Crash of a Beechcraft D18S in Sachse

Date & Time: Nov 19, 1976 at 2250 LT
Type of aircraft:
Registration:
N2050D
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Dallas - Huntington
MSN:
A-849
YOM:
1952
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1900
Captain / Total hours on type:
100.00
Circumstances:
While in normal cruise, the aft cargo door opened. The pilot shut down the right engine and attempted an emergency landing when the airplane struck power cables and crashed. The pilot was slightly injured while the aircraft was damaged beyond repair.
Probable cause:
Collision with wires/poles on final approach after inadequate preflight preparation. The following contributing factors were reported:
- Improperly secures,
- Improper action,
- Forced landing off airport on land,
- Door/panel open in flight,
- Lateral control problem,
- Aft cargo door opened in flight,
- Unmaintained altitude.
Final Report:

Crash of a Piper PA-31-310 Navajo in Tallahassee: 3 killed

Date & Time: Nov 17, 1976 at 2238 LT
Type of aircraft:
Operator:
Registration:
N50BB
Flight Phase:
Survivors:
No
Schedule:
Tallahassee - Fort Lauderdale
MSN:
31-323
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
3000
Circumstances:
After takeoff from Tallahassee Airport, while climbing by night under instruments, the twin engine airplane descended into ground and crashed. The aircraft was destroyed upon impact and all three occupants have been killed.
Probable cause:
Controlled collision with ground during climb to cruise after the pilot failed to maintain a positive rate of climb. The following contributing factors were reported:
- Misread or failed to read instruments,
- Low ceiling (200 feet),
- Fog.
Final Report:

Crash of a Rockwell Grand Commander 690A near Independence: 1 killed

Date & Time: Nov 17, 1976 at 1950 LT
Registration:
N57186
Flight Phase:
Survivors:
No
Schedule:
Kansas City - Oklahoma City
MSN:
690-11186
YOM:
1974
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
10000
Captain / Total hours on type:
980.00
Circumstances:
En route from Kansas City to Oklahoma City, the twin engine airplane was in normal cruise when control was lost. It entered a dive, suffered an overload failure then crashed in an open field. The pilot, sole on board, was killed.
Probable cause:
Airframe failure and fire or explosion in flight for undetermined reasons. The following findings were reported:
- Overload failure,
- Fire in wing,
- Separation in flight,
- Altitude varied between 14,500 and 15,300 feet during last 4 minutes of flight.
Final Report:

Crash of a Douglas DC-9-14 in Denver

Date & Time: Nov 16, 1976 at 1729 LT
Type of aircraft:
Operator:
Registration:
N9104
Flight Phase:
Survivors:
Yes
Schedule:
Salt Lake City - Denver - Houston
MSN:
47081/155
YOM:
1967
Flight number:
TI987
Crew on board:
5
Crew fatalities:
Pax on board:
81
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
15000
Captain / Total hours on type:
651.00
Copilot / Total flying hours:
8400
Copilot / Total hours on type:
4000
Aircraft flight hours:
24333
Circumstances:
On November 16, 1976, Texas International Flight 987, a McDonnell Douglas DC-9-14, N9104, operated as a scheduled passenger flight from Salt Lake City, Utah, to Houston, Texas, with an intermediate stop at Denver, Colorado. The flight was routine to Stapleton International Airport, Denver, Colorado. The flight left the gate at Stapleton International Airport with 81 passengers and 5 crew members aboard. When Flight 987 was cleared to taxi to runway 8R for takeoff, the weather was clear, the wind was from 130° at 7 kns, and the temperature was 40° F. At 1726:33, the tower cleared the flight to take the runway and to hold while two light: aircraft took off from a nearby intersection. At 1729:13, Flight 987 was cleared for takeoff, and at 1729: 15 the flight reported "rolling." The first officer was making the takeoff and, upon receipt of the clearance, he advanced the throttles to a position commanding 1.4 EPR and released the brakes. After the engines stabilized at 1.4 EPR, the first officer advanced the throttles to the takeoff thrust position. Upon reaching this position, he relinquished control of the throttles and placed his left hand on the control yoke. The captain guarded the throttles until rotation speed (VR) was reached. The pilots described the takeoff roll to rotation as "normal." The captain monitored the engine instruments and noted no abnormal readings. He said he called out 100 KIAS, 130 KIAS, V1, VR, V2; the cockpit voice recorder (CVR) readout corroborated his statement. The first officer stated that when the captain called VR, he checked his airspeed indicator before he moved his control column aft and saw 149 or 150 KIAS either at, or just before, he began to rotate the aircraft. He stated that he rotated the aircraft at a normal rate to a target pitch angle of 10° which he determined from his attitude indicator; he estimated that this took about 3 to 4 seconds. About halfway through the rotation--about a 5° pitch angle--the stall warning system's stickshaker activated. The first officer stated that once it began it was continuous. He said he continued the rotation to what he believed to be about 10° and the stickshaker continued to operate. He saw that although the airspeed was beyond 150 KIAS, the aircraft did not lift off. Since it had accelerated to a speed greater than V1, the first officer said that he tried to get it airborne. He could not recall how long he maintained the pitch angle, but he believed it was adequate to get the aircraft off the runway. When he concluded that the aircraft was not going to fly, he rejected the takeoff. The captain stated that rotation was normal and that as rotation was begun there were a couple of "clacks" from the stickshaker. As the rotation continued, the stickshaker began to operate continuously. He saw about 10° pitch angle on his attitude indicator and 152 KIAS on the airspeed indicator. All other instrument indications were normal. The stickshaker continued to operate and he believed that the aircraft would not lift off. At this point, with the airspeed well past V2, he decided to reject the takeoff. His actions to reject the takeoff were simultaneous with those of the first officer. When the first officer began to abort the takeoff, he reached over and, in what he described as one continuous motion, pulled the throttles to idle and applied full reverse thrust. Almost simultaneous with his initiation of the power reduction, he felt the captain's hand on top of his. He said that he had already started to apply forward pressure on the yoke to lower the nose. on his, he realized that the captain was assuming control of the aircraft and he removed his own hand from the thrust levers and placed it on the yoke. He described the lowering of the nosewheel to the runway as rapid, and once it was on the ground he pushed the yoke forward to hold the nosewheel there and applied brakes. The stickshaker had stopped, but neither pilot could recall exactly when. When he felt the captain's hand When the nose was lowered, full reverse thrust and maximum wheel braking were applied; however, the ground spoilers were not deployed. The captain estimated that there was 2,500 to 3,000 ft of runway remaining when the takeoff was rejected. He later noted that they were in the amber lighted area of the runway when the abort began. The first officer said that all he could see were the amber runway edge lights when the nose was lowered. The amber coded runway edge lights on 8R begin 2,000 feet from the eastern threshold of the runway. The captain stated that he steered the aircraft toward the right side of the runway to avoid the approach light stanchions for runway 26L. The aircraft left the runway, continued another 1,050 ft, traversed two drainage ditches, struck approach light stanchions, turned left, and stopped headed in a northerly direction. After the aircraft stopped, the captain ordered the first officer to proceed into the cabin and assist the flight attendants with the passenger evacuation. The captain then cleaned up the cockpit and carried out the emergency engine shutdown procedures. The engines were shut down, the fuel shutoff valves were closed, the engine fire handles were pulled, the fire extinguishing agent was discharged, and battery and ignition switches were turned off. All 86 occupants were evacuated safely and the aircraft was damaged beyond repair.
Probable cause:
A malfunction of the stall warning system, for undetermined reasons, which resulted in a false stall warning and an unsuccessful attempt to reject the take-off after the aircraft had accelerated beyond refusal and rotation speed. The decision to reject the take-off although not consistent with standard operating procedures and training, was reasonable in this instant case, based upon the unusual circumstances in which the crew found themselves, the minimal time available for decision, and the crew's judgment concerning a potentially catastrophic situation.
Final Report:

Crash of a Dassault Falcon 20C in Naples

Date & Time: Nov 12, 1976 at 0857 LT
Type of aircraft:
Operator:
Registration:
N27R
Flight Phase:
Survivors:
Yes
Schedule:
Naples - Winston Salem
MSN:
303
YOM:
1974
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3826
Captain / Total hours on type:
768.00
Circumstances:
Shortly after takeoff from Naples Airport, while initial climb, the airplane collided with a flock of seagulls that entered the engines. Both engines' compressors stalled, the airplane lost speed then stalled and crashed in an open field located past the runway end. The aircraft was damaged beyond repair and all 11 occupants were seriously injured.
Probable cause:
Bird strike during initial climb. The following contributing factors were reported:
- Inadequate preflight preparation,
- Failed to follow approved procedures,
- Failure to provide adequate directives, manual, equipment,
- Failure to notify of unsafe conditions / and or failure to mark obstruction,
- Bird ingestion,
- Forced landing off airport on land,
- Passengers not briefed,
- Emergency card instructions not correct for exits.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in Spring Lake: 2 killed

Date & Time: Nov 11, 1976 at 1636 LT
Registration:
N74941
Survivors:
Yes
Schedule:
Traverse City - Grand Haven
MSN:
31-7305086
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1798
Captain / Total hours on type:
221.00
Circumstances:
While approaching Grand Haven Airport, both engines stopped quite simultaneously. The pilot lost control of the airplane that stalled and crashed in Spring Lake, about three miles north of the airfield. Seven passengers were seriously injured while the pilot and an eighth passenger were killed.
Probable cause:
Engine failure on final approach due to mismanagement of fuel. The following contributing factors were reported:
- Fuel starvation,
- Failed to maintain flying speed,
- Failed to follow approved procedures,
- Improper emergency procedures,
- Attempted operation with known deficiencies in equipment,
- Fuel system: pumps,
- Right boost pump inoperative,
- Crossing feed used to start the right engine,
- Crossing feed found ON,
- Left inboard tank dry.
Final Report:

Crash of a Cessna 401B in Hot Springs

Date & Time: Oct 24, 1976 at 0805 LT
Type of aircraft:
Registration:
N2WP
Survivors:
Yes
Schedule:
Columbia - Hot Springs
MSN:
401B-0104
YOM:
1969
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6400
Captain / Total hours on type:
1000.00
Circumstances:
While descending to Hot Springs-Ingalls Field Airport, the crew encountered poor weather conditions with low ceiling, rain falls and fog. The twin engine airplane passed below the decision height when it struck trees and crashed. All six occupants were rescued and the aircraft was destroyed.
Probable cause:
Collision with trees on final approach due to improper IFR operation. The following contributing factors were reported:
- Low ceiling,
- Rain,
- Fog,
- Descended below decision height.
Final Report:

Crash of a Rockwell Aero Commander 690A in Culver City: 1 killed

Date & Time: Oct 21, 1976 at 1423 LT
Operator:
Registration:
N568H
Survivors:
No
Site:
Schedule:
Santa Barbara – Culver City
MSN:
690-11027
YOM:
1972
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
13785
Captain / Total hours on type:
972.00
Circumstances:
While approaching Culver City Airport on a flight from Santa Barbara, the twin engine airplane collided with a Beechcraft 35-C33 registered N21TH and owned by Steven I. Fendrik. Following the collision, both aircraft entered a dive and crashed in a residential area in Culver City. Both aircraft were destroyed as well as several cars and building. Both pilots on both aircraft were killed while there were no casualties on the ground. Both aircraft were under radar contact and flying in the vicinity of a controlled airport.
Probable cause:
In-flight collision in traffic pattern after the pilot failed to see and avoid other aircraft. The following contributing factors were reported:
- Pilot of other aircraft,
- Mid-air collision on downwind for runway 23.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain off Hampton: 4 killed

Date & Time: Oct 20, 1976 at 1908 LT
Registration:
N61436
Survivors:
No
Schedule:
Washington DC - Newport News - Baltimore
MSN:
31-7405465
YOM:
1974
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
2646
Captain / Total hours on type:
180.00
Circumstances:
While descending to Newport News-Williamsburg Airport on a schedule flight from Washington DC, the right engine failed. The crew lost control of the airplane that entered a dive and crashed into the sea off Hampton, about 12,5 miles southeast of the airport. The aircraft was lost and all four occupants were killed (the copilot's body was never recovered).
Probable cause:
Uncontrolled descent during initial approach due to engine structure failure (valve assemblies). The following contributing factors were reported:
- Diverted attention from operation of aircraft,
- Electrical system: generators/alternators,
- Failed to use or incorrectly used miscellaneous equipment,
- Aircraft came to rest in water,
- N°5 cylinder on right engine, exhaust valve would not seat,
- Right engine alternator bracket failed.
Final Report:

Crash of a Gulfstream GII in Hot Springs: 11 killed

Date & Time: Sep 26, 1976 at 1038 LT
Type of aircraft:
Operator:
Registration:
N500J
Survivors:
No
Schedule:
Trenton - Hot Springs
MSN:
60
YOM:
1969
Crew on board:
3
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
11
Captain / Total flying hours:
16982
Captain / Total hours on type:
523.00
Circumstances:
On approach to Hot Springs-Ingalls Field Airport, the crew encountered very poor weather conditions. On final, he failed to realize his altitude was too low when the airplane struck a mountain and crashed short of runway 24. The aircraft disintegrated on impact and all 11 occupants were killed. The wreckage was found 500 feet below the runway elevation. At the time of the accident, weather was poor with clouds down to 100 feet and fog.
Probable cause:
Controlled flight into terrain for undetermined reasons.
Final Report: