Region

Crash of a Shaanxi Y-8F-200W in Lengpui

Date & Time: Jan 23, 2024 at 1019 LT
Type of aircraft:
Operator:
Registration:
5821
Flight Type:
Survivors:
Yes
Location:
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
After touchdown on runway 35 at Lengpui Airport, the four engine airplane encountered difficulties to stop within the remaining distance. It overran, rolled through bushes, went down an embankment and came to rest, broken in two. All 14 occupants were rescued, among them eight were injured. The plane was dispatched to Lengpui to pick up 92 soldiers from the Myanmar Army who should be repatriated to Myanmar on behalf of the 7th Squadron. These Myanmarese soldiers crossed over to India last week, following gunfights with ethnic insurgent group 'Arakan Army'.

Crash of a Learjet 45 in Mumbai

Date & Time: Sep 14, 2023 at 1705 LT
Type of aircraft:
Operator:
Registration:
VT-DBL
Survivors:
Yes
Schedule:
Visakhapatnam – Mumbai
MSN:
45-404
YOM:
2009
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The approach to Mumbai-Chhatrapati Shivaji Airport was completed in poor weather conditions with reduced visibility due to heavy rain falls. On short final, the airplane was in a nose down attitude and rolling to the right when it impacted the runway surface. It went out of control, veered off runway and came to rest in a grassy area, broken in two. A small fire was quickly extinguished. All eight occupants were injured.

Crash of a Beechcraft B250GT Super King Air in Gwalior

Date & Time: May 6, 2021 at 2115 LT
Operator:
Registration:
VT-MPQ
Flight Type:
Survivors:
Yes
Schedule:
Indore - Gwalior
MSN:
BY-373
YOM:
2020
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
12324
Captain / Total hours on type:
9362.00
Copilot / Total flying hours:
5135
Copilot / Total hours on type:
50
Aircraft flight hours:
49
Circumstances:
Beechcraft Super King Air B200GT aircraft, VT-MPQ belonging to the Directorate of Aviation, Government of Madhya Pradesh (DoA,GoMP) was involved in an accident on 06.05.2021 while operating a flight from Indore Airport to Gwalior. The flight was under the command of an ATPL holder with another CPL holder as Co-Pilot. There was one passenger on board in addition. The flight crew contacted ATC Indore for clearance to operate the flight to Gwalior. The aircraft was cleared for Gwalior via airway W10N and FL270. Aircraft departed from RWY25 at Indore and climbed to FL 270. Aircraft descended into Gwalior in coordination with Delhi and Gwalior. Approaching Gwalior the crew were advised by the ATC that RWY24L was in use. ATC then asked the crew if they would like to carry out a VOR approach for the opposite RWY 06R. The crew requested for a visual approach for RWY 06R in the night time and were cleared to descend 2700 ft and called field in sight at 25 NM. Crew then requested for right base RWY 06R and were cleared to circuit altitude. Crew called turning right base with field visual and were cleared to land which the crew acknowledged. Just before landing the aircraft and short of the threshold, the main gear collided with the raised arrester barrier and came to a halt on the Runway 06R just beyond the threshold markings at 1515 UTC. The aircraft was substantially damaged, however there was no post impact fire. The 2 crew and 1 passenger received minor to serious injuries.
Probable cause:
The PIC (PF) carrying out a visual approach at night and knowingly deviated below the visual approach path profile (3°) while disregarding the PAPI indications, thereby the aircraft collided with the raised Arrester Barrier. Lack of assertiveness on the part of the copilot (PM).
The following contributing factors were identified:
- Non-Compliance to the SOP of “Change of Runway Checklist” by the ATC staff leading to the 'Arrester Barrier' remaining in a 'Raised Position' while the aircraft (VT-MPQ) came in for landing on runway 06R.
- Non-essential conversation by the flight crew during the final approach for landing causing distraction leading to a delayed sighting of the raised Arrester Barrier.
- Systemic failure at various levels at the Gwalior Air Force Base to ensure that the 'Arrester Barrier Position Indicator Lights and Integral Panel Lights' were not rectified in a stipulated time period.
- A robust alternate procedure was not defined when the 'Arrester Barrier Position Indicator Lights and Integral Panel Lights' were unserviceable.
- The Gwalior Airforce Base authorities did not install 'Red Obstacle Lights' on the Arrester Barrier Poles to indicate the position of the obstacle on the date of the accident as per the DGCA requirements (CAR Section 4, Series B, Part 1).
Final Report:

Crash of a Partenavia P.68C Observer 2 in Bhopal

Date & Time: Mar 27, 2021 at 1605 LT
Type of aircraft:
Operator:
Registration:
VT-TAA
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Bhopal - Guna
MSN:
398-07-OB2
YOM:
1994
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
772
Captain / Total hours on type:
472.00
Copilot / Total flying hours:
458
Copilot / Total hours on type:
220
Aircraft flight hours:
2835
Circumstances:
The aircraft was under the command of a CPL holder pilot-in-command (PIC), who was Pilot Flying (PF). PIC was assisted by a CPL holder copilot, who was pilot monitoring (PM). One passenger (Director of Operations M/s PAPL) was also onboard. The aircraft took off from Bhopal airport uneventfully. After takeoff, at about 20 NM, the crew observed abnormal noise followed by low oil pressure and high oil temperature indication on aircraft’s LH engine. Crew assessed the situation and decided to turn back to Bhopal. The crew however, reported to ATC Bhopal that they are returning back due to wind and turbulence. While returning, crew shutdown the LH engine. Post LH engine shut down, crew gave a call to ATC, Bhopal requested to land the aircraft on the taxiway (disuse runway). ATC did not agree to the request, as there was no cross runway at Bhopal. The ATC was also not made aware of the prevailing emergency situation by the crew. When ATC declined the request, the crew informed ATC, that they might be doing force landing. ATC Bhopal immediately responded and asked the crew to land on Runway 12. However, the crew carried out a force landing in an agriculture field approximately 3 NM from Bhopal Airport. During the force landing, the PIC received serious injury and the copilot and passenger received minor injuries.The aircraft sustained substantial damages.
Probable cause:
The probable cause of the accident was Oil leak from the LH engine during the flight. Consequently, oil starvation and lack of lubrication resulted in excessive heat generation amongst the frictional components. Due to excessive heat, the bearing of no. 4 piston connecting rod failed and broke into pieces. However, the root cause of the LH engine oil leak could not be conclusively established. Subsequent to LH engine seizure, the crew did not follow the emergency procedures for single engine operation and took a decision to come for landing with single engine (RH). The crew further aggravated the emergency situation by not communicating the actual reason with ATC, displaying gross lack of situational awareness in handling the emergency. Crew estimated that they cannot reach the airport runway due to the low altitude and force landed the aircraft before the airport.
Final Report:

Crash of a Boeing 737-8HG in Kozhikode: 21 killed

Date & Time: Aug 7, 2020 at 1941 LT
Type of aircraft:
Operator:
Registration:
VT-AXH
Survivors:
Yes
Schedule:
Dubai - Kozhikode
MSN:
36323/2109
YOM:
2006
Flight number:
IX1344
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
184
Pax fatalities:
Other fatalities:
Total fatalities:
21
Captain / Total flying hours:
10848
Captain / Total hours on type:
4612.00
Copilot / Total flying hours:
1989
Copilot / Total hours on type:
1723
Aircraft flight hours:
43691
Aircraft flight cycles:
15309
Circumstances:
Air-India Express Limited B737-800 aircraft VT-AXH was operating a quick return flight on sector Kozhikode-Dubai-Kozhikode under ‘Vande Bharat Mission’ to repatriate passengers who were stranded overseas due to closure of airspace and flight operations owing to the Covid-19 pandemic. The aircraft departed from Kozhikode for Dubai at 10:19 IST (04:49 UTC) on 07 August 2020 and landed at Dubai at 08:11 UTC. The flight was uneventful. There was no change of crew and no defect was reported on the first sector. The aircraft departed from Dubai for Kozhikode at 10:00 UTC as flight AXB 1344 carrying 184 passengers and six crew members. AXB 1344 made two approaches for landing at Kozhikode. The aircraft carried out a missed approach on the first attempt while coming into land on runway 28. The second approach was on runway 10 and the aircraft landed at 14:10:25 UTC. The aircraft touched down approximately at 4,438 ft on 8,858 ft long runway, in light rain with tailwind component of 15 knots and a ground speed of 165 knots. The aircraft could not be stopped on the runway and this ended in runway overrun. The aircraft exited the runway 10 end at a ground speed of 84 knots and then overshot the RESA, breaking the ILS antennae and a fence before plummeting down the tabletop runway. The aircraft fell to a depth of approximately 110 ft below the runway elevation and impacted the perimeter road that runs just below the tabletop runway, at a ground speed of 41 knots and then came to an abrupt halt on the airport perimeter road just short of the perimeter wall. There was fuel leak from both the wing tanks; however, there was no postcrash fire. The aircraft was destroyed and its fuselage broke into three sections. Both engines were completely separated from the wings. The rescue operations were carried out by the ARFF crew on duty with help of Central Industrial Security Force (CISF) personnel stationed at the airport and several civilians who rushed to the crash site when the accident occurred. Upon receipt of the information about the aircraft crash the district administration immediately despatched fire tenders and ambulances to the crash site. Nineteen passengers were fatally injured and Seventy Five passengers suffered serious injuries in the accident while Ninety passengers suffered minor or no injuries. Both Pilots suffered fatal injuries while one cabin crew was seriously injured and three cabin crew received minor injuries. The rescue operation was completed at 16:45 UTC (22:15 IST).
Probable cause:
The probable cause of the accident was the non adherence to SOP by the PF, wherein, he continued an unstabilized approach and landed beyond the touchdown zone, half way down the runway, in spite of ‘Go Around’ call by PM which warranted a mandatory ‘Go Around’ and the failure of the PM to take over controls and execute a ‘Go Around’.

The following contributing factors were identitified:

The investigation team is of the opinion that the role of systemic failures as a contributory factor cannot be overlooked in this accident. A large number of similar accidents/incidents that have continued to take place, more so in AIXL, reinforce existing systemic failures within the aviation sector. These usually occur due to prevailing safety culture that give rise to errors, mistakes and violation of routine tasks performed by people operating within the system. Hence, the contributory factors enumerated below include both the immediate causes and the deeper or systemic causes.

(i) The actions and decisions of the PIC were steered by a misplaced motivation to land back at Kozhikode to operate next day morning flight AXB 1373. The unavailability of sufficient number of Captains at Kozhikode was the result of faulty AIXL HR policy which does not take into account operational requirement while assigning permanent base to its Captains. There was only 01 Captain against 26 First Officers on the posted strength at Kozhikode.

(ii) The PIC had vast experience of landing at Kozhikode under similar weather conditions. This experience might have led to over confidence leading to complacency and a state of reduced conscious attention that would have seriously affected his actions, decision making as well as CRM.

(iii) The PIC was taking multiple un-prescribed anti-diabetic drugs that could have probably caused subtle cognitive deficits due to mild hypoglycaemia which probably contributed to errors in complex decision making as well as susceptibility to perceptual errors.

(iv) The possibility of visual illusions causing errors in distance and depth perception (like black hole approach and up-sloping runway) cannot be ruled out due to degraded visual cues of orientation due to low visibility and suboptimal performance of the PIC’s windshield wiper in rain.

(v) Poor CRM was a major contributory factor in this crash. As a consequence of lack of assertiveness and the steep authority gradient in the cockpit, the First Officer did not take over the controls in spite of being well aware of the grave situation. The lack of effective CRM training of AIXL resulted in poor CRM and steep cockpit gradient.

(vi) AIXL policies of upper level management have led to a lack of supervision in training, operations and safety practices, resulting in deficiencies at various levels causing repeated human error accidents in AIXL

(vii) The AIXL pilot training program lacked effectiveness and did not impart the requisite skills for performance enhancement. One of the drawbacks in training was inadequate maintenance and lack of periodic system upgrades of the simulator. Frequently recurring major snags resulted in negative training. Further, pilots were often not checked for all the mandatory flying exercises during simulator check sessions by the Examiners.

(viii) The non availability of OPT made it very difficult for the pilots to quickly calculate accurate landing data in the adverse weather conditions. The quick and accurate calculations would have helped the pilots to foresee the extremely low margin for error, enabling them to opt for other safer alternative.

(ix) The scrutiny of Tech Logs and Maintenance Record showed evidence of nonstandard practice of reporting of certain snags through verbal briefing rather than in writing. There was no entry of windshield wiper snag in the Tech log of VT-AXH. Though it could not be verified, but a verbal briefing regarding this issue is highly probable.

(x) The DATCO changed the runway in use in a hurry to accommodate the departure of AIC 425 without understanding the repercussions on recovery of AXB 1344 in tail winds on a wet runway in rain. He did not caution AXB 1344 of prevailing strong tail winds and also did not convey the updated QNH settings.

(xi) Accuracy of reported surface winds for runway 10 was affected by installation of wind sensor in contravention to the laid down criteria in CAR. This was aggravated by frequent breakdown due to poor maintenance.

(xii) The Tower Met Officer (TMO) was not available in the ATC tower at the time of the accident. The airfield was under two concurrent weather warnings and it is mandatory for the TMO to be present to update and inform the fast changing weather variations to enhance air safety. During adverse weather conditions the presence of the TMO in the ATC tower was even more critical.

(xiii) The AAI has managed to fulfil ICAO and DGCA certification requirements at Kozhikode aerodrome for certain critical areas like RESA, runway lights and approach lights. Each of these, in isolation fulfils the safety criteria however, when considered in totality, this left the aircrew of AXB 1344 with little or no margin for error. Although not directly contributory to the accident causation, availability of runway centreline lights would have certainly enhanced the spatial orientation of the PIC.

(xiv) The absence of a detailed proactive policy and clear cut guidelines by the Regulator on monitoring of Long Landings at the time of the accident was another contributory factor in such runway overrun accidents. Long Landing has been major factor in various accidents and incidents involving runway excursion since 2010 and has not been addressed in CAR Section 5, Series F, Part II.

(xv) DGCA did not comprehensively revise CAR Section 5, Series F, Part II Issue I, dated 30 Sep 99 (Rev. on 26 Jul 2017) on ‘Monitoring of DFDR/QAR/PMR Data for Accident/Incident Prevention’ to address the recommendations of the COI of 2010 AIXL Managlore Crash regarding the exceedance limits, resulting in the persisting ambiguities in this matter.

(xvi) DFDR data monitoring for prevention of accidents/incidents is done by AIXL. However 100% DFDR monitoring is not being done, in spite of the provisions laid down in the relevant CAR and repeated audit observations by DGCA. DFDR data monitoring is the most effective tool to identify exceedance and provide suitable corrective training in order to prevent runway accidents like the crash of AXB 1344. However, ATR submitted by AIXL on the said findings were accepted by DGCA year after year without ascertaining its implementation or giving due importance to its adverse implications.
Final Report:

Crash of a Cessna 560XL Citation Excel in Aligarh

Date & Time: Aug 27, 2019 at 0840 LT
Operator:
Registration:
VT-AVV
Flight Type:
Survivors:
Yes
Schedule:
New Delhi - Aligarh
MSN:
560-5259
YOM:
2002
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5484
Captain / Total hours on type:
1064.00
Copilot / Total flying hours:
1365
Copilot / Total hours on type:
1060
Aircraft flight hours:
7688
Circumstances:
On 27 Aug 19, M/s Air Charter Services Pvt Ltd Cessna Citation 560 XL aircraft (VTAVV), while operating a flight from Delhi to Aligarh (Dhanipur Airstrip) was involved in an accident during landing on runway 11.The operator is having a maintenance facility at Aligarh Airport and aircraft was scheduled to undergo ADS-B modification. There were 02 cockpit crew and 04 SOD onboard the aircraft. The aircraft was under the command of a PIC, who was an ATPL holder duly qualified on type with a CPL holder co-pilot, duly qualified on type as Pilot Monitoring. This was the first flight of the day for both pilots. Both, PIC and Co-Pilot had prior experience of operating to Aligarh airport, which is an uncontrolled airport. As per the flight plan, ETD from Delhi was 0800 IST and ETA at Aligarh was 0820 IST. The crew had reported around 0630 IST at Delhi airport and underwent BA test. The MET report to operate the aircraft to Aligarh was well within the VFR conditions. The aircraft Take-off weight was within limits including 1900 Kgs of fuel on board. As per the statement of PIC, the Co-pilot was briefed about pre departure checklists including METAR before approaching the aircraft. Once at the aircraft, prefight checks were carried out by PIC before seeking clearance from Delhi delivery (121.95 MHz). Aircraft was accorded start up clearance by Delhi ground (121.75 Mhz) at 0800 IST.ATC cleared the aircraft to line up on runway 11 and was finally cleared for takeoff at 0821 IST. After takeoff, aircraft changed over to Delhi radar control from tower frequency for further departure instructions. Aircraft was initially cleared by Radar control to climb to FL090 and was given straight routing to Aligarh with final clearance to climb to FL130. Thereafter, aircraft changed to Delhi area control for further instructions. While at approximately 45 Nm from Aligarh, VT-AVV made contact with Aligarh (personnel of M/s Pioneer Flying Club manning radio) on 122.625 MHz. Ground R/T operator informed “wind 100/2-3 Kts, QNH 1005, Runway 11 in use” and that flying of Pioneer Flying Club is in progress. Further, he instructed crew to contact when at 10 Nm inbound. After obtaining initial information from ground R/T operator, VT-AVV requested Delhi area control for descent. The aircraft was cleared for initial descent to FL110 and then further to FL080. On reaching FL080, aircraft was instructed by Delhi area control to change over to Aligarh for further descent instruction in coordination with destination. At approx 10 Nm, VT-AVV contacted ground R/T operator on 122.625 MHz and requested for long finals for runway 11. In turn, ground R/T operator asked crew to report when at 5 Nm inbound. As per PIC, after reaching 5 Nm inbounds, Aligarh cleared VTAVV to descend to circuit altitude and land on runway 11. Aircraft had commenced approach at 5 Nm at an altitude of 2200 ft. Approach and landing checks briefing including wind, runway in use were carried out by PIC. During visual approach, Co-pilot called out to PIC “Slightly low on profile”. As per PIC, Co-pilot call out was duly acknowledged and ROD was corrected. Thereafter, PIC was visual with runway and took over controls on manual. Co-pilot was monitoring instruments and parameters. While PIC was focused on landing, a loud bang from left side of the aircraft was heard by PIC when the aircraft was below 100 feet AGL. Aircraft started pulling towards left and impacted the ground short of runway 11 threshold. After impact, aircraft veered off the runway and its left wing caught fire. The aircraft stopped short of airfield boundary wall. Crew carried out emergency evacuation. Co-pilot opened main exit door from inside of the aircraft for evacuation of passengers. Aircraft was destroyed due to post crash fire. The fire tender reached the crash site after 45 Minutes.
Probable cause:
While landing on runway 11, aircraft main landing gears got entangled in the powerline crossing extended portion of runway , due to which aircraft banked towards left and crash landed on extended portion of runway 11.
Contributory factors:
- It appears that there was a lack of proper pre-flight briefing, planning, preparation and assessment of risk factors.
- Non-Adherence to SOP.
- Sense of complacency seems to have prevailed.
Final Report:

Crash of a Boeing 737-85R in Mumbai

Date & Time: Jul 1, 2019 at 2351 LT
Type of aircraft:
Operator:
Registration:
VT-SYK
Survivors:
Yes
Schedule:
Jaipur - Mumbai
MSN:
30410/1228
YOM:
2002
Flight number:
SG6237
Country:
Region:
Crew on board:
7
Crew fatalities:
Pax on board:
160
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5355
Captain / Total hours on type:
5113.00
Copilot / Total flying hours:
4826
Copilot / Total hours on type:
4625
Circumstances:
On 01.07.2019, B737-800 aircraft was involved in an accident (runway excursion) at Mumbai airport while landing in moderate to heavy rain. The aircraft was under the command of an ATPL holder (PF) with a CPL holder as First Officer (PM). There were 160 passengers and 7 crew members on board. There was no injury to any of the passengers or crew members. The aircraft suffered substantial damage. The subject flight was fifth of the day for the aircraft and second for the flight crew. The flight crew had earlier operated Mumbai-Jaipur sector and the incident flight was from Jaipur to Mumbai. There were no technical issues reported by the flight crew either during Mumbai Jaipur sector or on the return leg (Jaipur- Mumbai) till descent into Mumbai. The pilots had carried out briefing amongst themselves for the approach including the weather and Go Around actions, if required. The aircraft commenced descent into Mumbai in the late evening hours. As per the reported weather at the time of approach visibility was 2100 metres in rain making it dark. Reported winds were 090/12 Knots. Runway was wet and the trend provided was ³temporary reduction in visibility to 1500 metres with thunder/ showers of rain´. During descend at approximately 7000' Pressure Altitude, the crew observed an indication for IAS disagree, indicating a discrepancy of airspeed between the instrument sources for the flight crew. Although this indication was momentary, the 'Non-Normal Checklist' was carried out. The indication discrepancy did not recur for the remainder of the flight. The aircraft was radar vectored for an ILS approach for Runway 27 at Mumbai. The approach was stabilized by 3800' Pressure Altitude with landing gear down, flaps 30 and auto brake selected at 3. The autopilot was engaged throughout the descent phase and during approach, the second autopilot was also coupled for the ILS approach. At 100', the autopilot and the auto-throttle were disengaged by the PF. The flare manoeuvre consumed approximately 5807' of the runway length prior to the aircraft touchdown with 3881' of runway remaining. After touchdown, the speed brakes deployed automatically and maximum reverse thrust and wheel brakes were applied. The aircraft exited the paved surface at 65 Knots and came to rest at a distance of 615' beyond the end of the runway. Once the aircraft came to rest, the flight crew advised cabin crew to be at their stations. The pilots were unable to contact ATC through VHF communication. The PF contacted his airline personnel using mobile phone and informed that the aircraft had overrun the runway and requested for step ladders. The ATC activated fire services and the runway was closed for operation. The Cabin crew carried out check on the passengers in the cabin. The fire services reached the aircraft location and verbal communication was established with the flight crew once the cockpit window was opened. Two Fire Services personnel boarded the aircraft from the L1 door using a fire ladder. An assessment of the aircraft structure and occupants was made and the fire services personnel informed the cabin crew that deplaning was to be carried out using fire ladders. There were no injuries during evacuation or otherwise.
Probable cause:
The runway excursion occurred because of combination of:
- Disconnection of auto pilot at an altitude 118' RA with the nose up trim bias without adequate compensation.
- Disconnection of auto throttle at 118' RA at a higher thrust setting for that phase of flight.
- Late touchdown of the aircraft on the runway.
- Reduced visual cues due to heavy rain impacting depth perception and ascertaining of actual touchdown position.
- Tailwind conditions at the time of landing resulting In increasing the distance covered during the extended flare (float).
- Approach with lower flaps (30) than recommended (40).
Final Report:

Crash of an Antonov AN-32 near Lipo: 13 killed

Date & Time: Jun 3, 2019 at 1300 LT
Type of aircraft:
Operator:
Registration:
K2752
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Jorhat - Mechuka
MSN:
10 09
YOM:
1987
Country:
Region:
Crew on board:
8
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
13
Circumstances:
The airplane departed Jorhat Airport at 1227LT on a flight to Mechuka, Arunachal Pradesh. About half an hour later, while in cruising altitude, radio and radar contact were lost. SAR operations were quickly initiated and the wreckage was spotted eight days later, on June 11, by the crew of a Mil Mi-17 helicopter. The wreckage was found at an altitude of 12,000 feet in a wooded and steep area, about 16 km north of Lipo and 32 km east of Mechuka Airport. The aircraft was totally destroyed and all 13 occupants were killed.

Crash of a Beechcraft C90A King Air in Mumbai: 5 killed

Date & Time: Jun 28, 2018 at 1315 LT
Type of aircraft:
Operator:
Registration:
VT-UPZ
Flight Type:
Survivors:
No
Site:
Schedule:
Juhu - Juhu
MSN:
LJ-1400
YOM:
1995
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
Following a technical maintenance, a test flight was scheduled with two engineers and two pilots. The twin engine airplane departed Mumbai-Juhu Airport and the crew completed several manoeuvres over the city before returning. On approach in heavy rain falls, the aircraft went out of control and crashed at the bottom of a building under construction located in the Ghatkopar West district, some 3 km east from Mumbai Intl Airport, bursting into flames. The aircraft was destroyed by impact forces and a post crash fire and all four occupants were killed as well as one people on the ground.

Crash of a Beechcraft 200 Super King Air in New Delhi: 10 killed

Date & Time: Dec 22, 2015 at 0938 LT
Operator:
Registration:
VT-BSA
Flight Phase:
Survivors:
No
Site:
Schedule:
New Delhi - Ranchi
MSN:
BB-1485
YOM:
1994
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
10
Captain / Total flying hours:
964
Captain / Total hours on type:
764.00
Copilot / Total flying hours:
891
Copilot / Total hours on type:
691
Aircraft flight hours:
4766
Aircraft flight cycles:
2745
Circumstances:
Beechcraft Super King Air B-200 aircraft, VT-BSA belonging to BSF Air Wing was involved in an accident on 22.12.2015 while operating a flight from IGI Airport, New Delhi to Ranchi. The flight was under the command of a CPL holder with another CPL holder as Second-in-Command. There were ten persons on board including two flight crew members. As per the scheduling procedure of the Operator, the flying programme for 22.12.2015 was approved by the ADG (Logistics) on the recommendation of the DIG (Air) for VT-BSA on 21.12.2015. The programme included names of the flight crew along with the following sectors: from Delhi to Ranchi ETD 0800 ETA 1030 and from Ranchi to Delhi ETD 1300 ETA 1600. The task was as per instructions on the subject dated 23rd July 2015. As per the weight & load data sheet there were 8 passengers with 20 Kgs. of baggage in the aft cabin compartment. The actual take-off weight shown was 5668.85 Kgs as against the maximum take-off weight of 5669.9 Kgs. Fuel uplifted was 1085 Kgs. The aircraft was taken out of hangar of the Operator at 0655 hrs on 22.12.2015 and parked outside the hangar for operating the subject flight. At around 0745 hrs, the passengers reached the aircraft who were mainly technical personnel supposed to carry out scheduled maintenance of Mi-17 helicopter of the Operator at Ranchi. They were carrying their personnel baggage along with tools and equipment required for the maintenance. At around 0915 hrs the flight crew contacted ATC Delhi and requested for clearance to operate the flight to Ranchi. The aircraft was cleared to Ranchi via R460 and FL210. Runway in use was given as 28. At 0918 hrs the doors were closed and the flight crew had started carrying out the check list. After the ATC issued taxi clearance, the aircraft had stopped for some time after commencing taxiing. The pilot informed the ATC that they will take 10 minutes delay for further taxi due to some administrative reasons. The taxi clearance was accordingly cancelled. After a halt of about 6 to 7 minutes, the pilot again requested the ATC for taxi clearance and the same was approved by the ATC. Thereafter, the aircraft was given take-off clearance from runway 28. The weather at the time of take-off was: Visibility 800 meters with Winds at 100°/03 knots. Shortly after take-off and attaining a height of approximately 400 feet AGL, the aircraft progressively turned left with simultaneous loss of height. It had taken a turn of approximately 180o and impacted some trees before hitting the outside perimeter road of the airport in a left bank attitude. Thereafter, it impacted 'head on' with the outside boundary wall of the airport. After breaking the outside boundary wall, the wings impacted two trees and the aircraft hit the holding tank of the water treatment plant. The tail portion and part of the fuselage overturned and went into the water tank. There was post impact fire and the portion of the aircraft outside the water tank was destroyed by fire. All passengers and crew received fatal injuries due impact and fire. The ELT was operated at 0410 hours UTC (0940 hours IST). The fire fighting team reached the site and extinguished the fire. The bodies were then recovered from the accident site. 08 bodies were recovered from the holding tank of the water treatment plant and bodies of both pilots were recovered from the heavily burnt portion of the cockpit lying adjacent (outside) to the wall of the holding tank of the water treatment tank.
Probable cause:
The accident was caused due to engagement of the autopilot without selecting the heading mode by the flight crew just after liftoff (before attaining sufficient height) in poor foggy conditions and not taking corrective action to control the progressive increase in left bank; thereby, allowing the aircraft to traverse 180° turn causing the aircraft to lose height in a steep left bank attitude followed by impact with the terrain.
Final Report: