airplane to an airport in order to have maintenance work performed on the right engine due to a boost problem. It was reported that the pilot had another mechanic at another airport look at the airplane. A work order for a transient airplane was found that indicated work performed on the right engine turbocharger system about 1 month before the accident. The work order shows that the wastegate oil filter was found clogged and collapsed and that it was cleaned, straightened and reinstalled. The pilot operated the airplane with a right engine boost problem. The boost problem with the right engine is evidenced by the previous work order, the excessive amount of runway used during takeoff, the reported smoke from the right engine after takeoff, and the airplane not climbing as expected after takeoff. Due to the reduced power from the right engine, the pilot was required to apply left brake in order to maintain directional control during takeoff, as evidenced by the blued left brake disk with metal transfer into the relief holes and slots. As a result of the pilot using left brake during takeoff, a fire erupted in the left wheel well, which spread to the aft fuselage. This is evidenced by the sooting, fire, and heat damage to the wheel well, the carpet above the wheel well, and aft fuselage. The fuselage immediately behind the baggage compartment had extensive fire damage. The damage in this area included blistered paint on the upper surface, and a two foot square section of the left fuselage skin that was burned away. The area that was burned away was in the vicinity of the hydraulic fluid reservoir. The aluminum hydraulic fluid reservoir was not found, only the steel filler neck, mounting screws, and cap were found. No evidence of fire was found within the right main landing gear wheel well or in the engine compartments. A witness reported seeing the airplane flying south and trailing smoke then banking to the left making a complete circle before descending and ultimately impacting the ground.
Probable cause:
The pilot's intentional operation of the airplane with a known engine boost problem resulting in the improper use of brakes to maintain directional control during takeoff, the brake system fire, and the loss of control for undetermined reasons during the emergency landing. A factor was the loss of engine power due to a restricted wastegate filter.
Final Report:

Crash of a Rockwell Sabreliner 75A in Liberal

Date & Time: Sep 29, 1986 at 1204 LT
Type of aircraft:
Operator:
Registration:
N64
Flight Type:
Survivors:
Yes
Schedule:
Oklahoma City - Liberal
MSN:
380-35
YOM:
1975
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8448
Captain / Total hours on type:
1540.00
Aircraft flight hours:
7327
Circumstances:
The right main landing gear downlock pin retracted just before or during touchdown. The airplane touched down 21 feet short of the runway. It traveled that 21 feet, traveled the full length of the 6999- foot runway, then traveled another one-fourth of a mile and stopped on a golf course. No pre-touchdown mechanical, hydraulic or electrical problems could be found. All four occupants escaped uninjured.
Probable cause:
Occurrence #1: gear collapsed
Phase of operation: landing - flare/touchdown
Findings
1. (c) procedures/directives - not followed - pilot in command
2. (c) gear retraction - inadvertent - copilot/second pilot
----------
Occurrence #2: loss of control - on ground/water
Phase of operation: landing - roll
----------
Occurrence #3: on ground/water encounter with terrain/water
Phase of operation: landing - roll
Findings
3. (f) terrain condition - ditch
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Occurrence #4: on ground/water collision with object
Phase of operation: landing - roll
Findings
4. (f) object - fence
----------
Occurrence #5: on ground/water encounter with terrain/water
Phase of operation: landing - roll
Findings
5. (f) terrain condition - water, glassy
Final Report:

Crash of a Rockwell Grand Commander 680FP near Henryville: 1 killed

Date & Time: Dec 17, 1970 at 1930 LT
Operator:
Registration:
N188HC
Flight Phase:
Survivors:
No
Schedule:
Cincinnati – Liberal
MSN:
680-1220-115
YOM:
1963
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2400
Circumstances:
En route from Cincinnati to Liberal, the twin engine airplane went out of control, entered a dive and crashed in an open field located in the region of Henryville. The pilot, sole on board, was killed.
Probable cause:
Loss of control in flight for undetermined reason. Investigations reported an overload failure and a separation in flight of the elevator assembly (attachments) for unknown reason. The flight phase when the airframe failure occurred remains unknown.
Final Report: