Crash of a Cessna 340 in Kingman: 1 killed

Date & Time:
Type of aircraft:
Operator:
Registration:
N2340C
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Kingman - Kingman
MSN:
340-0672
YOM:
1970
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1649
Captain / Total hours on type:
1.00
Circumstances:
The pilot, sole on board, departed Kingman-Clyde Cessna Field on a local test flight on this first Cessna 340 prototype. While flying in the vicinity of the airfield, he lost control of the airplane that crashed in an open field. The aircraft was destroyed and the pilot was killed.
Probable cause:
Uncontrolled descent caused by the failure of the elevator tab control system. The following factors were reported:
- Elevator tab control system improperly installed,
- Improper maintenance,
- Inadequate preflight preparation,
- Separation in flight,
- Bolt improperly secured in elevator trim push-pull rod came out and caused the loss of the horizontal stab assembly.
Final Report:

Crash of a Boeing B-52D-60-BO Stratofortress at Ellsworth AFB

Date & Time:
Type of aircraft:
Operator:
Registration:
55-0089
Flight Type:
Survivors:
Yes
Schedule:
Ellsworth - Ellsworth
MSN:
17205
YOM:
1955
Crew on board:
9
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The B52 of the 28th Bomb Wing at Ellsworth AFB, South Dakota, crashed and was destroyed after a landing accident. It caught fire and skidded into a brick storage building containing six 25,000 gallon tanks (150,000 total) of jet fuel. The firemen did a fantastic job in saving the crew member (the navigator) who was trapped inside the nose section that had broken off for almost an hour before being freed. The fire truck rammed the gun turret, breaking it off and freeing the tail gunner. Crew:
Cpt Wesley G. Swann, pilot,
Cpt Gary C. Christensen, copilot,
Maj Ralph P. Smiley, radar navigator,
Cpt Curtis L. Christy, navigator,
1Lt James L. Welch, electronic warfare officer,
S/Sgt Charles E. Adkins, gunner,
Maj Harry D. Meehan, instructor navigator,
Lt Col Paul R. Houser, 28th Bomb Wing Chief of Operations,
A1C Randall Hart, avionics maintenance.
Source: ASN

Crash of a Cessna 401A in Morrisville: 5 killed

Date & Time:
Type of aircraft:
Registration:
N401RA
Survivors:
No
Schedule:
Huntsville – Morrisville
MSN:
401A-0117
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
3247
Captain / Total hours on type:
297.00
Circumstances:
On final approach in poor weather conditions, the twin engine aircraft went out of control, struck trees and crashed in an open field located short of runway threshold. The airplane was destroyed and all five occupants were killed.
Probable cause:
Improper IFR operation on part of the pilot-in-command. The following factors were considered as contributing:
- Improper compensation for wind coditions,
- Sudden windshift,
- Erratic flight path after passing outer marker,
- ILS straight-in approach,
- Strong windshift reported at approximately 400 feet.
Final Report:

Crash of a Beechcraft 65-A80 Queen Air in Chicago: 1 killed

Date & Time:
Type of aircraft:
Operator:
Registration:
N242U
Flight Phase:
Survivors:
Yes
Schedule:
Chicago - New Castle
MSN:
LD-242
YOM:
1965
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
6115
Captain / Total hours on type:
263.00
Circumstances:
At liftoff, the twin engine encountered serious difficulties to gain height, stalled and crashed. A pilot was killed while the second crew member was seriously injured.
Probable cause:
Stall after takeoff due to an excessive accumulation of snow on wings and fuselage. The following contributing factors were reported:
- Inadequate preflight preparation,
- Airframe ice,
- Icing conditions,
- Snow,
- Slush on runway,
- The crew partially removed snow before taxi,
- 13 minutes time span between taxi out and takeoff in snow conditions.
Final Report:

Crash of a Beechcraft C-45H Expeditor in Binghamton: 3 killed

Date & Time:
Type of aircraft:
Operator:
Registration:
N497DM
Flight Phase:
Survivors:
Yes
Schedule:
Binghampton - Washington DC
MSN:
AF-690
YOM:
1954
Crew on board:
2
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
6630
Captain / Total hours on type:
106.00
Circumstances:
At liftoff from Binghamton-Broome County Airport, the twin engine airplane encountered serious difficulties to gain height. Suddenly, it stalled and crashed in flames in an open field located near the airport. A pilot and two passengers were killed while eight other occupants were seriously injured.
Probable cause:
The accident was caused by a poor flight preparation on part of the crew who decided to takeoff with a snow covered aircraft. The following factors were considered as contributing:
- Inadequate preflight preparation,
- Airframe ice,
- Icing conditions including sleet and freezing rain,
- Delayed action in aborting takeoff,
- Intentional wheels-up landing,
- Low ceiling,
- Snow,
- The crew attempted to takeoff with snow on wings,
- Aircraft not cleaned prior to takeoff.
Final Report:

Crash of a Cessna 402 in Newark: 4 killed

Date & Time:
Type of aircraft:
Operator:
Registration:
N3218Q
Survivors:
No
Schedule:
Sherbrooke - Newark
MSN:
402-0018
YOM:
1967
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
10461
Captain / Total hours on type:
83.00
Circumstances:
The pilot initiated the approach to Newark Airport in marginal weather conditions (heavy rain falls). On final, he failed to realize his altitude was insufficient when the airplane crashed onto a natural gas storage tank located in Elizabeth, few miles short of runway 04L threshold. The aircraft was totally destroyed and all four occupants were killed.
Probable cause:
Ground collision during initial approach caused by the combination of the following factors:
- The pilot-in-command failed to follow the approved procedures,
- Improper IFR operation on part of the pilot-in-command,
- Instruments misread or failed to read,
- Obstructions to vision,
- Rain,
- No second pilot on board,
- Descended below glide slope on an ILS approach to runway 04L.
Final Report:

Crash of a Stinson V-77 Reliant in Perris Valley: 1 killed

Date & Time:
Type of aircraft:
Operator:
Registration:
N69440
Flight Phase:
Survivors:
Yes
Schedule:
Perris Valley - Perris Valley
MSN:
77-107
YOM:
1943
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
800
Captain / Total hours on type:
252.00
Circumstances:
While completing a skydiving flight, the aircraft suffered an airframe failure. Control was lost and it crashed near the Perris Valley Airport. Five occupants were rescued while a passenger was killed.
Probable cause:
Probable cause(s):
- pilot in command - inadequate preflight preparation and/or planning,
- pilot in command - exercised poor judgment,
- pilot in command - failed to follow approved procedures, directives,etc.,
- personnel - maintenance, servicing, inspection: inadequate maintenance and inspection,
- airframe - wings: skin and attachments,
- miscellaneous acts,conditions - improperly loaded aircraft-weight-and/or c.g.
Factor(s):
- miscellaneous acts,conditions - overload failure.
Remarks- metal skin coverage top left wing loose, skin working, separation occurred. Pilot exceeded aircraft operations limits before occurrence.
Final Report:

Crash of a Convair CV-240-0 at Langley AFB

Date & Time:
Type of aircraft:
Registration:
N741J
Survivors:
Yes
Schedule:
Richmond - Linden
MSN:
146
YOM:
1949
Crew on board:
4
Crew fatalities:
Pax on board:
24
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
11000
Captain / Total hours on type:
1000.00
Circumstances:
En route from Richmond to Linden, NJ, the crew informed ATC about technical problems and that he was unable to lower the landing gear. ATC cleared the crew to divert to Langley AFB for an emergency landing. The airplane belly landed on a foamed runway and came to rest. All 28 occupants were evacuated safely while the aircraft was damaged beyond repair.
Probable cause:
Wheels-up landing caused by the malfunction of the landing gear mechanism. The following contributing factors were reported:
- Improper maintenance on part of the maintenant personnel,
- Failure of the landing gear mechanism,
- Material failure, corrosion,
- Suspected mechanical discrepancy,
- Numerous aircraft maintenance discrepancies,
- Uplock cable broken,
- Emergency system pressure too low.
Final Report:

Crash of a Beechcraft E18S in Kansas City: 1 killed

Date & Time:
Type of aircraft:
Operator:
Registration:
N5659D
Flight Type:
Survivors:
No
Schedule:
Little Rock – Kansas City
MSN:
BA-392
YOM:
1958
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2014
Captain / Total hours on type:
1133.00
Circumstances:
On final approach to Kansas City Airport, while completing a night mail flight, the pilot encountered engine problems. Control was lost and the airplane crashed few miles short of runway. The aircraft was destroyed and the pilot was killed.
Probable cause:
Uncontrolled collision with ground during initial approach caused by the combination of the following factors:
- Powerplant problems caused by vacuum pumps failure,
- The pilot-in-command failed to maintain flying speed,
- Airframe ice,
- Ice on windshield,
- Icing conditions including sleet and freezing rain,
- Weather conditions slightly worse than forecast,
- The pilot was aware of the icing conditions,
- The left vacuum pump failed at an undetermined time, limiting the de-icing capabilities.
Final Report:

Crash of a De Havilland DHC-6 Twin Otter 100 off Groton: 5 killed

Date & Time:
Operator:
Registration:
N124PM
Survivors:
No
Schedule:
Groton - New York
MSN:
41
YOM:
1967
Flight number:
PM203
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
6335
Captain / Total hours on type:
2180.00
Copilot / Total flying hours:
991
Copilot / Total hours on type:
669
Aircraft flight hours:
5817
Circumstances:
Pilgrim Flight 203 departed from Groton about 16:21, approximately 15 minutes behind schedule primarily because of ground delays encountered on previous flights which used the aircraft. Shortly after takeoff, Flight 203 reported on course and was instructed to contact the New York Center. Communications were established at 16:27 and the Center cleared the flight to Deer Park via its flight plan route to cross Saybrook at 4,000 feet, and then to climb and maintain 6,000 feet. At 16:33, the New York Center controller recleared the flight to Deer Park, to climb to 9,000 feet, and issued it holding instructions at Deer Park. About 2 minutes later, the controller advised that 7,000 feet was open for the flight, with the possibility of no holding, and he cleared it back to 7,000 feet. The flight reported at 7,000 immediately thereafter. About 16:36, the controller told Pilgrim 203 that if holding were necessary, its expected approach clearance time was 17.06. At 16:47 the crew contacted Kennedy Approach Control and they reported holding at Deer Park at 7,000 feet. About this time, the weather conditions at the Kennedy Airport deteriorated, and some flights which were then making instrument approaches to runway 13L began missing their approaches. Because of this, instrument approaches were changed to runway 22R, which had a better RVR. At 16:55, in connection with the runway change, Pilgrim 203 was recleared to hold in the Medford holding pattern. At 1709, Pilgrim 203 was given an expected approach clearance time of 17:46, which the flight acknowledged. At 17:39, the Kennedy approach controller cleared Pilgrim Flight 203 to descend to 6,000 feet. At 17:42, the crew of Pilgrim 203 radioed: "Pilgrim 203 request New Haven if we can get there, expedite." At 17:48, the flight was cleared to descend to 4,000 feet, and at 1750, it was cleared to Pond Point, which is the final approach fix from which VOR instrument approaches are made to New Haven-Tweed Airport. During the next minute, Pilgrim Flight 203 contacted Westchester Approach Control and asked for the latest Tweed weather. It was advised that the weather was: Scattered clouds 200 feet, estimated ceiling 500 feet broken, 700 feet overcast; visibility 2 miles, rain and fog; altimeter 29.46: wind variable 120° to 040° at 15 knots with gusts to 25 knots. At 17:53, the Westchester approach controller instructed Flight 203, "Upon reaching Pond Point hold southwest on the 205 radial, right turns, EAC 1815." Two minutes later the controller checked the position of the flight and, finding it was suitable for descent, cleared the flight to descend to 3,000 feet. At 17:57, the flight reported at Pond Point and asked if holding were still necessary. The controller advised that it was and repeated the holding instruction. At 18:12, the Westchester approach controller called Flight 203 and advised that, based on a report from the Cessna pilot who just landed, the airport was below minimums. He advised the weather was: Aircraft ceiling 200 feet broken, 500 feet, overcast: visibility 2 miles. He then asked the pilot his intentions. About 18:13, after asking for and being given the Bridgeport weather, which was lower than New Haven, the flight advised it would make the approach. The flight was cleared for the approach and instructed to contact New Haven Tower. This was done, and, at 1814, the flight advised New Haven it was inbound from Pond Point. The controller acknowledged, cleared the flight to land, and repeated the surface wind as variable 120° to 060°, 15 knots with gusts to 25 knots. Shortly before 18:17, Flight 203 reported to New Haven it had missed its approach. The tower controller immediately cleared the flight to the Madison VOR at 2,000 feet and instructed it to contact Westchester Approach Control. At 18:17, the flight asked for the Groton weather. The controller then gave the flight the Groton weather as: Measured ceiling 300 feet overcast; visibility 1-1/2 miles, moderate rain and fog; wind 100° at 15 knots, with gusts to 25 knots; altimeter 29.50. At 18:19, the crew told the controller, "Westchester, we’d like to ah get direct Groton right now." Within the same minute, the controller advised he was getting the clearance. The flight repeated that it had to get direct to Groton and the controller replied he had to coordinate (with New York Center). At 18:20, Flight 203 advised the Westchester controller, "Ah Westchester, 203 ah we got minimum fuel now, we gotta get to Groton." About 18:21, the controller cleared the flight to the Groton VOR via Victor Airway 126 and climb and maintain 3,000 feet. The flight reported it was level at 3,000 feet and asked to be cleared for an approach to Groton direct from Saybrook. The controller advised the flight to contact Quonset Approach Control. At 18:22, Flight 203 called Bradley FSS and advised it could not contact Quonset Approach Control, it was low on fuel, and wanted clearance for an instrument approach direct to Groton from Saybrook. On request, Quonset Approach Control gave this clearance to Bradley FSS and, at 18:23, the latter delivered it to the flight. About 18:24, the captain of Flight 203 called his company radio and said, "We’re coming home with this... pile of junk. We ain’t got any equipment working." He then asked to talk to the chief pilot. The captain asked initially for the Groton weather which was ceiling 300 feet, overcast; visibility 1-1/2 miles, rain and fog Later, he was advised that the ceiling had lowered to 200 feet. The captain said that Kennedy would not accept him because the aircraft transponder was not working. He said he was inbound to Groton on the 270 degree radial of the Groton VOR, flying about 100 feet above the water, and he could see the shoreline. Asked how much fuel he had remaining, the captain answered "none," and added, in essence, that fuel exhaustion could occur at anytime. Shortly thereafter, he radioed that he had lost one engine and was going to try to reach the shore. He then said he had just lost the other engine, could not make the shore, and was going into the water off Harkness Point. This was the last transmission from the aircraft.
Probable cause:
Fuel exhaustion resulting from inadequate flight preparation and erroneous in-flight decisions by the pilot-in-command.
Final Report: