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Crash of a Cessna 550 Citation II in Mesquite

Date & Time: Jul 17, 2019 at 1844 LT
Type of aircraft:
Operator:
Registration:
N320JT
Flight Type:
Survivors:
Yes
Schedule:
Pasco - Las Vegas
MSN:
550-0271
YOM:
1981
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
17000
Captain / Total hours on type:
2000.00
Aircraft flight hours:
9000
Circumstances:
While approaching class B airspace, the airline transport pilot was in communication with a controller who later stated that the pilot's speech was slurred, and the controller repeatedly asked if the oxygen system on the airplane was working properly. As the airplane approached a nearby airport, about 85 miles from his destination airport, the pilot stated he had the airport in sight and repeatedly requested a visual approach. The controller instructed the pilot to continue his flight to his destination, in a southwest direction. As the controller attempted to maintain communications, the pilot dropped off radar shortly after passing the nearby airport and subsequently landed at the nearby airport, which was not his destination airport. According to a surveillance video and impact marks on the runway, the airplane landed hard about halfway down the runway and slid to a stop on the left side of the runway. The airplane fuselage and wings were mostly consumed by postimpact fire. After authorities arrived onsite, the pilot was arrested for operating an aircraft under the influence of alcohol. The pilot was found to have a blood alcohol level of .288, which likely contributed to the pilot landing at the incorrect airport and his subsequent loss of airplane control during landing.
Probable cause:
The pilot's operation of the airplane while intoxicated, which resulted in a loss of airplane control on landing.
Final Report:

Crash of a Cessna T207A Skywagon near Henderson: 1 killed

Date & Time: Dec 8, 2004 at 1031 LT
Operator:
Registration:
N1783U
Flight Phase:
Survivors:
No
Site:
Schedule:
Henderson - Henderson
MSN:
207-0383
YOM:
1977
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1209
Captain / Total hours on type:
117.00
Aircraft flight hours:
12616
Circumstances:
The airplane impacted mountainous terrain in an extreme nose-down attitude following a departure from controlled flight. The purpose of the flight was to check the weather conditions for passenger tour flights that day. The pilot reported about 20 minutes prior to the accident that the ceiling was 6,500 feet mean sea level (msl). Radar data showed that following this weather report, the airplane's radar track continued eastbound and upon its return westbound, at an altitude of about 6,000 feet msl, the airplane entered a series of altitude fluctuations approximately 1 mile west of a ridge that was the location of the accident, descending at 4,000 feet per minute while turning northbound, and then climbing at 3,900 feet per minute while traveling eastbound, prior to disappearing from the radar. The airplane impacted on the eastern side of the ridge. There were no monitored distress calls from the aircraft and no known witnesses to the accident. Prior to the accident, there were reports of vibrations during flight on this aircraft, although many went unreported to maintenance personnel. The day (and flight) prior to the accident, a pilot experienced a vibration during flight with passengers and it was not reported to maintenance personnel because it was logged improperly in the operator's maintenance tracking system. No corrective actions were taken. During the post accident examinations, no portions of the right elevator and trim tab were identified in the wreckage, or at the accident site. The bracket attachment to the right elevator was found loose within the wreckage and was torsionally twisted counterclockwise (aft). Ground and aerial searches for the missing parts based on a trajectory study were unsuccessful. This aircraft was equipped with a foam cored elevator trim tab that was installed during aircraft manufacture. A service difficulty report (SDR) query showed that 47 reports had been issued on elevator trim tab corrosion and many included reports of vibrations during flight. On January 20, 2005, the Federal Aviation Administration (FAA) issued Special Airworthiness Information Bulletin (SAIB) CE-05-27, which addressed potential problems with foam-filled elevator trim tabs in the accident make/model airplane, and Cessna 206 and 210 series airplanes. The SAIB indicated that the foam-filled elevator trim tabs, manufactured until 1985, were reported to have corrosion between the tab and the foam. The SAIB further said, in part, "When the skin of the trim tab becomes thin enough due to the corrosion, the actuator can pull the fasteners through the skin and disconnect. When this occurs, the tab can flutter." Some reports indicated prior instances of "vibrations in the tail section and portions of the elevator tearing away with the trim tab." Prior to the issuance of the SAIB, Cessna Aircraft Company issued a Service Bulletin (SB) SEB85-7 on April 5, 1985, that addressed elevator and trim tab inspection due to corrosion from moisture trapped in the foam cored trim tabs. Based on a review of the airplane's logbooks, the SB was not complied with, nor was the operator required to do so based on the FAA approved maintenance specifications.
Probable cause:
A loss of control due to the in-flight separation of the right elevator and elevator trim tab control surfaces. The precipitating reason for the elevator separation could not be resolved as related to the tab foam core issue with the available evidence.
Final Report:

Crash of a Mitsubishi MU-2B-10 Marquise in Henderson: 1 killed

Date & Time: Apr 23, 1980 at 2042 LT
Type of aircraft:
Operator:
Registration:
N307MA
Flight Type:
Survivors:
No
Schedule:
San Angelo – Albuquerque – Henderson
MSN:
0007
YOM:
1967
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
808
Circumstances:
On approach to Henderson-Sky Harbor Airport, the pilot encountered technical problems with the fuel supply system. On final, the twin engine airplane stalled and crashed in a rocky area located one mile short of runway. The aircraft burst into flames and the pilot, sole on board, was killed.
Probable cause:
Stall on traffic pattern-circling after the pilot-in-command failed to maintain flying speed. The following contributing factors were reported:
- The pilot-in-command attempted operation with known deficiencies in equipment,
- Fuel system: other,
- Material failure,
- ATC failed to advise the pilot of unsafe airport conditions,
- Airport facilities: other,
- Precautionary landing on airport,
- Low on fuel,
- Wingtip tank sniffer valve o-ring seal failed before flight,
- Diverted to unlighted runway.
Final Report: