Crash of a Beechcraft 65-80 Queen Air in Sebring

Date & Time: Apr 6, 1980 at 2200 LT
Type of aircraft:
Registration:
N717Q
Flight Type:
Survivors:
Yes
MSN:
LD-66
YOM:
1963
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
While flying at low height by night on an illegal flight, both engines failed. The airplane descend, collided with trees and crash landed in a swamp. Both occupants were injured and the aircraft was damaged beyond repair.
Probable cause:
Engine failure or malfunction for undetermined reasons. The following contributing factors were reported:
- Forced landing off airport on land,
- 16 bales of marijuana found aboard the aircraft.
Final Report:

Crash of a Canadair CL-600-1A11 Challenger 600 in California City: 1 killed

Date & Time: Apr 3, 1980 at 0910 LT
Type of aircraft:
Operator:
Registration:
C-GCGR-X
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Mojave - Mojave
MSN:
1001
YOM:
1978
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
7782
Captain / Total hours on type:
468.00
Circumstances:
The crew departed Mojave-Kern County Airport in the morning on a series of tests on this new Bombardier prototype. While in cruising altitude, the crew initiated an unscheduled stall when the airplane reached an angle of attack of 34°. Control was lost and the airplane entered a dive. All three crew members bailed out and the airplane crashed in a desert area. Two crew members were injured while the third occupant was killed as his parachute failed to open.
Probable cause:
Uncontrolled collision with ground following an emergency descent due to technical problems with instruments/equipment. The following contributing factors were reported:
- Flight and navigation instruments: angle of attack indicator,
- Binding,
- Hydraulic system: seals, deteriorated,
- Unknown failure in emergency chute jettison system.
Final Report:

Crash of a Cessna 414 Chancellor in Gulfport

Date & Time: Apr 2, 1980 at 1846 LT
Type of aircraft:
Registration:
N1659T
Flight Phase:
Survivors:
Yes
Schedule:
Gulfport - Greenville
MSN:
414-0452
YOM:
1974
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2670
Captain / Total hours on type:
59.00
Circumstances:
After takeoff from Gulfportg-Biloxi Airport, while in initial climb, the twin engine airplane banked right, descended and crashed near the airfield. All five occupants were injured, the pilot and a passenger seriously. The airplane was destroyed.
Probable cause:
Engine malfunction during initial climb and subsequent controlled collision with ground for undetermined reasons. The following contributing factors were reported:
- Powerplant failure for undetermined reasons,
- The pilot failed to follow approved procedures,
- Improper emergency procedures on part of the pilot,
- Forced landing off airport,
- Right engine lost power,
- Right propeller not feathered.
Final Report:

Crash of a Cessna 441 Conquest II in Butte: 2 killed

Date & Time: Apr 1, 1980 at 1842 LT
Type of aircraft:
Operator:
Registration:
N36941
Survivors:
No
Site:
Schedule:
Forsyth - Butte
MSN:
441-0018
YOM:
1977
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
13826
Captain / Total hours on type:
68.00
Circumstances:
On approach to Butte-Bert Mooney Airport, the pilot encountered poor weather conditions and decided to initiate a go-around and to divert to another airport. At low height, the twin engine airplane struck a hill and crashed 11 miles south of the airport. Both occupants were killed.
Probable cause:
Controlled collision with ground during a missed approach due to improper IFR operation. The following contributing factors were reported:
- Low ceiling,
- Fog,
- Snow.
Final Report:

Crash of a Beechcraft 200 Super King Air 200 near Parker: 10 killed

Date & Time: Mar 27, 1980 at 1452 LT
Operator:
Registration:
N456L
Flight Phase:
Survivors:
No
Schedule:
Lufkin – Denver – Nacogdoches
MSN:
BB-112
YOM:
1976
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
10
Captain / Total flying hours:
10225
Captain / Total hours on type:
550.00
Circumstances:
About 9 1/2 minutes after departure from Denver-Arapahoe County Airport, while climbing, the crew declared an emergency, reporting airframe icing. The crew was vectored to Denver-Stapleton International Airport when the aircraft entered a controlled descent until it crashed in a prairie located about 13 miles east of Arapahoe Airport, northeast of Parker. The aircraft was totally destroyed upon impact and all 10 occupants were killed.
Probable cause:
The probable cause of the accident was the rapid accumulation of ice on the underwing surface aft of the deicing boots which destroyed the aircraft's capability to maintain level flight because the flightcrew: failed to obtain a current weather briefing before departure; failed to make a timely decision to discontinue the climb and return to Arapahoe Airport; and operated the over-gross-weight aircraft at high angles of attack in severe icing conditions.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in Houston: 7 killed

Date & Time: Mar 21, 1980 at 1949 LT
Registration:
N59932
Flight Phase:
Survivors:
Yes
Schedule:
Houston - Brownwood
MSN:
31-7552046
YOM:
1975
Crew on board:
2
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
4313
Captain / Total hours on type:
813.00
Copilot / Total flying hours:
3250
Aircraft flight hours:
5545
Circumstances:
The flight from William P. Hobby Airport, Houston, Texas, to Brownwood, Texas, was scheduled to depart Hobby Airport at 1915. Two intermediate stops were scheduled. It was operating behind schedule because of delays in the first three flights of the day which were flown by the same captain who was readying Flight 108. The aircraft had been on the ground for 31 minutes between the time it landed and the time it taxied for takeoff. Two crewmembers and eight passengers were on board Flight 108. At 1941, the ground controller cleared Flight 108 to taxi to runway 22. At 1943:40 the captain reported that Flight 108 was ''ready to go on 22," and at 1945:10 transmitted "Eagle Air 108 is No. 1 for 22." At 1945:55, Flight 108 was cleared to taxi into position and to hold on runway 22. A pilot of an aircraft in the runup area adjacent to runway 22 stated that Flight 108 did not use the runup area, nor did he see the crew conduct an engine runup while awaiting takeoff clearance. At 1947:50, Flight 108 was cleared for takeoff, and at 1948:35, the tower air traffic controller inquired if Flight 108 would be making a right turn away from the airport. Flight 108 responded, "Eagle 108 just lost the right engine." The controller stated that when this transmission was made the aircraft was about 4,300 ft from the start of its takeoff roll and about 100 ft above the runway. A pilot witness on the ground stated that the aircraft was between 100 and 200 ft above the runway when the crew reported the loss of the right engine. An Eagle Airlines employee identified the person who made the transmission as a company employee--a pilot-in-command trainee who was in the copilot seat. The aircraft maintained runway heading for about 10 sec more before it began a right turn and a shallow descent. The rate of turn, the angle of bank to the right, and the rate of descent continued to increase as the aircraft turned 90° away from the runway heading. The angle of bank also increased as the aircraft descended, but the crew managed to level the wings just before impact. A passenger who was seated two seats behind the captain stated that when the aircraft was about 50 ft in the air he heard an engine "sputter" which continued until impact. The aircraft dropped, veered left, then right, and down." He recalled that a crewmember said, "What's next or what do we do now." A passenger on the right side, four seats back, heard a "popping or thudding" noise after the aircraft left the runway and veered to the right. He recalled that someone said, 'What do I do?". The third survivor was seated in the left rear seat. He heard an engine go "pop-pop like a backfire." He saw the captain pull back the "left red controls and the right pilot reach and turn things." None of the survivors could tell who was flying the aircraft. The aircraft crashed on a concrete airport parking ramp in a nearly level pitch attitude, with the right wing slightly lowered, about 1,000 ft from the runway. It then slid 200 ft on the ramp and hit two aircraft, four cars, and finally a hangar. A fire broke out when the aircraft hit the cars and the hangar. The accident occurred during hours of darkness.
Probable cause:
The probable cause of the accident was a power loss in the right engine for undetermined reasons at a critical point in the takeoff phase, the aircraft's marginal single-engine performance capability, and the captain's immediate landing on the remaining runway, or to configure the aircraft properly for the engine-out incorrect emergency response to the engine power loss when he failed either to land condition.
Final Report:

Crash of a Cessna 421C Golden Eagle III in Decatur: 2 killed

Date & Time: Mar 20, 1980 at 2323 LT
Registration:
N31LP
Survivors:
No
Schedule:
Little Rock - Decatur
MSN:
421C-0046
YOM:
1976
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
28260
Captain / Total hours on type:
610.00
Circumstances:
On an instrument approach to Decatur-Crystal Lake Airport, the pilot cancelled the IFR flight plan and continued under VFR mode when he encountered limited visibility due to fog. He decided to initiate a go-around when the twin engine airplane struck power cables and crashed in flames. Both occupants were killed.
Probable cause:
Collision with wires/poles during a go-around after the pilot continued VFR flight into adverse weather conditions. The following contributing factors were reported:
- Fog,
- High obstructions,
- Weather conditions below minimums,
- Fog on runway surface,
- Runway lights on,
- VASI inoperative.
Final Report:

Crash of a Douglas DC-9-14 in Baton Rouge

Date & Time: Mar 17, 1980 at 1645 LT
Type of aircraft:
Operator:
Registration:
N9103
Survivors:
Yes
Schedule:
Houston - Baton Rouge
MSN:
45796/74
YOM:
1966
Crew on board:
4
Crew fatalities:
Pax on board:
46
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
15732
Captain / Total hours on type:
8720.00
Circumstances:
The airplane landed in rain falls with a 18 knots tailwind about 2,000 feet down runway 13 which is 5,800 feet long. Unable to stop within the remaining distance, the airplane overran and came to rest in a ditch about 350 feet further and 200 feet to the right of the extended centreline. All 50 occupants escaped without injuries while the aircraft was damaged beyond repair. At the time of the accident, the total weight of the airplane was 71,000 lbs.
Probable cause:
Overshoot on landing and subsequent overrun and collision with ditch because ATC cleared the aircraft to wrong runway for existing conditions. The following contributing factors were reported:
- Improper in-flight decisions on part of the pilot-in-command,
- Improper operation of brakes and flight controls on part of the pilot-in-command,
- Rain,
- Wet runway,
- Downwind,
- Haze,
- Aircraft over 25,000 lbs upon landing on runway 13, restricted to zero tailwind/10 knots crosswind when wet,
- Runway 22 available,
- Spoilers not used after touchdown.
Final Report:

Crash of a Cessna 414 Chancellor near Vacaville: 5 killed

Date & Time: Mar 14, 1980 at 1845 LT
Type of aircraft:
Operator:
Registration:
N4632G
Flight Phase:
Survivors:
No
Schedule:
Auburn - Novato
MSN:
414-0903
YOM:
1976
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
En route from Auburn to Novato, both engines stopped almost simultaneously. The pilot attempted to make an emergency landing when the airplane struck tree tops and crashed in a wooded area located near Vacaville, about 31 miles northeast of Novato-Gnoss Field. All five occupants were killed.
Probable cause:
Double engine failure in flight and subsequent collision with trees while attempting an emergency landing due to an inadequate preflight preparation on part of the pilot. The following contributing factors were reported:
- Mismanagement of fuel,
- Fuel exhaustion,
- Forces landing off airport on land.
Final Report:

Crash of a Cessna 421B Golden Eagle II in Tucson: 2 killed

Date & Time: Mar 14, 1980 at 1645 LT
Operator:
Registration:
N59RZ
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Tucson - Tucson
MSN:
421B-0249
YOM:
1972
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
9590
Circumstances:
The twin engine airplane departed Tucson-Ryan Airport on a local post maintenance flight, carrying one pilot and one mechanic. During initial climb, the airplane went out of control and crashed in flames in a field. Both occupants were killed.
Probable cause:
Airframe failure during climb due to inadequate maintenance and inspection. The following contributing factors were reported:
- Airframe - flight control surfaces: elevator assembly, attachments, missing, flutter,
- Overload failure,
- Bolts missing from elevators,
- Elevator push-pull tube rivets failed,
- Overload elevator/stabilizers twisted.
Final Report: