Crash of a PZL-Mielec AN-2R in Promin: 2 killed

Date & Time: Mar 25, 2015 at 0046 LT
Type of aircraft:
Registration:
UR-62681
Flight Type:
Survivors:
No
MSN:
1G179-11
YOM:
1978
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The crew was performing an illegal flight, most probably from Belarus, with a load of cigarettes on board. By night, he was attempting to land in a field located in Promin when the single engine aircraft impacted the roof of a house and crashed on a small road, bursting into flames. The aircraft was destroyed by a post crash fire and both occupants were killed.

Crash of a Cessna 208B Grand Caravan in Verdigris

Date & Time: Mar 24, 2015 at 1507 LT
Type of aircraft:
Operator:
Registration:
N106BZ
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Tulsa - Tulsa
MSN:
208B-0106
YOM:
1988
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6500
Captain / Total hours on type:
970.00
Aircraft flight hours:
11443
Circumstances:
The pilot reported that, during the postmaintenance test flight, the turboprop engine lost power. The airplane was unable to maintain altitude, and the pilot conducted a forced landing, during which the airplane was substantially damaged. The engine had about 9 total flight hours at the time of the accident. A teardown of the fuel pump revealed that the high-pressure drive gear teeth exhibited wear and that material was missing from them, whereas the driven gear exhibited little to no visible wear. A metallurgical examination of the gears revealed that the damaged drive gear was made of a material similar to 300-series stainless steel instead of the harder specified M50 steel, whereas the driven gear was made of a material similar to the specified M50 steel. Subsequent to these findings, the airplane manufacturer determined that the gear manufacturer allowed three set-up gears made from 300-series stainless steel to become part of the production inventory during the manufacturing process. One of those gears was installed in the fuel pump on the accident airplane, and the location of the two other gears could not be determined. Based on the evidence, it is likely that the nonconforming gear installed in the fuel pump failed because it was manufactured from a softer material than specified, which resulted in a loss of fuel flow to the engine and the subsequent loss of engine power. The manufacturer subsequently inspected its stock of gears and issued notices to customers that had engines with fuel pumps installed with the same part number gear set as the one installed on the accident airplane. The manufacturer also issued a service information letter and service bulletins regarding the fuel pump gear set for engines used in civilian and military applications. As of the date of this report, the two remaining gears have not been located.
Probable cause:
The fuel pump gear manufacturer’s allowance of set-up gears made from a nonconforming material to be put in the production inventory system, the installation of a nonconforming gear in the accident airplane’s production fuel pump, and the gear’s failure, which resulted in a loss of fuel flow to the engine and the subsequent loss of engine power.
Final Report:

Crash of a Piper PA-46-350P Malibu Mirage JetProp DLX in Sézenove: 1 killed

Date & Time: Jan 30, 2015 at 1201 LT
Operator:
Registration:
N246PR
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Geneva - Genk
MSN:
46-36063
YOM:
1996
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1073
Captain / Total hours on type:
89.00
Aircraft flight hours:
1997
Circumstances:
The pilot, sole on board, departed Geneva-Cointrin Airport on a private flight to Genk-Zwartberg Airport where the aircraft was supposed to follow a maintenance program. The single engine aircraft departed runway 23 at 1157LT and continued to climb in IMC conditions. About 30 seconds after he was transferred to the departure frequency, the pilot was cleared to climb to FL090. At an altitude of 4,200 feet and at a speed of 142 knots, the aircraft climbed steeply then veered to the left. About 12 seconds later, the aircraft stopped to climb and another period of 8 seconds was necessary to stabilize and to follow the route. At 1159LT, the aircraft deviated to the left during 20 seconds, drifting about 555 metres from the runway axis. After following various headings with huge variations in ground speed and altitude, the aircraft entered an uncontrolled descent and crashed in an open field located in Sézenove, about 7,8 km southwest from Geneva-Cointrin Airport runway 05 threshold. The aircraft disintegrated on impact and the pilot was killed.
Probable cause:
The accident was due to a loss of control that brought the aircraft into unusual attitudes, which the pilot was unable to restore and which led to his fall. The insufficient skills of the pilot when faced with a high performance aircraft, whose systems are complex, contributed to the occurrence of the accident.
Final Report:

Crash of a Britten Norman BN-2T Islander near Dawlatabad

Date & Time: Jan 20, 2015
Type of aircraft:
Operator:
Registration:
ZS-NAT
Flight Phase:
Survivors:
Yes
MSN:
2158
YOM:
1986
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft was completing a geophysical mission on behalf of Xcalibur Airborne Geophysics, with two pilots on board. En route, the crew encountered an unexpected situation and attempted an emergency landing. The aircraft crash landed in a rocky terrain, lost its undercarriage and came to rest. Both occupants escaped uninjured and the aircraft was damaged beyond repair.

Crash of a Britten Norman BN-2A-6 Islander near Mahdia: 2

Date & Time: Dec 28, 2014 at 1145 LT
Type of aircraft:
Operator:
Registration:
8R-GHE
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Mahdia – Karisparu
MSN:
269
YOM:
1971
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
8000
Aircraft flight hours:
25818
Circumstances:
The crew (a pilot and a load master) was performing a regular cargo service to Karisparu and departed Mahdia Airport at 1142LT. The duration of the flight should be less than 20 minutes as the aircraft was scheduled to arrive at Karisparu Airfield at 1200LT. Less than three minutes after departure, the radio contact was lost with the pilot. SAR operations were initiated but after four days, no trace of the aircraft nor the crew was found. The Director General of the Guyana Civil Aviation Authority (GCAA), Zulfikar Mohamed, said that the crucial 72-hour window period since the aircraft vanished in the thick jungle in Region Eight expired on Tuesday December 30. On January 4, 2015, all SAR operations were suspended as no trace of the aircraft was found.
Probable cause:
Due to lack of evidences, the cause of the accident could not be determined.
Final Report:

Crash of a Learjet 25D in Champotón: 2 killed

Date & Time: Dec 19, 2014 at 1800 LT
Type of aircraft:
Operator:
Registration:
N265TW
Flight Type:
Survivors:
No
MSN:
265
YOM:
1979
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The crew was performing a flight from Texas and the aircraft was carrying a load consisting of six fuel drums according to a Campeche daily newspaper. The Learjet 25D was flying at a very low altitude, maybe in an attempt to land, when it crashed and burned in an open field located in Champotón, some 40 km south of Campeche. Both crew members were killed. Illegal flight suspected.

Crash of a Rockwell Aero Commander 500A in McDade: 1 killed

Date & Time: Nov 23, 2014 at 0945 LT
Operator:
Registration:
N14AV
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Tomball – Austin
MSN:
500-914-22
YOM:
1960
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
7075
Captain / Total hours on type:
168.00
Aircraft flight hours:
12859
Circumstances:
The airline transport pilot was conducting a cross-country repositioning flight. While en route to the destination airport, the pilot contacted air traffic control and stated that he was beginning to descend. No further radio transmissions were made by the pilot. Radar and GPS information showed, about the same time as the pilot's last transmission, the airplane's flightpath began descending in a westerly direction. The last recorded GPS point showed the airplane about 200 ft southwest of the initial impact point, 90 ft above ground level, and at a groundspeed of 66 knots. The airplane wreckage was located in an open field and impact signatures were consistent with a stall/spin, which had resulted in a near-vertical impact at a slow airspeed. The right propeller blades were found in the feathered position. Examination of the right engine found that the oil gauge housing extension was improperly secured to the oil gauge housing, which resulted in a loss of engine oil. Additionally, the examination revealed a hole in the right engine's crankcase, metal material in the oil sump, and signatures consistent with the lack of lubrication. Cockpit switches were positioned in accordance with the in-flight shutdown of the right engine. No anomalies were found with the left engine or airframe that would have precluded normal operation. Another pilot who had flown with the accident pilot reported that the pilot typically used the autopilot, and the autopilot system was found with the roll, heading, and pitch modes active. During the descent, no significant changes of heading were recorded, and the direction of travel before the stall was not optimal for the airplane to land before a fence line. It is likely that the autopilot was controlling the airplane's flightpath before the stall. Despite one operating engine, the pilot did not maintain adequate airspeed and exceeded the airplane's critical angle-of-attack (AOA), which resulted in an aerodynamic stall/spin. Correcting the last GPS recorded airspeed for prevailing wind, the airplane's indicated airspeed would have been about 72 knots, which is above the airplane's 0-bank stall speed, but an undetermined mount of bank would have been applied to maintain heading, which would have accelerated the stall speed. It could not be determined why the pilot did not maintain adequate airspeed or notify air traffic controller of an engine problem. Although a review of the pilot's medical records revealed that he had several historical medical conditions and the toxicology tests detected several sedating allergy medications in his system, it was inconclusive whether the medical conditions or medications impaired the pilot's ability to fly the airplane or if the pilot was incapacitated. It is also possible that the pilot was distracted by the loss of oil from the right engine and that this resulted in his failure to maintain adequate airspeed, his exceedance of the airplane's critical AOA, and a subsequent stall/spin; however, based on the available evidence, the investigation could not determine the reason for the pilot's lack of corrective actions.
Probable cause:
The pilot's failure to maintain adequate airspeed and his exceedance of the airplane's critical angle-of-attack for reasons that could not be determined based on the available evidence, which resulted in an aerodynamic stall/spin. Contributing to the accident was the improperly installed oil gauge housing extension, which resulted in a loss of oil quantity and right engine power.
Final Report:

Crash of a Fletcher FU-24-954 in Mount Linton

Date & Time: Nov 14, 2014 at 1300 LT
Type of aircraft:
Operator:
Registration:
ZK-EMN
Flight Phase:
Survivors:
Yes
MSN:
265
YOM:
1979
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The pilot was engaged in an agricultural spraying mission. In unknown circumstances, the single engine aircraft impacted terrain and came to rest against a small hill in Mount Linton. The aircraft was damaged beyond repair and the pilot, sole aboard, was seriously injured.

Crash of a Socata TBM-850 in Fayetteville

Date & Time: Oct 5, 2014 at 1255 LT
Type of aircraft:
Operator:
Registration:
N536EM
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Atlanta – Pine Mountain
MSN:
536
YOM:
2010
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4244
Captain / Total hours on type:
411.00
Aircraft flight hours:
719
Circumstances:
The private pilot was conducting a personal cross-country flight. The pilot reported that, during cruise flight at 6,000 ft mean sea level, he observed a crew alerting system oil pressure message, followed by a total loss of engine power. An air traffic controller provided vectors to a local airport; however, the pilot reported that the airplane would not reach the runway. He did not attempt to restart the engine. He feathered the propeller and placed the power lever to "idle" and the condition lever to "cut off." The pilot subsequently attempted a forced landing to a sports field with the gear and flaps retracted. The airplane collided with trees and the ground and then came to rest upright. Examination of the engine revealed that it displayed contact signatures to its internal components and evidence of ingested unburned organic debris, consistent with the engine likely being unpowered and the engine gas generator and power sections wind-milling at the time of impact. No evidence of any preimpact mechanical anomalies or malfunctions to any of the engine components was found that would have precluded normal operation. Recorded GPS flight track and systems data showed that the loss of engine power was preceded by about 5 minutes of flight on a constant heading and altitude with an excessive lateral g force of about 0.17 g and a bank angle between about 8 and 10 degrees, consistent with a side-slip flight condition. The airplane then entered a right turn with the autopilot engaged, and it lost power at the end of the turn. The data indicated that, even though the autopilot was engaged, the lateral g forces increased as the airplane leveled off and accelerated, indicating that the automatic rudder trim feature of the yaw damper system was not engaged. Given that the yaw damper system operated normally after the flight, it is likely that the pilot inadvertently and unknowingly disengaged the yaw damper during flight with the autopilot engaged. During a postaccident interview, the pilot stated that he was not aware of a side-slip condition before the loss of engine power. Although the fuel tank system was designed to prevent unporting of the fuel lines during momentary periods of uncoordinated flight, it was not intended to do so for extended periods of uncoordinated flight. Therefore, the fuel tank feed line likely unported during the prolonged uncoordinated flight, which resulted in the subsequent loss of engine power. If the pilot had recognized the side-slip condition, he could have returned to coordinated flight and prevented the engine power loss. Also, once the airplane returned to coordinated flight, an engine restart would have been possible.
Probable cause:
The pilot's inadvertent deactivation of the yaw damper in flight, which resulted in a prolonged side-slip condition that led to fuel starvation and the eventual total loss of engine power. Contributing to the accident was the pilot's failure to attempt to restart the engine.
Final Report:

Crash of a Beechcraft E90 King Air in Casigua El Cubo: 3 killed

Date & Time: Sep 19, 2014
Type of aircraft:
Operator:
Registration:
YV1537
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Anaco – Santa Bárbara del Zulia
MSN:
LW-309
YOM:
1979
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
En route from Anaco to Santa Bárbara del Zulia, the twin engine aircraft crashed in unknown circumstances by a wooded area located near Casigua El Cubo. The aircraft was destroyed by a post crash fire and all three occupants were killed. It is believed that the aircraft was engaged in an illegal contraband flight.