Crash of an Antonov AN-24B at Talil AFB

Date & Time: Mar 23, 2006
Type of aircraft:
Operator:
Registration:
ER-AZZ
Flight Type:
Survivors:
Yes
Schedule:
Baghdad - Talil AFB
MSN:
7 99 011 10
YOM:
1967
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On approach to Talil AFB, the crew was forced to shut down one of the engines due to the failure of the engine control system. As the nose gear could not be lowered, the crew initiated a go-around. As the main gears could not be retracted, the captain decided to attempt an emergency landing. The aircraft crash landed in an unpaved area of the airfield and came to rest. All occupants escaped uninjured and the aircraft was damaged beyond repair.

Crash of a Beechcraft C99 Airliner in Butte: 2 killed

Date & Time: Mar 18, 2006 at 1455 LT
Type of aircraft:
Operator:
Registration:
N54RP
Flight Type:
Survivors:
No
Schedule:
Helena - Butte
MSN:
U-218
YOM:
1983
Flight number:
AMF2591
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
5219
Captain / Total hours on type:
2616.00
Aircraft flight hours:
22169
Aircraft flight cycles:
35539
Circumstances:
The cargo flight collided with mountainous terrain in controlled flight while executing an instrument approach procedure. Two pilots were aboard; the company's training and check captain/pilot-in-command in the right seat, and a newly hired commercial pilot in left seat, who was in training for captain The flight had been cleared for the VOR or GPS-B approach via the 7 DME arc. According to the approach plate, the transition to the approach is via a DME arc at 9,000 feet with no procedure turn. The flight is to track inbound on the 127 degree radial, descending down to, but no lower than, 7,700 feet to the initial approach fix (IAF). After crossing the IAF, the flight is to turn to 097 degrees for 10 nautical miles and descend to 6,900 feet. The remainder of the 1.5 nautical miles to the runway is to be flown under visual conditions. Documentation of the accident site indicated that the aircraft collided with trees and subsequently the mountainous terrain on a heading of approximately 127 degrees and about 6,900 feet mean sea level. The initial impact point was located approximately nine nautical miles on a magnetic bearing of 130 degrees from the IAF. Documentation of the horizontal situation indicator (HSI) on the left side instrument panel indicated that the course arrow was positioned to approximately 127 degrees, the inbound heading to the IAF. The copilot (right side) course arrow was positioned to 115 degrees. The location of the wreckage and the 127 degree heading on the HSI indicate that the pilots failed to follow the approach procedure and turn to a heading of 097 degrees after crossing the IAF. Instrument meteorological conditions were reported in the area consisting of icing conditions, heavy snow fall, with poor visibility and mountain obscuration. No pre-impact mechanical malfunctions or failures were identified.
Probable cause:
The second pilot's failure to follow the published instrument approach procedure and the captain/PIC's inadequate supervision. Snow and mountain obscuration were factors.
Final Report:

Crash of an Avro 748-286-2A-LFD in Old Fangak

Date & Time: Mar 17, 2006 at 0930 LT
Type of aircraft:
Registration:
5Y-TCA
Flight Type:
Survivors:
Yes
MSN:
1740
YOM:
1976
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was completing a positioning flight from Kenya to Old Fangak Airport. After landing, the twin engine aircraft was unable to stop within the remaining distance. It overran, lost its right main gear and came to rest. Both pilots escaped uninjured while the aircraft was damaged beyond repair.

Crash of an ATR72-212A in Bangalore

Date & Time: Mar 11, 2006 at 1017 LT
Type of aircraft:
Operator:
Registration:
VT-DKC
Survivors:
Yes
Schedule:
Coimbatore – Bangalore
MSN:
721
YOM:
2005
Flight number:
DN108
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
40
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The twin engine aircraft landed hard on runway 27 at Bangalore-Hindustan Airport. After touchdown, it veered off runway and came to rest. All 44 occupants escaped uninjured while the aircraft was damaged beyond repair. Brand new, it was delivered four months ago.

Crash of a Lockheed L-1329-23E JetStar 8 in Dallas

Date & Time: Mar 10, 2006 at 1445 LT
Type of aircraft:
Registration:
N116DD
Flight Type:
Survivors:
Yes
Schedule:
Houston - Dallas
MSN:
5155
YOM:
1972
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
After landing on runway 13R, directional control was lost and the aircraft veered off runway to the right. While contacting soft ground, the nose gear collapsed and the aircraft came to rest. All three occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
No investigation has been conducted by the NTSB.

Crash of a Cessna 414A Chancellor in Kahului: 3 killed

Date & Time: Mar 8, 2006 at 1913 LT
Type of aircraft:
Operator:
Registration:
N5601C
Flight Type:
Survivors:
No
Schedule:
Honolulu - Kahului
MSN:
414A-0113
YOM:
1978
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
3141
Aircraft flight hours:
8734
Circumstances:
The twin-engine medical transport airplane was on a positioning flight when the pilot reported a loss of power affecting one engine before impacting terrain 0.6 miles west of the approach end of the runway. The airplane was at 2,600 feet and in a shallow descent approximately 8 miles northwest of the airport when the pilot checked in with the tower and requested landing. Three and a half minutes later, the pilot reported that he had lost an engine and was in a righthand turn. Radar data indicated that the airplane was 2 miles southwest of the airport at 1,200 feet msl. The radar track continued to depict the airplane in a descent and in a right-hand turn, approximately 1.9 miles west of the approach end of the runway. The altitude fluctuated between 400 and 600 feet, the track turned right again, and stabilized on an approximate 100- degree magnetic heading, which put the airplane on a left base for the runway. The track entered a third right-hand turn at 500 feet. The pilot's last transmission indicated that one engine was not producing power. The last radar return was 6 seconds later at 200 feet, in the direct vicinity of where the wreckage was located. Using the radar track data, the average ground speed calculations showed a steady decrease from 134 knots at the time of the pilot's initial report of a problem, to 76 knots immediately before the airplane impacted terrain. The documented minimum controllable airspeed (VMC) for this airplane is 68 knots. The zero bank angle stall speed varied from 78 knots at a cruise configuration to 70 knots with the gear and flaps down. A sound spectrum study using recorded air traffic control communications concluded that one engine was operating at 2,630 rpm, and one engine was operating at 1,320 rpm. Propeller damage was consistent with the right engine operating at much higher power than the left engine at the time of impact, and both propellers were at or near the low pitch stops (not feathered). Examination and teardown of both engines did not reveal any evidence of mechanical malfunction. Investigators found that the landing gear was down and the flaps were fully deployed at impact. In this configuration, performance calculations showed that level flight was not possible with one engine inoperative, and that once the airspeed had decreased below minimum controllable airspeed (VMC), the airplane could stall, roll in the direction of the inoperative engine, and enter an uncontrolled descent. The pilot had been trained and had demonstrated a satisfactory ability to operate the airplane in slow flight and single engine landings. However, flight at minimum controllable airspeed with one engine inoperative was not practiced during training. The operator's training manual stated that during single engine training an objective was to ensure the pilot reduced drag; however, there was no procedure to accomplish this objective, and the ground training syllabus did not specifically address engine out airplane configuration performance as a dedicated topic of instruction. The operator's emergency procedures checklist and manufacturer's information manual clearly addressed the performance penalties of configuring the airplane with an inoperative engine, propeller unfeathered, the landing gear down, and/or the flaps deployed. The engine failure during flight procedure checklist and the engine inoperative go-around checklist, if followed, configure the airplane for level single engine flight by feathering the propeller, raising the flaps, and retracting the landing gear.
Probable cause:
The failure of the pilot to execute the published emergency procedures pertaining to configuring the airplane for single engine flight, which would have allowed him to maintain minimum controllable airspeed (VMC) and level flight. The pilot's failure to maintain minimum controllable airspeed (VMC) led to a stall and subsequent VMC roll at a low altitude. Contributing to the accident was the operator's inadequate pilot training in the single engine flight regime, and the loss of power from the left engine for undetermined reasons.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in Powell River: 1 killed

Date & Time: Mar 8, 2006 at 1639 LT
Operator:
Registration:
C-GNAY
Flight Type:
Survivors:
Yes
Schedule:
Vancouver – Powell River
MSN:
31-8052095
YOM:
1980
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1200
Copilot / Total flying hours:
500
Circumstances:
The aircraft departed from its home base at Vancouver, British Columbia, with two crew members on board. The aircraft was being repositioned to Powell River (a 30-minute flight) to commence a freight collection route. On arriving at Powell River, the crew joined the circuit straight-in to a right downwind for a visual approach to Runway 09. A weather system was passing through the area at the same time and the actual local winds were shifting from light southwesterly to gusty conditions (11 to 37 knots) from the northwest. The aircraft was lower and faster than normal during final approach, and it was not aligned with the runway. The crew completed an overshoot and set up for a second approach to the same runway. On the second approach, at about 1639 Pacific standard time, the aircraft touched down at least halfway down the wet runway and began to hydroplane. At some point after the touchdown, engine power was added in an unsuccessful attempt to abort the landing and carry out an overshoot. The aircraft overran the end of the runway and crashed into an unprepared area within the airport property. The pilot-in-command suffered serious injuries and the first officer was fatally injured. A local resident called 911 and reported the accident shortly after it occurred. The pilot-in-command was attended by paramedics and eventually removed from the wreckage with the assistance of local firefighters. The aircraft was destroyed, but there was no fire. The ELT (emergency locator transmitter) was automatically activated, but the signal was weak and was not detected by the search and rescue satellite.
Probable cause:
Findings as to Causes and Contributing Factors:
1. The downwind condition on approach contributed to the aircraft landing long and with a high ground speed. This, in combination with hydroplaning, prevented the crew from stopping the aircraft in the runway length remaining.
2. When the decision to abort the landing was made, there was insufficient distance remaining for the aircraft to accelerate to a sufficient airspeed to lift off.
3. The overrun area for Runway 09 complied with regulatory standards, but the obstacles and terrain contour beyond the overrun area contributed to the fatality, the severity of injuries, and damage to the aircraft.
Finding as to Risk:
1. Alert Service Bulletin A25-1124A (dated 01 June 2000), which recommended replacing the inertia reel aluminum shaft with a steel shaft, was not completed, thus resulting in the risk of failure increasing over time.
Other Findings:
1. The weather station at the Powell River Airport does not have any air–ground communication capability with which to pass the flight crew timely wind updates.
2. The decision to make a second approach was consistent with normal industry practice, in that the crew could continue with the intent to land while maintaining the option to break off the approach if they assessed that the conditions were becoming unsafe.
Final Report:

Crash of a Cessna 421C Golden Eagle III in Pamplona: 2 killed

Date & Time: Mar 7, 2006 at 1648 LT
Operator:
Registration:
EC-JAX
Survivors:
Yes
Site:
Schedule:
Madrid - Pamplona
MSN:
421C-0337
YOM:
1977
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1771
Captain / Total hours on type:
520.00
Copilot / Total flying hours:
7000
Copilot / Total hours on type:
460
Aircraft flight hours:
3518
Circumstances:
The twin engine aircraft departed Madrid-Torrejón AFB on a charter flight to Pamplona with 4 businessmen and a crew of two on board. While descending to Pamplona-Noain Airport, the crew encountered marginal weather conditions. Unable to establish a visual contact with runway 15, the crew initiated a go-around procedure. Few minutes later, while flying at an insufficient altitude, the aircraft impacted ground and crashed in a hilly terrain located in the Sierra de Tajonar, near the village of Labiano. The copilot and a passenger were killed while all other occupants were seriously injured. The aircraft was totally destroyed by impact forces and a post crash fire.
Probable cause:
The crew did not establish a visual contact with the runway and initiated a go-around procedure during which approximations were noted in the flight techniques adopted by the pilots who continued the flight in unstable conditions. As a result, the aircraft was 16 ° off the prescribed path and was flying at an insufficient altitude.
The following contributing factors were identified:
- The wind did not correspond to the component reported in the bulletin published for the destination airport, which affected the aircraft flight path,
- The total weight of the airplane was higher than the allowable limit and the CofG was out of permissible limits, reducing the aircraft's performances and its maneuverability,
- The pilots did not have sufficient experience in instrument flight conditions,
- The lack of clear procedures within the operator,
- The lack of supervision from the Spanish Civil Aviation Authority regarding the activities of the operator.
Final Report:

Crash of a McDonnell Douglas MD-82 in Surabaya

Date & Time: Mar 4, 2006 at 1625 LT
Type of aircraft:
Operator:
Registration:
PK-LMW
Survivors:
Yes
Schedule:
Denpasar – Surabaya
MSN:
49443/1291
YOM:
1986
Flight number:
JT8987
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
138
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Prior to departure from Bali to Surabaya, the crew was informed that the left engine's thrust reverser system was out of service. Following an uneventful flight, the crew completed a normal approach to runway 10 then landed according to procedures. After touchdown, the crew activated the thrust reverser when the airplane deviated to the right. The crew elected to counteract but the aircraft veered off runway, lost its undercarriage and came to rest in a grassy area. All 144 occupants evacuated safely while the aircraft was damaged beyond repair.

Crash of a Cessna 501 Citation I/SP near Sulaymānīyah: 6 killed

Date & Time: Feb 16, 2006 at 1115 LT
Type of aircraft:
Operator:
Registration:
D-IMRX
Survivors:
No
Site:
Schedule:
Munich - Budapest - Baku - Sulaymānīyah
MSN:
501-0688
YOM:
1985
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
The aircraft was performing a business flight from Baku to Sulaymānīyah with 5 passengers and one pilot on board. It departed Munich to Baku via Budapest on February 14. As it descended through the altitude of 8,000 feet, the aircraft disappeared from radar screens and crashed near Buschin, few dozen km from Sulaymānīyah Airport. The wreckage was found on February 19 in a snow covered and hilly terrain. All 6 occupants were killed, among them 4 German businessmen, one pilot and one translator. The aircraft was owned by the German Company Hasit Trockenmörtel, specialised in building reconstruction.