Crash of a De Havilland Dash-8-Q402 in Vilnius

Date & Time: Sep 12, 2007 at 0136 LT
Operator:
Registration:
LN-RDS
Survivors:
Yes
Schedule:
Copenhagen - Palanga
MSN:
4035
YOM:
2001
Flight number:
SK2748
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
48
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7928
Captain / Total hours on type:
291.00
Copilot / Total flying hours:
4674
Copilot / Total hours on type:
262
Aircraft flight hours:
11366
Aircraft flight cycles:
14224
Circumstances:
The aircraft departed Copenhagen-Kastrup AIrport on a flight to Palanga with 48 passengers and a crew of 4 on board. Following an uneventful flight, the crew started the descent. At an altitude of about 2,000 feet, the crew selected the landing gear down. However, the right-hand main gear extended but did not lock down and the landing gear doors did not close. The approach was abandoned and the crew initiated a go-around. During the second attempt to land, the crew recycled the system but the warning remained so the decision was taken to divert to Vilnius. On approach, the crew attempted to release the undercarriage using a backup system, but the undercarriage control panel still showed an unsafe warning. The right engine was shut down and the propeller was feathered prior to landing. Upon touchdown, the right main gear collapsed. The aircraft veered off runway and came to rest 40 metres further, some 1,150 metres pas the runway threshold. All 52 occupants evacuated safely and the aircraft was damaged beyond repair.
Probable cause:
The aircraft accident was caused by the separation of the piston rod of the extension/retraction actuator from the rod end during right hand main landing gear extension due to thread connection corrosion. The freely falling landing gear broke the apex hinge lugs of the stabilizer sections, the right hand landing gear did not lock in the extended position and collapse occurred when the aircraft was rolling after landing.
Final Report:

Crash of a De Havilland Dash-8-Q402 in Aalborg

Date & Time: Sep 9, 2007 at 1557 LT
Operator:
Registration:
LN-RDK
Survivors:
Yes
Schedule:
Copenhagen - Aalborg
MSN:
4025
YOM:
2000
Flight number:
SK1209
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
69
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
17000
Captain / Total hours on type:
1000.00
Copilot / Total flying hours:
6540
Copilot / Total hours on type:
1085
Aircraft flight hours:
12141
Aircraft flight cycles:
14795
Circumstances:
The accident flight was a scheduled domestic flight from Copenhagen Airport, Kastrup (EKCH) to Aalborg Airport (EKYT). The flight was uneventful until the landing gear was selected down during the approach to EKYT runway 26R. The nose landing gear and the left main landing gear (MLG) indicated down and locked. The right MLG indicated “in transit” (not down and locked). The Aalborg Tower was informed about the problem with the right MLG indication. A go-around was initiated at 1100 feet MSL with a climb towards 2000 ft. The flight crew consulted the Quick Reference Handbook (QRH). An alternate landing gear procedure was initiated. The right MLG indication remained in “transit”. A mayday call was made to Aalborg Tower and they were informed about the unsafe landing gear. The flight crew reset the alternate gear extension system and subsequently they tried to make a normal gear up selection. The nose landing gear and the left MLG retracted normally, however the right main landing gear indication remained in “transit”. A second attempt to use the alternate landing gear extension procedure was performed without any changes to the right MLG indication. The aircraft entered a holding pattern in order to reduce the amount of fuel and at the same time to brief the passengers about the situation and to prepare the passengers for an emergency landing. Passengers seated at rows 6, 7 and 8 seats D and F were reseated away from the right propeller area. During the approach the flaps were selected to 10° and the landing gear horn started. The warning horn continued throughout the remaining flight. During the emergency landing the left MLG touched down on the runway first, followed by the right MLG. Shortly after the right MLG contacted the runway the right MLG collapsed. The aircraft departed the runway to the right and came to rest on a heading of 340° at 1357:26 hrs.
Probable cause:
There were five factors’ leading to the accident:
1. There were no specified inspection tasks for inspection of the MLG retraction/extension actuator and rod end either in the MRB’s report or in the Maintenance Requirement Manual in so far as “L”, “A” and “C” checks.
2. The right and left MLG retraction/extension actuator piston and rod end were made of noble martensitic stainless steel and the less noble 4340 steel material, respectively.
3. Severe corrosion in the threaded connection between the right MLG actuator rod and rod end.
4. Separation of the right MLG retraction/extension actuator from the actuator piston rod end.
5. The right MLG stabilizer joint lugs failed.
Final Report:

Crash of a Partenavia P.68C Victor in Bangalore: 4 killed

Date & Time: Sep 8, 2007 at 1520 LT
Type of aircraft:
Operator:
Registration:
VT-JOY
Flight Phase:
Survivors:
No
Schedule:
Bangalore – Cochin
MSN:
436
YOM:
2004
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
3140
Circumstances:
The aircraft departed Bangalore-Hindustan Airport runway 27 at 1514LT on a flight to Cochin with 3 passengers and one pilot on board. Six minutes after takeoff, the pilot reported technical problems and elected to return for an emergency landing. However, the aircraft entered an uncontrolled descent and crashed in the lakebed of the Gawdanapalya Lake located about 9 km southwest of the airport. The aircraft was destroyed and all four occupants were killed.
Probable cause:
Engine power loss during initial climb after the aircraft had been refueled with Jet fuel instead of Avgas 100LL.
The following contributing factors were identified:
- The low experience of the pilot on type,
- The non-compliance of correct refueling procedure and its supervision by IOC personnel and pilot or operator's representative.
Final Report:

Crash of an Antonov AN-12BP in Goma: 8 killed

Date & Time: Sep 7, 2007 at 1200 LT
Type of aircraft:
Registration:
4L-SAS
Flight Type:
Survivors:
No
Schedule:
Kisangani – Goma – Bukavu
MSN:
3 3 411 08
YOM:
1970
Location:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
8
Circumstances:
The four engine aircraft departed Kisangani on a cargo flight to Bukavu with an intermediate stop in Goma, carrying 3 passengers, 5 crew members and a load consisting of 18 tons of palm oil. After landing, the aircraft was unable to stop within the remaining distance and overran. While contacting petrified lava, it lost its undercarriage and came to rest, bursting into flames. The aircraft was totally destroyed and all 8 occupants were killed. It was reported that the certificate of airworthiness expired last March and was not renewed since.

Crash of a Rockwell Sabreliner 75 in San José

Date & Time: Sep 3, 2007
Type of aircraft:
Operator:
Registration:
N726JR
Flight Phase:
Survivors:
Yes
Schedule:
San José – Cartagena
MSN:
370-4
YOM:
1971
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
During the takeoff roll from San José-Juan Santamaria Airport runway 07, one of the tyre burst. The captain decided to abandon the takeoff procedure and initiated an emergency braking manoeuvre. Unable to stop within the remaining distance, the aircraft overran, lost its undercarriage, hit obstacles and came to rest near the perimeter fence. All six occupants escaped uninjured while the aircraft was damaged beyond repair.

Crash of a Cessna 208B Grand Caravan in Port-au-Prince

Date & Time: Aug 31, 2007 at 1645 LT
Type of aircraft:
Operator:
Registration:
HH-CAR
Flight Phase:
Survivors:
Yes
Schedule:
Port-au-Prince – Cap Haïtien
MSN:
208B-0699
YOM:
1998
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Shortly after takeoff from Port-au-Prince-Toussaint Louverture Airport runway 10, while in initial climb, the engine lost power. The pilot attempted an emergency landing when the aircraft crash landed in Croix-des-Bouquets, about 5 km east of the airport, coming to rest upside down. A passenger was slightly injured and the aircraft was damaged beyond repair.

Crash of a Piper PA-31T Cheyenne II in Madison

Date & Time: Aug 31, 2007 at 1218 LT
Type of aircraft:
Operator:
Registration:
N199MA
Flight Type:
Survivors:
Yes
MSN:
31-8104005
YOM:
1981
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On approach to Madison-Dane County-Truax Field, the pilot encountered technical problems with the right main gear that remained stuck in its wheel well. He decided to retract the gear and to complete a wheels-up landing. The twin engine aircraft belly landed and slid for few dozen metres before coming to rest. Both occupants escaped uninjured and the aircraft was damaged beyond repair.

Crash of a Lockheed C-130K Hercules in Afghanistan

Date & Time: Aug 29, 2007
Type of aircraft:
Operator:
Registration:
XV205
Flight Type:
Survivors:
Yes
MSN:
4230
YOM:
1967
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The airplane landed hard on a rough airstrip located in the Helmand Province in Afghanistan. The aircraft was damaged beyond repair but all occupants escaped uninjured. Due to Taliban presence in the vicinity of the accident area, the airplane was deliberately destroyed by fire.

Ground fire of an Antonov AN-32B in Mitú

Date & Time: Aug 27, 2007 at 0950 LT
Type of aircraft:
Operator:
Registration:
HK-4117
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Villavicencio – Mitú
MSN:
29 09
YOM:
1992
Country:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft completed a cargo flight from Villavicencio to Mitú, carrying four crew members and a load consisting of fuel drums. After all fuel drums were offloaded by ground crew, the pilot contacted the fire brigade because fuel leaked on the cabin floor and around the aircraft. Airport firefighters approached to attend the event but were not allowed the use or foam or water due to electrical and electronic equipment that could be affected by the liquid. After starting the APU and the right engine for the flight back to Villavicencio, an explosion occurred. The crew shut down the engines and evacuated the aircraft. Firefighters were unable to extinguish the rapidly developing fire and the aircraft was totally destroyed.
Probable cause:
Lack of adequate and effective procedures for fuel handling by the company and crew. Non-compliance by the crew of the aircraft, of the recommendations made by the Fire Fighting Service Airport and Control Tower.
Final Report:

Crash of an Antonov AN-32 in Kongolo: 14 killed

Date & Time: Aug 26, 2007 at 1600 LT
Type of aircraft:
Registration:
9Q-CAC
Flight Type:
Survivors:
Yes
Schedule:
Kongolo – Goma
MSN:
14 07
YOM:
1987
Location:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
12
Pax fatalities:
Other fatalities:
Total fatalities:
14
Circumstances:
The aircraft departed Kongolo on a cargo flight to Goma with 12 passengers, a crew of 3 and a load consisting of 9 tons of cassiterite on board. Ten minutes after takeoff, the crew informed ATC about engine problem and decided to return to Kongolo. On approach, the aircraft stalled, collided with trees and crashed in a wooded area located 3 km short of runway. A young boy aged two survived while 14 other occupants were killed. Not sure if the image here above refers to this accident.