Crash of a Cessna 411 in Vineland: 4 killed

Date & Time: May 9, 1980 at 1453 LT
Type of aircraft:
Operator:
Registration:
N4973T
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Bridgeport – Washington DC – Atlantic City
MSN:
411-0193
YOM:
1966
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
652
Circumstances:
While in cruising altitude, one of the engine failed. The pilot lost control of the airplane that stalled and entered a spin. It crashed in a field located near Vineland and exploded on ground. All four occupants were killed.
Probable cause:
Powerplant failure for undetermined reasons. The following contributing factors were reported:
- The pilot failed to maintain flying speed,
- Complete failure on one engine,
- Emergency circumstances unknown/not reported.
Final Report:

Crash of a Learjet 23 in Richmond: 2 killed

Date & Time: May 6, 1980 at 0312 LT
Type of aircraft:
Registration:
N866JS
Flight Type:
Survivors:
No
Schedule:
Richmond – Louisville – Gainesville – Richmond
MSN:
23-018
YOM:
1965
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
2547
Captain / Total hours on type:
301.00
Copilot / Total flying hours:
905
Copilot / Total hours on type:
10
Aircraft flight hours:
4861
Circumstances:
On May 5, 1980, an unmodified Gates Learjet 23 (N866JS) was operated by Kennedy Flite Center, Richmond, Virginia, on a purported crew training flight. The pilot called the Newport News, Virginia, flight service station (FSS) about 2105 and received a weather briefing for a flight originating in Richmond to Louisville, Kentucky, continuing to Gainesville, Florida, and returning to Richmond. He filed three instrument flight rules (IFR) flight plans. The first flight plan called for a flight of 1+00 hour from Richmond to Louisville with the pilot and copilot aboard. The second flight plan called for a flight of 1+29 hours from Louisville to Gainesville with the pilot, copilot, and six passengers aboard. The third flight plan called for a flight of 1+10 hours from Gainesville to Richmond with the pilot and copilot aboard. All of the plans requested flight level (FL) 410 as an en route altitude. N866JS departed Richmond about 2128 with the two pilots aboard, and arrived at Standiford Field in Louisville at 2228 after a routine flight. The aircraft was refueled with 386 gallons of Jet A fuel costing $479.46, which was paid by check. The flightcrew boarded the six passengers, who were friends of the copilot according to the company's flight manager, and the aircraft departed Louisville at 2315. After a routine flight, the aircraft arrived at Gainesville Regional Airport at 0044, May 6, 1980, and the passengers deboarded. Charter Air Center service personnel "topped off" the fuel tanks with 404 gallons of Jet A fuel. The fuel bill was $596.63, which was paid in cash. The flight departed Gainesville at 0152. Initial climb was to 23,000 feet with further clearance to FL 370 and final clearance to the requested FL 410. The en route portion of the flight proceeded normally, and at 0257, during descent, the aircraft was handed off at 14,000 feet by the Washington Air Route Traffic Control Center to Richmond approach control. The Richmond approach controller acknowledged the handoff, gave current weather and wind conditions, and told the flightcrew to expect a visual approach to runway 2 at the Byrd International Airport. The flightcrew requested an instrument landing system (ILS) approach to runway 33. This request was acknowledged, and the approach controller vectored the aircraft to the ILS final approach course, outside of the outer marker, at 2,000 feet. The approach controller turned the aircraft over to the local control tower operator at 0308. Radio communication between the aircraft and the tower controller was established, and the aircraft was cleared to land at 0308:41. While on final approach at about 2 miles from the runway, the pilot asked for a wind check, and the controller responded that the winds were calm. About 0311:10, the flightcrew requested that the sequenced flashing approach lights be turned down and the controller asked that the message be repeated. The controller heard two garbled radio transmissions within 40 seconds referring to lights, and he dimmed the lights when the aircraft was about 0.5 mile from the runway. The tower controller stated that the aircraft's flightpath appeared higher than normal and that N866JS seemed, to float down the runway at about 50 feet altitude. He then'saw the wingtip lights rocking back and forth, the nose of the aircraft rising, and the aircraft starting to roll. He stated that he reached for the crash phone when he saw the wings rocking because he was concerned about the safety of the aircraft. He then saw a ball of fire on runway 33 and immediately sounded the crash alert; the time was 0311:58. A Virginia Air National Guard security guard on duty near an aircraft parking ramp and the "M" taxiway adjacent to runway 33 witnessed the accident. He stated that he was in a parked truck, engine off, with an unobstructed view of the runway approach zone and touchdown area. He said that the aircraft was "a bit high" on its approach, but descended to a normal touchdown attitude and altitude with the noise of the engines winding down. He did not hear the "screech" of the tires which would have been normal if the aircraft touched the runway. Instead, he said that the aircraft yawed right, the nose came up, and the aircraft started to roll to the right. The roll continued to the inverted position accompanied by a buildup of engine noise. He then saw the aircraft strike the ground inverted, catch fire, and explode. Another security guard on duty at the entrance to the Air National Guard base also witnessed part of the accident sequence. He observed the approach to runway 33 and stated that he thought the aircraft was landing farther down the runway than normal. He did not hear the aircraft touch down, but did hear a sudden rise of engine noise. He saw a white light traveling down the runway followed by an orange fireball and flames. The aircraft was totally destroyed and both pilots were killed.
Probable cause:
The pilot's failure to maintain proper airspeed and aircraft attitude while transitioning from final approach through flare to touchdown. The low-speed/high angle-of attack flight condition precipitated wing rolloff, wingtip strikes, and ultimate loss of aircraft control. The pilot's improper technique during roundout may have been due to fatigue, his limited knowledge, training, and experience regarding the flight characteristics of the Learjet aircraft, and distraction caused by concern over the intensity of the approach lighting.
Final Report:

Crash of a Cessna 404 Titan in New Orleans: 1 killed

Date & Time: Apr 27, 1980 at 2332 LT
Type of aircraft:
Registration:
N5237J
Survivors:
Yes
Schedule:
Las Vegas - New Orleans - Mobile
MSN:
404-0619
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
On final approach to New Orleans-Moisant Airport, both engines failed. The aircraft stalled and crashed few miles from the airport. The passenger was seriously injured and the pilot was killed. The aircraft was destroyed.
Probable cause:
Double engine failure, stall and subsequent crash on final approach due to an inadequate preflight preparation. The following contributing factors were reported:
- Mismanagement of fuel,
- Improper in-flight decisions or planning,
- Fuel exhaustion,
- The pilot failed to maintain flying speed,
- Complete failure of both engines.
Final Report:

Crash of a Cessna 404 Titan in Dade-Collier

Date & Time: Apr 25, 1980 at 0430 LT
Type of aircraft:
Operator:
Registration:
N3994C
Flight Type:
Survivors:
Yes
MSN:
404-0021
YOM:
1976
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The twin engine airplane was engaged in an illegal flight, carrying a load of marijuana. While flying at low height by night in the vicinity of Dade-Collier Airport, the airplane struck trees and crashed. The passenger was seriously injured and the pilot disappeared and was not found.
Probable cause:
Collision with trees by night for unknown reasons. Illegal flight.
Final Report:

Crash of a Mitsubishi MU-2B-10 Marquise in Henderson: 1 killed

Date & Time: Apr 23, 1980 at 2042 LT
Type of aircraft:
Operator:
Registration:
N307MA
Flight Type:
Survivors:
No
Schedule:
San Angelo – Albuquerque – Henderson
MSN:
0007
YOM:
1967
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
808
Circumstances:
On approach to Henderson-Sky Harbor Airport, the pilot encountered technical problems with the fuel supply system. On final, the twin engine airplane stalled and crashed in a rocky area located one mile short of runway. The aircraft burst into flames and the pilot, sole on board, was killed.
Probable cause:
Stall on traffic pattern-circling after the pilot-in-command failed to maintain flying speed. The following contributing factors were reported:
- The pilot-in-command attempted operation with known deficiencies in equipment,
- Fuel system: other,
- Material failure,
- ATC failed to advise the pilot of unsafe airport conditions,
- Airport facilities: other,
- Precautionary landing on airport,
- Low on fuel,
- Wingtip tank sniffer valve o-ring seal failed before flight,
- Diverted to unlighted runway.
Final Report:

Crash of a Douglas C-47B-20-DK in Fort Lauderdale

Date & Time: Apr 23, 1980 at 1654 LT
Registration:
N709Z
Survivors:
Yes
Schedule:
Bimini - Fort Lauderdale
MSN:
15737/27182
YOM:
1945
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
12053
Captain / Total hours on type:
64.00
Circumstances:
On final approach to Fort Lauderdale-Hollywood Airport, the airplane stalled and crashed near Dania. A pilot was seriously injured while seven other occupants were slightly injured.
Probable cause:
Stall and subsequent crash while initiating a go-around. The following contributing factors were reported:
- The pilot-in-command delayed in initiating go-around,
- The pilot-in-command failed to maintain flying speed,
- The copilot failed to follow approved procedures,
- The copilot misused or failed to use flaps.
Final Report:

Crash of a Learjet 25B near Conlon: 2 killed

Date & Time: Apr 11, 1980 at 1719 LT
Type of aircraft:
Registration:
N25TA
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Vernal - Houston
MSN:
25-196
YOM:
1975
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
7800
Captain / Total hours on type:
1000.00
Circumstances:
While cruising at an altitude of 41,200 feet, the airplane entered an uncontrolled descent following an airframe failure in flight. The airplane crashed in an open field and was totally destroyed. Both pilots who were completing a ferry flight from Vernal to Houston were killed.
Probable cause:
Airframe failure in flight, separation in flight and subsequent uncontrolled descent for undetermined reasons.
Final Report:

Crash of a Douglas C-47A-30-DL in Athol: 3 killed

Date & Time: Apr 11, 1980 at 1700 LT
Registration:
N64490
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Athol - Athol
MSN:
13915/25360
YOM:
1944
Crew on board:
3
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
3600
Circumstances:
Shortly after takeoff from Athol-Silverwood, while in initial climb, the airplane encountered difficulties to gain height. It stalled and crashed in flames in a prairie located past the runway end. All three passengers were seriously injured while all three crew members were killed.
Probable cause:
Engine failure during initial climb for undetermined reasons. The following contributing factors were reported:
- Failed to abort takeoff,
- First flight of aircraft for approximately 11 months,
- Pilot's certificate was under suspension.
Final Report:

Crash of a Cessna 340 in Crystal: 2 killed

Date & Time: Apr 8, 1980 at 1924 LT
Type of aircraft:
Registration:
N98547
Flight Phase:
Survivors:
Yes
Schedule:
Crystal - Fargo
MSN:
340-0027
YOM:
1972
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1538
Captain / Total hours on type:
700.00
Circumstances:
During a night takeoff from a snow covered runway at Crystal Airport, the twin engine airplane drifted off, collided with trees and crashed, bursting into flames. The pilot was seriously injured while both passengers were killed. At the time of the accident, the visibility was below minimums due to fog and snow falls.
Probable cause:
Collision with trees during initial climb after the pilot failed to abort takeoff and failed to maintain a positive rate of climb. The following contributing factors were reported:
- Fog,
- Snow,
- Snow on runway,
- Visibility 3/4 mile or less,
- Weather conditions below minimums,
- Drifted off, back on runway,
- Take off at end.
Final Report:

Crash of a Cessna 401 in Linville: 1 killed

Date & Time: Apr 7, 1980 at 0837 LT
Type of aircraft:
Operator:
Registration:
N9912F
Flight Phase:
Survivors:
No
Site:
Schedule:
Myrtle Beach - Cincinnati
MSN:
401-0091
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
8919
Captain / Total hours on type:
480.00
Circumstances:
While cruising at an altitude of 5,900 feet in limited visibility due to marginal weather conditions, the twin engine airplane struck the slope of a mountain located near Linville. The aircraft was destroyed and the pilot, sole on board, was killed. At the time of the accident, the visibility was reduced to zero due to low ceiling, rains falls and fog.
Probable cause:
Controlled flight into terrain during normal cruise after the pilot continued VFR flight into adverse weather conditions. The following contributing factors were reported:
- Physical impairment of the pilot,
- Alcoholic impairment of efficiency and judgment,
- Low ceiling,
- Rain,
- Fog,
- Blood ethanol level 90 mg %,
- Hit the mountain at 5,909 feet,
- Mountain obscured.
Final Report: