Crash of a Beechcraft E18S in Lone Rock: 1 killed

Date & Time: May 4, 1993 at 0140 LT
Type of aircraft:
Operator:
Registration:
N80CB
Flight Type:
Survivors:
No
Schedule:
Aurora - Minneapolis
MSN:
BA-257
YOM:
1957
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4492
Captain / Total hours on type:
310.00
Aircraft flight hours:
15027
Circumstances:
The pilot of a twin-engine cargo airplane shut down the left engine and feathered the propeller due to a loss of engine oil. The FAA ARTCC handling the flight vectored the airplane toward a VOR. Due to the airplane's altitude and distance from the center's radar, the pilot of the airplane had to perform a full instrument approach procedure. The airplane maintained its enroute assigned altitude until passing the VOR outbound. Ntap readouts show the airplane descending throughout the procedure turn and inbound leg of the approach. The airplane's last radar contact was 300 feet below the inbound altitude for the approach while outside the final approach fix. The airplane collided with trees and terrain approximately 2 1/4 miles from the airport. The VOR is 5.5 miles from the airport. The on-scene investigation revealed the left engine's propeller had been feathered, its number nine cylinder mounting studs on the engine's case were crushed downward or were broken off at the case's surface, and the landing gear had been extended. The pilot, sole on board, was killed.
Probable cause:
The National Transportation Safety Board determines the probable cause(s) of this accident to be: was a pre-mature extension of the landing gear by the pilot which resulted in the inability of
the pilot to maintain the minimum descent altitude. Factors related to the accident were the loose cylinder and loss of oil.
Final Report:

Crash of a Beechcraft G18AS in DuPage

Date & Time: Dec 4, 1991 at 0405 LT
Type of aircraft:
Operator:
Registration:
N38RM
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
DuPage - Covington
MSN:
BA-574
YOM:
1961
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4571
Captain / Total hours on type:
330.00
Circumstances:
The pilot stated she felt the twin engined tailwheel cargo airplane yaw to the right during takeoff. The pilot stated she applied left rudder and set differential power to correct for the perceived right hand crosswind. As the airplane lifted off, it made a sharp right turn and performed left and right banks leveling off prior to colliding with the ground. The airplane slid through security fences and a fuel supply depot before stopping. The newspaper bundle cargo moved from the two forward bays to the aft end of the cargo compartment. The newspapers were covered with plastic wrapper. The cargo compartment floor was slippery when walked upon and had traces of snow on it. According to the pilot the cargo was covered by a cargo net secured at the forward end but not at the aft end. Two cargo straps were crisscrossed over the net and secured at the aft end of the cargo load. The left throttle was found in the full forward position. The right throttle was found one inch aft of the full forward position.
Probable cause:
A result of the pilot in command's not maintaining directional control, an improper inflight decision, and improper remedial action once the loss of directional control was recognized by the pilot. Factors contributing to this accident are inadequate cargo restraints, loose cargo, and improper security of the cargo not observed by the pilot. Additional factors contributing to this accident are the inadequate standards for aircraft equipment and training provided by the company employing and operating the airplane.
Final Report:

Crash of a Beechcraft E18S in Chicago: 1 killed

Date & Time: Sep 28, 1986 at 2254 LT
Type of aircraft:
Operator:
Registration:
N101VE
Flight Type:
Survivors:
No
Site:
Schedule:
Chicago - Covington
MSN:
BA-190
YOM:
1956
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
6400
Captain / Total hours on type:
2059.00
Aircraft flight hours:
17743
Circumstances:
The aircraft had departed on runway 13. He was then directed to climb to 6,000 feet. Thirty seconds later he advised he had engine trouble and was returning to the airport. Shortly thereafter he advised he could not maintain altitude. The aircraft, one mile southeast of the airport, struck the roofs of two family type residences. Then struck two garages, ground impacted and struck the rear area of a third residence. An intense fire followed. Left engine had impeller failure. Propeller was pitched between low and high rpm. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: loss of engine power (total) - mech failure/malf
Phase of operation: climb - to cruise
Findings
1. (f) eng assembly, blower/impeller/integral supercharger - failure, total
2. (f) lubricating system - lack of
----------
Occurrence #2: airframe/component/system failure/malfunction
Phase of operation: descent - emergency
Findings
3. (c) propeller system/accessories, feathering system - incorrect
4. Propeller feathering - attempted - pilot in command
5. (c) propeller system/accessories, feathering system - movement restricted
----------
Occurrence #3: forced landing
Phase of operation: descent - emergency
----------
Occurrence #4: in flight collision with object
Phase of operation: descent - emergency
Findings
6. (c) object - residence
----------
Occurrence #5: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report: