Crash of a Swearingen SA226T Merlin III in San Marcos

Date & Time: May 31, 1979 at 1042 LT
Operator:
Registration:
N5654M
Flight Type:
Survivors:
Yes
Schedule:
San Marcos - San Marcos
MSN:
T-303
YOM:
1979
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5300
Captain / Total hours on type:
6.00
Circumstances:
The twin engine airplane was engaged in a local experimentation flight at San Marcos Airport on behalf of the Federal Aviation Administration (FAA). During the last segment, at level off, the airplane landed hard and struck the runway surface. Upon impact, the undercarriage were torn off and the airplane came on its belly. All four occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
Hard landing following improper operation of powerplant and powerplant controls. The following contributing factors were reported:
- Improper level off,
- Overload failure,
- FAA flight test pilot at controls.
Final Report:

Crash of a De Havilland DHC-6 Twin Otter in Rockland: 17 killed

Date & Time: May 30, 1979 at 2055 LT
Operator:
Registration:
N68DE
Survivors:
Yes
Schedule:
Boston - Rockland
MSN:
229
YOM:
1969
Flight number:
DE46
Crew on board:
2
Crew fatalities:
Pax on board:
16
Pax fatalities:
Other fatalities:
Total fatalities:
17
Captain / Total flying hours:
5050
Captain / Total hours on type:
603.00
Copilot / Total flying hours:
2580
Copilot / Total hours on type:
46
Aircraft flight hours:
21050
Circumstances:
About 2055LT, Downeast Airlines flight 46 crashed into a heavily wooded area about 1,2 mile south-southwest of the Knox County Regional Airport in Rockland, Maine. The crash occurred during a non-precision instrument approach to runway 03 in instrument meteorological conditions. Of the 16 passengers and 2 crew members aboard, only one passenger survived the accident. The aircraft was destroyed.
Probable cause:
The National Transportation Safety Board determines that the probable cause of the accident was the failure of the flightcrew to arrest the aircraft's descent at the minimum descent altitude for the non-precision approach, without the runway environment in sight, for unknown reasons. Although the Safety Board was unable to determine conclusively the reason(s) for the flightcrew's deviation from standard instrument approach procedures, it is believed that inordinate management pressures, the first officer's marginal instrument proficiency, the captain's inadequate supervision of the flight, inadequate crew training and procedures, and the captaints chronic fatigue were all factors in the accident.
Final Report:

Crash of a Rockwell Grand Commander 680FL in Phoenix

Date & Time: May 29, 1979 at 1717 LT
Operator:
Registration:
N783EF
Flight Type:
Survivors:
Yes
Schedule:
Las Vegas - Phoenix
MSN:
680-1392-51
YOM:
1964
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2255
Captain / Total hours on type:
100.00
Circumstances:
On final approach to Phoenix-Sky Harbor Airport, while completing a cargo flight from Las Vegas, both engines lost power. The crew attempted an emergency landing when the airplane lost height and crashed short of runway threshold. The aircraft was damaged beyond repair and both pilots were seriously injured.
Probable cause:
Controlled collision with ground on final approach after the airplane encountered vortex turbulences. The following contributing factors were reported:
- Fuel starvation,
- Failure of both engines,
- Forced landing off airport on land,
- Violent wingrock on final uncovered fuel sump pickups allowing air to enter fuel lines.
Final Report:

Crash of a Beechcraft 65 Queen Air in Boca Raton: 1 killed

Date & Time: May 27, 1979 at 1620 LT
Type of aircraft:
Operator:
Registration:
N72DR
Flight Type:
Survivors:
Yes
Schedule:
West Palm Beach – Boca Raton – Fort Lauderdale
MSN:
LC-6
YOM:
1960
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
162
Circumstances:
On final approach to Boca Raton Airport, the pilot decided to initiate a go-around when the twin engine airplane struck power cables and crashed in flames short of runway. All three passengers were injured, two of them seriously, while the pilot was killed.
Probable cause:
Collision with power cables during a go-around procedure after the pilot failed to follow approved procedures. The following contributing factors were reported:
- Evasive maneuver to avoid collision,
- Witnesses stated that the aircraft appeared overtaking another aircraft on final,
- No communication established,
- Gear down during go-around.
Final Report:

Crash of a SCAN-30 near Skykomish: 4 killed

Date & Time: May 27, 1979
Type of aircraft:
Registration:
N4451
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Wenatchee - Stevens Lake
MSN:
33
YOM:
1949
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
712
Captain / Total hours on type:
49.00
Circumstances:
The seaplane was completing a flight from Wenatchee to Lake Stevens, carrying three passengers and one pilot. While cruising under VFR mode into adverse weather conditions, the airplane struck the slope of a mountain and crashed in the region of Skykomish. SAR operations were initiated but eventually abandoned after few days as no trace of the aircraft nor the four occupants was found. The wreckage was discovered by walkers in an isolated area on July 20, 1979.
Probable cause:
Controlled flight into terrain after the pilot continued VFR flight into adverse weather conditions. The following contributing factors were reported:
- High obstructions,
- low ceiling,
- Rain,
- Thunderstorm activity,
- Visibility less than a quarter of a mile.
Final Report:

Crash of a Lockheed PV-1 Ventura in Fort Lauderdale: 2 killed

Date & Time: May 26, 1979 at 1445 LT
Type of aircraft:
Registration:
N1514S
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Fort Lauderdale – Bimini
MSN:
5891
YOM:
1943
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3344
Circumstances:
After takeoff from Fort Lauderdale-Hollywood Airport, while climbing, the pilot reported engine problems and was cleared to return. The airplane lost speed and height then struck trees and crashed in a swamp. Both occupants were killed.
Probable cause:
Engine failure during initial climb and subsequent collision with trees and crash due to improper maintenance on part of the maintenance personnel. The following contributing factors were reported:
- Fuel system: carburetor,
- Leak,
- Corrosion,
- Lack of familiarity with aircraft,
- Forced landing off airport on land,
- Pilot had 15 hours dual,
- Hole in diaphragm,
- Anti-detonant fluid found in carburetor.
Final Report:

Crash of a Beechcraft D18 in Charleston: 1 killed

Date & Time: May 25, 1979 at 2317 LT
Type of aircraft:
Registration:
N1812D
Flight Type:
Survivors:
No
Schedule:
Charlotte - Youngstown
MSN:
A-826
YOM:
1952
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
7928
Captain / Total hours on type:
1800.00
Circumstances:
While in cruising altitude on a cargo flight from Charlotte to Youngstown, the pilot reported engine problems and elected to divert to Charleston-Kanawha Airport for an emergency landing. After being cleared, he initiated the descent when the airplane went out of control and crashed in flames few miles from the airfield. The aircraft was destroyed and the pilot, sole on board, was killed.
Probable cause:
Uncontrolled collision with ground on final approach after the pilot attempted operation with known deficiencies in equipment. The following contributing factors were reported:
- Improper IFR operation,
- Lubricating system: lines, hoses, fitting,
- Oil leak,
- Pilot fatigue,
- Low ceiling,
- Forced landing off airport on land,
- Pilot departed on last leg of flight despite observing large oil leak,
- Pilot on duty since 0730LT.
Final Report:

Crash of a De Havilland DHC-4 Caribou in Bullen Point: 3 killed

Date & Time: May 25, 1979 at 2040 LT
Type of aircraft:
Operator:
Registration:
N581PA
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Bullen Point - Deadhorse
MSN:
253
YOM:
1967
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
14738
Captain / Total hours on type:
2630.00
Circumstances:
During initial climb, the cargo shifted, causing the aircraft to stall and to crash in flames within the runway. The aircraft was destroyed and all three crew members were killed.
Probable cause:
Stall during initial climb due to inadequate preflight preparation. The following contributing factors were reported:
- Failed to follow approved procedures,
- Cargo shifted,
- Inadequate ground training procedures,
- Aircraft configured for STOL departure,
- Crashed 1,400 feet from start point,
- STOL operation not approved,
- New loadmaster.
Final Report:

Crash of a Douglas DC-10-10 in Chicago: 273 killed

Date & Time: May 25, 1979 at 1504 LT
Type of aircraft:
Operator:
Registration:
N110AA
Flight Phase:
Survivors:
No
Schedule:
Chicago - Los Angeles
MSN:
46510/22
YOM:
1971
Flight number:
AA191
Crew on board:
13
Crew fatalities:
Pax on board:
258
Pax fatalities:
Other fatalities:
Total fatalities:
273
Captain / Total flying hours:
22500
Captain / Total hours on type:
3000.00
Copilot / Total flying hours:
9275
Copilot / Total hours on type:
1200
Aircraft flight hours:
19871
Circumstances:
American Airlines Flight 191, a McDonnell-Douglas DC-10-10, crashed on takeoff from Chicago-O'Hare International Airport, Illinois, USA. The aircraft was destroyed and all 271 occupants were killed. Additionally, two persons on the ground sustained fatal injuries. At 14:59 hours local time Flight 191 taxied from the gate at O'Hare Airport. The flight was bound for Los Angeles, California, with 258 passengers and 13 crew members on board. Maintenance personnel who monitored the flight's engine start, push-back, and start of taxi did not observe anything out of the ordinary. The weather at the time of departure was clear, and the reported surface wind was 020° at 22 kts. Flight 191 was cleared to taxi to runway 32R for takeoff. The company's Takeoff Data Card showed that the stabilizer trim setting was 5° aircraft nose up, the takeoff flap setting was 10°, and the takeoff gross weight was 379,000 lbs. The target low pressure compressor (N1) rpm setting was 99.4 percent, critical engine failure speed (V1) was 139 kts indicated airspeed (KIAS), rotation speed (VR) was 145 KIAS, and takeoff safety speed (V2) was 153 KIAS. Flight 191 was cleared to taxi into position on runway 32R and hold. At 15:02:38, the flight was cleared for takeoff, and at 15:02:46 the captain acknowledged, "American one ninety-one under way." The takeoff roll was normal until just before rotation at which time sections of the No.1 (left) engine pylon structure came off the aircraft. Witnesses saw white smoke or vapor coming from the vicinity of the No. 1 engine pylon. During rotation the entire No. 1 engine and pylon separated from the aircraft, went over the top of the wing, and fell to the runway. Flight 191 lifted off about 6,000 ft down runway 32R, climbed out in a wings-level attitude. About nine seconds after liftoff, the airplane had accelerated to 172 knots and reached 140 feet of altitude. As the climb continued, the airplane began to decelerate at a rate of about one knot per second, and at 20 seconds after liftoff, and an altitude of 325 feet, airspeed had been reduced to 159 knots. At this point, the airplane began to roll to the left, countered by rudder and aileron inputs. The airplane continued to roll until impact, 31 seconds after liftoff, and in a 112-degree left roll, and 21-degree nose down pitch attitude. At 15:04 Flight 191 crashed in an open field and trailer park about 4,600 ft northwest of the departure end of runway 32R. The aircraft was demolished during the impact, explosion, and ground fire. The No.1 engine pylon failure during takeoff was determined to have been caused by unintended structural damage which occurred during engine/pylon reinstallation using a forklift. The engine/pylon removal and reinstallation were being conducted to implement two DC-10 Service Bulletins. Both required that the pylons be removed, and recommended that this be accomplished with the engines removed. The Service Bulletin instructions assumed that engines and pylons would be removed separately, and did not provide instructions to remove the engine and pylon as a unit. Additionally, removal of the engines and pylons as a unit was not an approved Maintenance Manual procedure. The lack of precision associated with the use of the forklift, essentially an inability to perform the fine manipulations necessary to accomplish reinstallation of the engine/strut assembly, in combination with the tight clearances between the pylon flange and the wing clevis resulted in damage to the same part that had just been inspected. Inspections of other DC-10 pylon mounts following the accident resulted in nine additional cracked mounts being identified.
Probable cause:
The asymmetrical stall and the ensuing roll of the aircraft because of the uncommanded retraction of the left wing outboard leading edge slats and the loss of stall warning and slat disagreement indication systems resulting from maintenance-induced damage leading to the separation of the no.1 engine and pylon assembly procedures which led to failure of the pylon structure. Contributing to the cause of the accident were the vulnerability of the design of the pylon attach points to maintenance damage; the vulnerability of the design of the leading edge slat system to the damage which produced asymmetry; deficiencies in FAA surveillance and reporting systems which failed to detect and prevent the use of improper maintenance procedures; deficiencies in the practices and communications among the operators, the manufacturer, and the FAA which failed to determine and disseminate the particulars regarding previous maintenance damage incidents; and the intolerance of prescribed operational procedures to this unique emergency.
Final Report:

Crash of a Douglas C-54S Skymaster in Mesa

Date & Time: May 15, 1979 at 1455 LT
Type of aircraft:
Operator:
Registration:
N44905
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Mesa - Chandler
MSN:
22159
YOM:
1945
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
12127
Captain / Total hours on type:
4399.00
Circumstances:
During the takeoff roll at Mesa-Falcon Field Airport, the crew started the rotation but the aircraft did not liftoff. It overran, struck a 10 feet high dirt bank, crossed a road where it hit a truck and eventually came to rest in flames in an orange grove. Both pilots, en route to Chandler-Stellar Airpark on a test flight, were seriously injured and the aircraft was destroyed by fire.
Probable cause:
Collision with dirt bank on takeoff due to inadequate preflight preparation. The following contributing factors were reported:
- Failed to abort takeoff,
- Failed to use the checklist,
- Gust locks engaged.
Final Report: