Crash of an Antonov AN-24RV in Cheboksary

Date & Time: Nov 5, 2000
Type of aircraft:
Registration:
RA-46499
Flight Phase:
Survivors:
Yes
MSN:
2 73 083 02
YOM:
1972
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
During the takeoff roll at Cheboksary Airport, after V1 speed, the crew decided to abort. Unable to stop within the remaining distance, the aircraft overran, lost its nose gear and came to rest 270 metres further. All occupants escaped uninjured while the aircraft was damaged beyond repair. At the time of the accident, the visibility was reduced to 350 metres due to foggy conditions.

Crash of a De Havilland DHC-6 Twin Otter 100 off Vancouver

Date & Time: Nov 1, 2000 at 1510 LT
Operator:
Registration:
C-GGAW
Flight Phase:
Survivors:
Yes
Schedule:
Vancouver - Victoria
MSN:
086
YOM:
1967
Flight number:
8O151
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
15
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4000
Captain / Total hours on type:
2500.00
Copilot / Total flying hours:
2000
Copilot / Total hours on type:
1650
Circumstances:
A de Havilland DHC-6-100 float-equipped Twin Otter (serial number 086), operated by West Coast Air Ltd., was on a regularly scheduled flight as Coast 608 from Vancouver Harbour water aerodrome, British Columbia, to Victoria Harbour water aerodrome. The flight departed at about 1510 Pacific standard time with two crew members and 15 passengers on board. Shortly after lift-off, there was a loud bang and a noise similar to gravel hitting the aircraft. Simultaneously, a flame emanated from the forward section of the No. 2 (right-hand) engine, and this engine completely lost propulsion. The aircraft altitude was estimated to be between 50 and 100 feet at the time. The aircraft struck the water about 25 seconds later in a nose-down, right wing-low attitude. The right-hand float and wing both detached from the fuselage at impact. The aircraft remained upright and partially submerged while the occupants evacuated the cabin through the main entrance door and the two pilot doors. They then congregated on top of the left wing and fuselage. Within minutes, several vessels, including a public transit SeaBus, arrived at the scene. The SeaBus deployed an inflatable raft for the occupants, and they were taken ashore by several vessels and transported to hospital for observation. There were no serious injuries. The aircraft subsequently sank. All of the wreckage was recovered within five days.
Probable cause:
Findings as to Causes and Contributing Factors:
1. A planetary gear disintegrated in the propeller reduction gearbox of the No. 2 engine and caused the engine drive shaft to disconnect from the propeller, resulting in a loss of propulsion from this engine.
2. The planetary gear oil strainer screen wires fractured by fatigue as a consequence of the installation at the last overhaul. This created an unsafe condition and it is most probable that the release of wire fragments and debris from this strainer screen subsequently initiated or contributed to distress of the planetary gear bearing sleeve and resulted in the disintegration of the planetary gear.
3. Although airspeed was above Vmc at the time of the power loss, the aircraft became progressively uncontrollable due to power on the remaining engine not being reduced to relieve the asymmetric thrust condition until impact was imminent.
Findings as to Risk:
1. The propeller reduction gearboxes were inspected in accordance with the West Coast Air maintenance control manual. These inspections exceeded requirements of the de Havilland Equalized Maintenance Maximum Availability program. Since the last inspection, 46 hours of flight time before the accident, did not reveal any anomaly, a risk remains of adverse developments with
resulting consequences occurring during the unmonitored period between inspections.
2. Regulations require the installation of engine oil chip detectors, but not the associated annunciator system on the DHC-6. Without an annunciator system, monitoring of engine oil contamination is limited to the frequency and thoroughness of maintenance inspections. An annunciator system would have provided a method of continuous monitoring and may have warned the crew of the impending problem.
3. Although regulations do not require the aircraft to be equipped with an auto-feather system, its presence may have assisted the flight crew in handling the sudden loss of power by reducing the drag created by a windmilling propeller.
4. Since most air taxi and commuter operators use their own aircraft rather than a simulator for pilot proficiency training, higher-risk emergency scenarios can only be practiced at altitude and discussed in the classroom. As a result, pilots do not gain the benefit of a realistic experience during training.
Other Findings:
1. The fact that the aircraft remained upright and floating in daylight conditions contributed to the successful evacuation of the cabin without injury and enabled about half of the passengers to locate and don their life vests.
2. The aircraft was at low altitude and low airspeed at the time of power loss. The selection of full flaps may have contributed to a single-engine, high-drag situation, making a successful landing difficult.
Final Report:

Crash of a Boeing 747-412 in Taipei: 83 killed

Date & Time: Oct 31, 2000 at 2318 LT
Type of aircraft:
Operator:
Registration:
9V-SPK
Flight Phase:
Survivors:
Yes
Schedule:
Singapore – Taipei – Los Angeles
MSN:
28023/1099
YOM:
1997
Flight number:
SQ006
Country:
Region:
Crew on board:
20
Crew fatalities:
Pax on board:
159
Pax fatalities:
Other fatalities:
Total fatalities:
83
Captain / Total flying hours:
11235
Captain / Total hours on type:
2017.00
Copilot / Total flying hours:
2442
Copilot / Total hours on type:
552
Aircraft flight hours:
18459
Aircraft flight cycles:
2274
Circumstances:
Singapore Airlines Flight 006 departed Singapore for a flight to Los Angeles via Taipei. Scheduled departure time at Taipei was 22:55. The flight left gate B-5 and taxied to taxiway NP, which ran parallel to runway 05L and 05R. The crew had been cleared for a runway 05L departure because runway 05R was closed because of construction work. CAA Taiwan had issued a NOTAM on Aug 31, 2000 indicating that part of runway 05R between Taxiway N4 and N5 was closed for construction between Sept. 13 to Nov. 22, 2000. Runway 05R was to have been converted and re-designated as Taxiway NC effective Nov. 1, 2000. After reaching the end of taxiway NP, SQ006 turned right into Taxiway N1 and immediately made a 180-degree turn to runway 05R. After approximately 6 second hold, SQ006 started its takeoff roll at 23:15:45. Weather conditions were very poor because of typhoon 'Xiang Sane' in the area. METAR at 23:20 included Wind 020 degrees at 36 knots gusting 56 knots, visibility - 600 meters, and heavy rainfall. On takeoff, 3.5 seconds after V1, the aircraft hit concrete barriers, excavators and other equipment on the runway. The plane crashed back onto the runway, breaking up and bursting into flames while sliding down the runway and crashing into other objects related to work being done on runway 05R. The aircraft wreckage was distributed along runway 05R beginning at about 4,080 feet from the runway threshold. The airplane broke into two main sections at about fuselage station 1560 and came to rest about 6,480 feet from the runway threshold.
Probable cause:
Findings related to probable causes:
- At the time of the accident, heavy rain and strong winds from typhoon "Xangsane" prevailed. At 2312:02 Taipei local time, the flight crewmembers of SQ006 received Runway Visual Range (RVR) 450 meters on Runway 05L from Automatic Terminal Information Service (ATIS) "Uniform". At 2315:22 Taipei local time, they received wind direction 020 degrees with a magnitude of 28 knots, gusting to 50 knots, together with the takeoff clearance issued by the local controller.
- On August 31, 2000, CAA of ROC issued a Notice to Airmen (NOTAM) A0606 indicating that a portion of the Runway 05R between Taxiway N4 and N5 was closed due to work in progress from September 13 to November 22, 2000. The flight crew of SQ006 was aware of the fact that a portion of Runway 05R was closed, and that Runway 05R was only available for taxi.
- The aircraft did not completely pass the Runway 05R threshold marking area and continue to taxi towards Runway 05L for the scheduled takeoff. Instead, it entered Runway 05R and CM-1 commenced the takeoff roll. CM-2 and CM-3 did not question CM-1's decision to take off.
- The flight crew did not review the taxi route in a manner sufficient to ensure they all understood that the route to Runway 05L included the need for the aircraft to pass Runway 05R, before taxiing onto Runway 05L.
- The flight crew had CKS Airport charts available when taxing from the parking bay to the departure runway; however, when the aircraft was turning from Taxiway NP to Taxiway NI and continued turning onto Runway 05R, none of the flight crewmembers verified the taxi route. As shown on the Jeppesen "20-9" CKS Airport chart, the taxi route to Runway 05L required that the aircraft make a 90-degree right turn from Taxiway NP and then taxi straight ahead on Taxiway NI, rather than making a continuous 180-degree turn onto Runway 05R. Further, none of the flight crewmembers confirmed orally which runway they had entered.
- CM-1's expectation that he was approaching the departure runway coupled with the saliency of the lights leading onto Runway 05R resulted in CM?1 allocating most of his attention to these centerline lights. He followed the green taxiway centerline lights and taxied onto Runway 05R.
- The moderate time pressure to take off before the inbound typhoon closed in around CKS Airport, and the condition of taking off in a strong crosswind, low visibility, and slippery runway subtly influenced the flight crew's decision?making ability and the ability to maintain situational awareness.
- On the night of the accident, the information available to the flight crew regarding the orientation of the aircraft on the airport was:
- CKS Airport navigation chart
- Aircraft heading references
- Runway and Taxiway signage and marking
- Taxiway NI centerline lights leading to Runway 05L
- Color of the centerline lights (green) on Runway 05R
- Runway 05R edge lights most likely not on
- Width difference between Runway 05L and Runway 05R
- Lighting configuration differences between Runway 05L and Runway 05R
- Para-Visual Display (PVD) showing aircraft not properly aligned with the Runway 05L localizer
- Primary Flight Display (PFD) information
The flight crew lost situational awareness and commenced takeoff from the wrong runway.
The Singapore Ministry of Transport (MOT) did not agree with the findings and released their own report. They conclude that the systems, procedures and facilities at the CKS Airport were seriously inadequate and that the accident could have been avoided if internationally-accepted precautionary measures had been in place at the Airport.
Final Report:

Crash of a Harbin Yunsunji Y-12 II in Sam Neua: 8 killed

Date & Time: Oct 19, 2000 at 1212 LT
Type of aircraft:
Operator:
Registration:
RDPL-34130
Survivors:
Yes
Site:
Schedule:
Vientiane – Sam Neua
MSN:
0086
YOM:
1994
Flight number:
QV703
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
15
Pax fatalities:
Other fatalities:
Total fatalities:
8
Circumstances:
While descending to Sam Neua Airport, the crew encountered poor weather conditions with limited visibility. Approaching in clouds, the aircraft struck the slope of a mountain located 12 km from the airport. Eight passengers were killed while nine other occupants were injured.
Probable cause:
Controlled flight into terrain after the crew descended too low in poor visibility. At the time of the accident, the aircraft deviated from the approach path from 4 to 6 km.

Crash of a Douglas DC-9-31 in Reynosa: 4 killed

Date & Time: Oct 6, 2000 at 1655 LT
Type of aircraft:
Operator:
Registration:
N936ML
Survivors:
Yes
Schedule:
Mexico City - Reynosa
MSN:
47501
YOM:
1970
Flight number:
AM250
Country:
Crew on board:
5
Crew fatalities:
Pax on board:
85
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
10184
Captain / Total hours on type:
701.00
Copilot / Total flying hours:
1764
Copilot / Total hours on type:
40
Aircraft flight hours:
74277
Circumstances:
Following an uneventful flight from Mexico City, the crew started the descent to Reynosa-General Lucio Blanco Airport and encountered poor weather conditions with heavy rain falls issued from the tropical storm 'Keith'. Following a wrong approach configuration, the aircraft was too high on the glide and approaching at an excessive speed. It landed too far down the wet runway 31 and was unable to stop within the remaining distance. It overran, lost its undercarriage, struck several houses, went down an embankment and came to rest in a canal. All 90 occupants were rescued, among them one passenger was slightly injured. On the ground, four people were killed.
Probable cause:
Long landing and contact, after a high approach with excessive speed as a result of a non-precision approach, on a waterlogged runway and in adverse weather conditions (discharge of CB's in the area), with the aircraft departing from the opposite runway threshold (13).
Final Report:

Crash of a PZL-Mielec AN-28 in Tigil

Date & Time: Sep 19, 2000
Type of aircraft:
Operator:
Registration:
RA-28950
Flight Phase:
Survivors:
Yes
Schedule:
Tigil – Petropavlovsk-Kamchatsky
MSN:
1AJ009-16
YOM:
1991
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
While taking off from a waterlogged and unpaved runway in Tigil, the crew decided to abort as the aircraft was unable to reach a sufficient speed. Despite the situation, the crew attempted a second takeoff manoeuvre during which control was lost. The aircraft deviated to the left, veered off runway and struck an embankment before coming to rest in a ditch. All 11 occupants escaped uninjured while the aircraft was damaged beyond repair.

Crash of a Cessna 208B Grand Caravan on Mt Arenal: 10 killed

Date & Time: Aug 26, 2000 at 1210 LT
Type of aircraft:
Operator:
Registration:
HP-1357APP
Flight Phase:
Survivors:
No
Site:
Schedule:
San Juan – La Fortuna – Tamarindo
MSN:
208-0709
YOM:
1998
Flight number:
RZ1644
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
10
Captain / Total flying hours:
2354
Copilot / Total flying hours:
350
Aircraft flight hours:
792
Circumstances:
The single engine airplane departed San Juan Airport at 1138LT on a flight to Tamarindo with an intermediate stop in La Fortuna on behalf of SANSA - Servicios Aéreos Nacionales. At La Fortuna Airport, a Japanese tourist was drop off and the aircraft took off at 1205LT. About five minutes after takeoff, while cruising in IMC conditions at an altitude of 5,380 feet, the aircraft struck the slope of the Arenal Volcano. The wreckage was found about 200 metres below the summit and all 10 occupants were killed.
Crew:
Karl Acevedo Neverman, pilot,
William Badilla Salazar, copilot.
Passengers:
Terry Pratt,
Silvia Rhissiner,
Catherine Shoep,
Steven Bohmer,
Helena Gutierrez-Bohmer,
Frank Consolazio,
Yudi Consolazio,
Cristopher Damia.
Probable cause:
Controlled flight into terrain after the crew continued under VFR mode in IMC conditions. The following findings were identified:
- The pilot's unsafe flying and failure to maintain adequate separation (vertical and horizontal) with mountainous terrain and not remain in VMC. Moreover, lack of timely corrective action by the crew allowed the aircraft to fly in a controlled manner and unnoticed into the ground.
- Loss of situational awareness and attention from the crew.
- Inadequate monitoring and enforcement by the pilot not flying.
- Lack of application or adherence to standard operating procedures established by SANSA.
- Using flight procedures not written or approved.
- Lack of culture regarding operational safety.

Crash of an Airbus A320-212 off Bahrain: 143 killed

Date & Time: Aug 23, 2000 at 1930 LT
Type of aircraft:
Operator:
Registration:
A4O-EK
Survivors:
No
Schedule:
Cairo - Bahrain - Muscat
MSN:
481
YOM:
1994
Flight number:
GF072
Country:
Region:
Crew on board:
8
Crew fatalities:
Pax on board:
135
Pax fatalities:
Other fatalities:
Total fatalities:
143
Captain / Total flying hours:
4416
Captain / Total hours on type:
1083.00
Copilot / Total flying hours:
608
Copilot / Total hours on type:
408
Aircraft flight hours:
17370
Aircraft flight cycles:
13990
Circumstances:
On 23 August 2000, at about 1930 local time, Gulf Air flight GF072, an Airbus A320-212, a Sultanate of Oman registered aircraft A4O-EK, crashed at sea at about 3 miles north-east of Bahrain International Airport. GF072 departed from Cairo International Airport, Egypt, with two pilots, six cabin crew and 135 passengers on board for Bahrain International Airport, Muharraq, Kingdom of Bahrain. GF072 was operating a regularly scheduled international passenger service flight under the Convention on International Civil Aviation and the provisions of the Sultanate of Oman Civil Aviation Regulations Part 121 and was on an instrument flight rules (IFR) flight plan. GF072 was cleared for a VOR/DME approach for Runway 12 at Bahrain. At about one nautical mile from the touch down and at an altitude of about 600 feet, the flight crew requested for a left hand orbit, which was approved by the air traffic control (ATC). Having flown the orbit beyond the extended centreline on a south-westerly heading, the captain decided to go-around. Observing the manoeuvre, the ATC offered the radar vectors, which the flight crew accepted. GF072 initiated a go-around, applied take-off/go-around thrust, and crossed the runway on a north-easterly heading with a shallow climb to about 1000 feet. As the aircraft rapidly accelerated, the master warning sounded for flap over-speed. A perceptual study, carried out as part of the investigation, indicated that during the go-around the flight crew probably experienced a form of spatial disorientation, which could have caused the captain to falsely perceive that the aircraft was ‘pitching up’. He responded by making a ‘nose-down’ input, and, as a result, the aircraft commenced to descend. The ground proximity warning system (GPWS) voice alarm sounded: “whoop, whoop pull-up …”. The GPWS warning was repeated every second for nine seconds, until the aircraft impacted the shallow sea. The aircraft was destroyed by impact forces, and all 143 persons on board were killed.
Probable cause:
The factors contributing to the above accident were identified as a combination of the individual and systemic issues. Any one of these factors, by itself, was insufficient to cause a breakdown of the safety system. Such factors may often remain undetected within a system for a considerable period of time. When these latent conditions combine with local events and environmental circumstances, such as individual factors contributed by “frontline” operators (e.g.: pilots or air traffic controllers) or environmental factors (e.g.: extreme weather conditions), a system failure, such as an accident, may occur.
The investigation showed that no single factor was responsible for the accident to GF072. The accident was the result of a fatal combination of many contributory factors, both at the individual and systemic levels. All of these factors must be addressed to prevent such an accident happening again.
(1) The individual factors particularly during the approach and final phases of the flight were:
(a) The captain did not adhere to a number of SOPs; such as: significantly higher than standard aircraft speeds during the descent and the first approach; not stabilising the approach on the correct approach path; performing an orbit, a non-standard manoeuvre, close to the runway at low altitude; not performing the correct go-around procedure; etc.
(b) In spite of a number of deviations from the standard flight parameters and profile, the first officer (PNF) did not call them out, or draw the attention of the captain to them, as required by SOP’s.
(c) A perceptual study indicated that during the go-around after the orbit, it appears that the flight crew experienced spatial disorientation, which could have caused the captain to perceive (falsely) that the aircraft was ‘pitching up’. He responded by making a ‘nose-down’ input, and as a result, the aircraft descended and flew into the shallow sea.
(d) Neither the captain nor the first officer perceived, or effectively responded to, the threat of increasing proximity to the ground, in spite of repeated hard GPWS warnings.
(2) The systemic factors, identified at the time of the above accident, which could have led to the above individual factors, were:
(a) Organisational factors (Gulf Air):
(i) A lack of training in CRM contributing to the flight crew not performing as an effective team in operating the aircraft.
(ii) Inadequacy in the airline's A320 training programmes, such as: adherence to SOPs, CFIT, and GPWS responses.
(iii) The airline’s flight data analysis system was not functioning satisfactorily, and the flight safety department had a number of deficiencies.
(iv) Cases of non-compliance, and inadequate or slow responses in taking corrective actions to rectify them, on the part of the airline in some critical regulatory areas, were identified during three years preceding the accident.
(b) Safety oversight factors:
A review of about three years preceding the accident indicated that despite intensive efforts, the DGCAM as a regulatory authority could not make the operator comply with some critical regulatory
requirements.
Final Report:

Crash of an Antonov AN-26B near Tshikapa: 27 killed

Date & Time: Aug 12, 2000
Type of aircraft:
Operator:
Registration:
9Q-CJI
Flight Phase:
Survivors:
No
Schedule:
Kinshasa – Tshikapa
MSN:
60 04
YOM:
1977
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
21
Pax fatalities:
Other fatalities:
Total fatalities:
27
Circumstances:
While approaching Tshikapa on a flight from Kinshasa, the crew decided to return to Kinshasa for unknown reasons. Shortly later, the aircraft crashed in unknown circumstances some 64 km northwest of Tshikapa. All 27 occupants were killed.

Crash of a Douglas DC-9 in Greensboro

Date & Time: Aug 8, 2000 at 1544 LT
Type of aircraft:
Operator:
Registration:
N838AT
Survivors:
Yes
Schedule:
Greensboro - Atlanta
MSN:
47442/524
YOM:
1970
Flight number:
FL913
Crew on board:
5
Crew fatalities:
Pax on board:
58
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
22000
Captain / Total hours on type:
15000.00
Copilot / Total flying hours:
8000
Copilot / Total hours on type:
2000
Circumstances:
Examination of the area of the fire origin revealed that relay R2-53, the left heat exchanger cooling fan relay, was severely heat damaged, as were R2-54 and the other relays in this area. However, the R2-53 relay also exhibited loose terminal studs and several holes that had burned through the relay housing that the other relays did not exhibit. The wire bundles that run immediately below the left and right heat exchanger cooling fans and the ground service tie relays exhibited heat damage to the wire insulation, with the greatest damage located just below the R2-53 relay. The unique damage observed on the R2-53 relay and the wire damage directly below it indicates that fire initiation was caused by an internal failure of the R2-53 relay. Disassembly of the relay revealed that the R2-53 relay had been repaired but not to the manufacturer's standards. According to the manufacturer, the damage to the relay housing was consistent with a phase-to-phase arc between terminals A2 and B2 of the relay. During the on-scene portion of the investigation, three of the four circuit breakers in the left heat exchanger cooling fan were found in the tripped position. To determine why only three of the four circuit breakers tripped, all four were submitted to the Materials Integrity Branch at Wright-Patterson Air Force Base, Dayton, Ohio, for further examination. The circuit breakers were visually examined and were subjected to an insulation resistance measurement, a contact resistance test, a voltage drop test, and a calibration test (which measured minimum and maximum ultimate trip times). Testing and examination determined that the circuit breaker that did not trip exhibited no anomalies that would prevent normal operation, met all specifications required for the selected tests, and operated properly during the calibration test. Although this circuit breaker appeared to have functioned properly during testing, the lab report noted that, as a thermal device, the circuit breaker is designed to trip when a sustained current overload exists and that it is possible during the event that intermittent arcing or a resistive short occurred or that the circuit opened before the breaker reached a temperature sufficient to trip the device.
Probable cause:
A phase-to-phase arc in the left heat exchanger cooling fan relay, which ignited the surrounding wire insulation and other combustible materials within the electrical power center panel. Contributing to the left heat exchanger fan relay malfunction was the unauthorized repair that was not to the manufacturer's standards and the circuit breakers' failure to recognize an arc-fault.
Final Report: