Crash of a Piper PA-46-310P Malibu in Hilltop Lakes: 4 killed

Date & Time: Sep 20, 2020 at 1050 LT
Operator:
Registration:
N236KM
Flight Type:
Survivors:
No
Schedule:
Horseshoe Bay – Natchitoches
MSN:
46-8508014
YOM:
1985
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
1107
Circumstances:
While in cruise flight at 19,000 ft mean sea level (msl), the pilot declared an emergency to air traffic control and stated that the airplane had lost engine power and that he needed to divert. The pilot elected to divert to an airport that was about 5 miles south of his position. Archived automatic dependent surveillance-broadcast data and commercially available flight track data showed that a descent was initiated from 19,000 ft and the airplane proceeded directly to, and circled around, the airport one time while descending. The last data point showed the airplane at 1,250 ft msl (about 750 ft above ground level) and about 1 mile north of the approach end of the runway. From the cruise altitude of 19,000ft until the last data point, about 12 minutes and 45 seconds had elapsed, which equated to an average descent rate of about 1,392ft per minute. Witnesses located about 1/4 mile south of the end of the runway on a miniature golf course noticed the propeller on the airplane was not turning. They stated that they saw the airplane in a “really hard” left bank; the nose of the airplane dropped, and it impacted the ground in a near vertical attitude. The airplane came to rest along a road about 200 ft south of the airport property. The airplane impacted the terrain in a nose low, near vertical attitude and sustained substantial damage to fuselage and both wings. It is likely that, based on the location of the runway, relative to the miniature golf course, the pilot initiated the left bank to avoid bystanders on the ground and inadvertently exceeded the wing’s critical angle of attack, which resulted in an aerodynamic stall. The airplane was equipped with an engine trend monitor (ETM), which captured various events concerning the accident flight, including engine start, operating limit exceedances, and power checks. The ETM captured a power check while the airplane was at 19,100 ft. About 3 minutes 32 seconds later, an engine off event was recorded. The ETM further captured a logon message, which was consistent with the power being cycled, at an altitude of 3,542 ft, 9 minutes, 52 seconds later. The ETM did not record any start attempts between the logged engine off event and when power was lost to the unit. A postaccident examination of the airframe, engine, and accessories did not reveal any mechanical malfunctions or anomalies that would have precluded normal operation. Although it cannot be determined whether a restart attempt would have been successful, the data were consistent with a restart not being attempted. Both the engine failure and power off landing checklists contained instructions for the pilot to establish the airspeed at 90 knots; however, when the winds aloft were applied to the reported groundspeeds, it was evident this did not occur. Furthermore, the power off landing checklist instructed the pilot to be about 1,500 ft above the airport on the downwind leg; however, data indicate that the airplane was about 5,000 ft above the airport on the downwind leg. The rapid descent from 5,000 ft on the downwind leg to about 750 ft above ground level on the final leg resulted in an unstabilized approach.
Probable cause:
The loss of engine power for reasons that could not be determined and the pilot’s failure to maintain control of the airplane which resulted in an aerodynamic stall and spin. Contributing to the accident was the pilot’s failure to establish and maintain a proper glidepath.
Final Report:

Crash of a Pilatus PC-6/B2-H4 Turbo Porter in Livrasco: 2 killed

Date & Time: Sep 20, 2020 at 0949 LT
Operator:
Registration:
T7-SKY
Survivors:
Yes
Schedule:
Cremona - Cremona
MSN:
902
YOM:
1993
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
4400
Captain / Total hours on type:
2500.00
Aircraft flight hours:
4920
Circumstances:
The single engine airplane departed Cremona-Migliaro Airport in the morning on a local skydiving flight, carrying eight skydivers and one pilot. This was the second sortie of the day. Once the altitude of 4,000 metres was reached, all eight skydivers successfully jumped out and the pilot started the descent to return to the airport. While descending to runway 11, the airplane collided with the eighth skydivers that hit the left wing and the vertical stabilizer. A large section of the left wing separated, causing the airplane to enter an uncontrolled descent and to crash in a cornfield located in Livrasco, about two km north of the airport. The pilot and the skydiver were killed. The airplane was totally destroyed.
Probable cause:
The cause of the accident was an in-flight collision between the Pilatus PC-6 descending and a free-falling track-suit parachutist. This collision resulted in a loss of control of the aircraft in flight and the destruction of the left wing of the aircraft, which fell to the ground uncontrolled.
The following factors contributed to the accident:
- Inadequate coordination between pilot and parachutist in relation to their respective descent and drift paths,
- The meteorological conditions at the time of the parachutist's exit from the aircraft, which took place in cloud and in the absence of visual contact with the ground, in a situation, therefore, incompatible with VFR flight rules and ENAC regulations for parachuting,
- The absence of codified procedures at the Italian level, integrating the procedures for jumps with those of aircraft operators used for parachute jumps, including deconfliction between descending aircraft and parachutists performing drift or wingsuit jumps.
The inadequate coordination between the pilot and parachutist in relation to their respective descent and drift paths could also be attributable to the absence of a responsible person to ensure that the above mentioned coordination was in place. In addition to the above mentioned criticalities, the ANSV investigation activity revealed, also in the present case, a general lack of rules and controls regarding parachuting activities carried out outside of training activities, which reasonably contributed to the occurrence of the investigated aircraft accidents.
Final Report:

Crash of a North American TB-25N Mitchell in Stockton

Date & Time: Sep 19, 2020 at 1925 LT
Registration:
N7946C
Flight Type:
Survivors:
Yes
Schedule:
Vacaville - Stockton
MSN:
108-33263
YOM:
1944
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5100
Captain / Total hours on type:
296.00
Aircraft flight hours:
8099
Circumstances:
While the airplane was in cruise flight and being flown by the copilot, the left engine fuel pressure fluctuated, which was followed by a brief loss of engine power. Concerned that the airplane might have a failed engine-driven fuel pump, the pilot turned the boost pumps to high and asked the passenger (the airplane’s mechanic) to open the fuel cross-feed valve. As the airplane approached its intended destination, both fuel pressure needles began to fluctuate. The pilot assumed that fuel starvation to the engines was occurring and decided to make an off-airport landing to a field behind their airplane’s position due to residential areas located between the airplane’s location and the airport. The pilot stated that he took control of the airplane from the copilot and initiated a right turn toward the field, and that, shortly afterward, both engines lost total power. During the landing roll, the pilot observed a ditch in front of the airplane and was able to get the airplane airborne briefly to avoid the first ditch; however, he was not able to avoid a second, larger ditch. Subsequently, the airplane struck the second ditch, became airborne, and impacted the ground, which resulted in substantial damage to the fuselage. Recovery company personnel reported that, during recovery of the wreckage, about 1 gallon of fuel was removed from the two forward and the two aft wing fuel tanks. Postaccident examination of the airplane revealed no evidence of any pre-existing anomalies that would have precluded normal operation of either engine except that all four main fuel tank fuel gauges displayed erroneous indications after each tank was filled with water. No leaks were observed throughout the fuel system. The airplane was last refueled on the day before the accident with 497.7 gallons. When the airplane was last refueled, the fuel tanks were reportedly filled to about 3 inches below the fuel filler neck. The investigation could not determine, based on the available evidence for this accident, how much of the airplane’s fuel load (maximum capacity was 670 gallons) the airplane had onboard after it was refueled. Additionally, the pilot reported that he commonly used a fuel burn rate of 150 gallons per hour for flight planning purposes; that figure included takeoff fuel burn. Recorded automatic dependent surveillance broadcast data showed that the airplane had flown for 4 hours 1 minute since refueling and included six takeoffs and five landings (but did not include taxi times). As part of the investigation, the pilot estimated that 485.9 gallons of fuel had been used since the last refueling. However, on the basis of the pilot’s initial planned fuel load and recorded flight times, the airplane would have used about 600 gallons of fuel. The pilot later submitted an estimated fuel burn for the flights since refueling of 485.9 gallons. The flight manual did not have fuel burn references for the exact power settings and altitudes flown; thus, the hourly fuel burn could not be determined. The pilot, copilot, and passenger did not visually verify the fuel levels in all four main fuel tanks before the accident flight. The pilot also underestimated the amount of fuel that would be used for the planned flights. As a result, fuel exhaustion occurred, which led to a total loss of engine power.
Probable cause:
A total loss of engine power due to fuel exhaustion. Contributing to the accident was the erroneous fuel gauge indications and inadequate preflight planning and inspection.
Final Report:

Crash of a Fokker 50 in Mogadishu

Date & Time: Sep 19, 2020 at 0755 LT
Type of aircraft:
Operator:
Registration:
5Y-MHT
Flight Type:
Survivors:
Yes
Schedule:
Mogadishu - Beledweyne
MSN:
20171
YOM:
1989
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft departed Mogadishu-Aden Abdulle Airport on a cargo flight to Beledweyne, carrying four crew members and various goods on behalf of the AMISOM, the African Union Mission in Somalia. After takeoff, the crew informed ATC about hydraulic problems and was cleared to return. After touchdown on runway 05, the aircraft went out of control, veered off runway to the right and collided with a concrete wall. Two crew members were slightly injured while both pilots were seriously injured after the cockpit was severely damaged on impact.

Crash of a Piper PA-46-350P Malibu Mirage in Jacksonville

Date & Time: Sep 16, 2020 at 1340 LT
Operator:
Registration:
N972DD
Flight Type:
Survivors:
Yes
Schedule:
Jacksonville - Jacksonville
MSN:
46-36637
YOM:
2014
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total hours on type:
1141.00
Copilot / Total flying hours:
534
Copilot / Total hours on type:
9
Aircraft flight hours:
629
Circumstances:
The instructor pilot reported that while practicing an engine-out landing in the traffic pattern, the pilot-rated student overshot the turn from base leg to final rolling out to the right of the runway centerline. The student pilot attempted to turn back toward the runway and then saw that the airplane’s airspeed was rapidly decreasing. The instructor reported that when he realized the severity of the situation it was too late to do anything. The student attempted to add power for a go-around but was unable to recover. The airplane stalled about 10 ft above the ground, impacted the ground right of the runway, and skidded onto the runway where it came to rest. Both wings and the forward fuselage were substantially damaged. Both pilots stated there were no preaccident mechanical failures or malfunctions with the airplane that would have precluded normal operation.
Probable cause:
The student pilot’s failure to maintain control of the airplane during the landing approach and the exceedance of the airplane’s critical angle of attack at low altitude resulting in an aerodynamic stall. Contributing was the instructor pilot’s failure to adequately monitor the student pilot’s actions during the approach.
Final Report:

Crash of a Cessna 208B Grand Caravan in Maji Moto

Date & Time: Sep 11, 2020
Type of aircraft:
Operator:
Registration:
5Y-CDH
Flight Type:
Survivors:
Yes
MSN:
208B-0608
YOM:
1997
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed in unknown circumstances in Maji Moto, Rift Valley. All three occupants escaped with various injuries and the aircraft was destroyed.

Crash of a Gulfstream G200 in Belo Horizonte

Date & Time: Sep 7, 2020 at 1826 LT
Type of aircraft:
Operator:
Registration:
PR-AUR
Flight Type:
Survivors:
Yes
Schedule:
Belo Horizonte - Belo Horizonte
MSN:
140
YOM:
2006
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was completing a local training flight at Belo Horizonte-Pampulha Airport, consisting of touch-and-go maneuvers. After landing on runway 13, the pilot-in-command decided to abort the takeoff. Unable to stop within the remaining distance, the aircraft overran, lost its landing gear and came to rest near a concrete block. All three occupants evacuated, among them the captain was slightly injured.

Crash of a Dassault Falcon 200 in Palenque

Date & Time: Aug 29, 2020 at 2100 LT
Type of aircraft:
Operator:
Registration:
XB-OAP
Flight Type:
Survivors:
Yes
MSN:
504
YOM:
1986
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
In unknown circumstances, the crew made a belly landing near Palenque Airport. By night, the aircraft crash landed in an open field and came to rest. The occupant(s) was/were not found but law enforcement officials found 3 tons of cocaine on board. The aircraft seems to be written off.

Crash of a Cessna 401A in Arnsberg

Date & Time: Aug 28, 2020 at 1602 LT
Type of aircraft:
Operator:
Registration:
N401JP
Flight Type:
Survivors:
Yes
Schedule:
Marl – Arnsberg
MSN:
401A-0046
YOM:
1969
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6300
Captain / Total hours on type:
500.00
Aircraft flight hours:
4568
Aircraft flight cycles:
5945
Circumstances:
At 1541 hrs, the airplane took off from Marl-Lohmühle Airfield with the pilot and 2 passengers on board to a VFR flight to Arnsberg-Menden Airfield which is located approximately 30 NM to the south-east. One of the passengers was seated in the right-hand seat next to the pilot and the other in the passenger seat behind the pilot. The radar recording of the air navigation service provider showed that the airplane climbed up to 2,200 ft AMSL. Ten minutes after take-off, the pilot established radio contact with Dortmund Tower with the request to cross Dortmund Airport control zone via the reporting point WHISKEY towards reporting point ECHO on his way to Arnsberg. At 1552:14 hrs, the tower controller answered: “[…] melden Sie WHISKEY und dann erwarten Sie Durchflug nach Arnsberg oder ECHO, wie Sie möchten, QNH eins null null eins (report WHISKEY and then expect cross flight to Arnsberg or ECHO, as you like, QNH one zero zero one)“. The pilot confirmed QNH and approach point. At 1555:22 hrs, the pilot reported having reached reporting point WHISKEY at 2,200 ft AMSL. The controller approved the flight through the control zone towards the south. The GPS and radar data showed that at 1556 hrs, the airplane turned tight towards 120° to a direct heading to Arnsberg. At 1559 hrs, as the airplane had left the control zone the controller issued the clearance to leave Tower frequency. At 1600 hrs, about 2.5 NM west of the destination aerodrome, the airplane turned left towards the east. About one minute later the airplane intersected the extended runway centre line of runway 23 at a distance of 0.7 NM from the threshold with an eastern heading. At the time, ground speed was approximately 150 kt. At 1601:39 hrs, the airplane turned left towards the final approach of runway 23. At 1602 hrs, about 1 NM from the threshold of runway 23 at about 1,500 ft AMSL, the airplane reached the extended runway centre line. The Flugleiter (A person required by German regulation at uncontrolled aerodromes to provide aerodrome information service to pilots.) stated that during final approach flaps and landing gear of the airplane had been extended. The approach looked normal. For a short time he had no longer observed the airplane because he had made some entries in the computer. His colleague had then addressed him and drew his attention to the speed of the airplane. The Flugleiter saw that the airplane had an upward large pitch angle, then plunged and disappeared from his sight. The airplane impacted the ground and the 3 occupants suffered severe injuries. The Flugleiter stated he had tried in vain to contact the pilot twice and then raised the alarm. His colleague and other first aiders had driven to the accident site immediately.
Probable cause:
The accident was due to:
• The pilot did not correct the approach by increasing engine power or did not abort the approach.
• The pilot did not monitor the airspeed during the final approach and steered the airplane into an uncontrolled flight attitude during the flare.
To the accident contributed that:
• The approach was not stabilized and not aborted.
• The pilot did not pay attention to the PAPI indication and did not perceive the stall warning.
• The large number of continuously changing approach parameters most likely exceeded the limits of the pilot’s capabilities and subsequently, the airplane was no longer controlled in a goal-oriented manner.
• The runway markings did not comply with the required standards.
Final Report:

Crash of a Rockwell 690B Turbo Commander in Ahuas

Date & Time: Aug 23, 2020
Operator:
Registration:
XB-DRA
Flight Type:
Survivors:
Yes
MSN:
11423
YOM:
1977
Country:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft was engagted in an illegal contraband flight when it crash landed in an open field located near Ahuas. No one was found on site and the aircraft was damaged beyond repair. A load of cocaine was found on board.