Crash of a Lockheed 12A Electra Junior in Pontiac: 1 killed

Date & Time: Aug 7, 1979 at 1336 LT
Type of aircraft:
Registration:
N36P
Survivors:
No
Schedule:
Pontiac - West Branch
MSN:
1254
YOM:
1938
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
6540
Captain / Total hours on type:
1846.00
Circumstances:
After takeoff from Pontiac-Oakland County Airport, while climbing, one of the engine failed. The pilot was cleared to return for an emergency landing and initiated a turn to the left when the airplane crashed into culvert storage area. The aircraft was destroyed and the pilot, sole on board, was killed.
Probable cause:
Engine malfunction during initial climb for undetermined reasons.
Final Report:

Crash of a Cessna 207A Skywagon in Nikiski: 1 killed

Date & Time: Aug 7, 1979 at 1110 LT
Operator:
Registration:
N6469H
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Nikiski - Kodiak
MSN:
207-0533
YOM:
1979
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
9500
Captain / Total hours on type:
2000.00
Circumstances:
After takeoff from Nikiski Airfield, the single engine airplane failed to gain height, struck trees and crashed in flames in a wooded area. A pilot was killed while the second occupant was seriously injured.
Probable cause:
Engine failure during initial climb and subsequent collision with trees due to powerplant failure for undetermined reasons. The following contributing factors were reported:
- Failed to see and avoid objects or obstructions,
- inadequate preflight preparation,
- Misused or failed to use flaps,
- Set and soft runway,
- Improperly loaded aircraft,
- High obstructions,
- Momentary power reduction,
- 340 lbs over MTOW.
Final Report:

Crash of a Beechcraft C90 King Air in Indianapolis: 1 killed

Date & Time: Aug 5, 1979 at 1750 LT
Type of aircraft:
Operator:
Registration:
N6040M
Flight Type:
Survivors:
Yes
Schedule:
Concordia - Indianapolis
MSN:
LJ-840
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
12463
Captain / Total hours on type:
30.00
Aircraft flight hours:
41
Circumstances:
On final approach to Indianapolis Airport, both engines failed due to fuel exhaustion. The pilot lost control of the airplane that struck trees and crashed. A passenger was killed while both other occupants were injured. The aircraft was destroyed.
Probable cause:
Engine failure on final approach and subsequent collision with trees due to inadequate preflight preparation. The following contributing factors were reported:
- Improper in-flight decisions,
- lack of familiarity with aircraft,
- Mismanagement of fuel,
- Fuel exhaustion,
- Powerplant- instruments: fuel quantity gauge, erratic,
- Complete engine failure both engines,
- Forced landing off airport on land,
- Power schedule pilot used exceeded max structural cruising speed, increasing fuel consumption rate by 100 lbs per hour.
Final Report:

Crash of a Cessna 421A Golden Eagle I in Norfolk

Date & Time: Aug 5, 1979 at 1630 LT
Type of aircraft:
Registration:
N3126K
Survivors:
Yes
Schedule:
Myrtle Beach - Farmingdale
MSN:
421A-0107
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8000
Circumstances:
En route from Myrtle Beach to Farmingdale, the pilot encountered engine problems, informed ATC about his situation and was vectored to Norfolk for an emergency landing. The aircraft descended from 8,000 to 3,000 feet when the pilot realized he could not reach Norfolk Airport. He attempted an emergency landing when the aircraft crash landed in an open field. Both occupants were seriously injured and the aircraft was destroyed.
Probable cause:
Engine failure during normal cruise due to piston rings failure. The following contributing factors were reported:
- Material failure,
- Failed to maintain flying speed,
- Improper in-flight decisions,
- Complete engine failure,
- Forced landing off airport on land,
- N° two cylinder piston failed,
- Pilot descended from 8,000 to 3,000 feet 12 miles from field with right engine shut down.
Final Report:

Crash of a Mitsubishi MU-2B-10 Marquise in Hays: 7 killed

Date & Time: Aug 3, 1979 at 2125 LT
Type of aircraft:
Registration:
N208MA
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Salina - Denver
MSN:
16
YOM:
1967
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
2168
Captain / Total hours on type:
140.00
Circumstances:
En route from Salina to Denver, the pilot informed ATC about an engine failure and elected to divert to the nearest airport. The airplane lost height and eventually stalled and crashed in Hays. The aircraft was destroyed and all seven occupants were killed.
Probable cause:
Engine failure during normal cruise and subsequent stall due to compressor assembly bearing failure. The following contributing factors were reported:
- Material failure,
- Improper in-flight decisions,
- Failed to maintain flying speed,
- Complete failure one engine,
- Forward main shaft bearing failed.
Final Report:

Crash of a Cessna 501 Citation I in Akron: 1 killed

Date & Time: Aug 2, 1979 at 1602 LT
Type of aircraft:
Registration:
N15NY
Flight Type:
Survivors:
Yes
Schedule:
Akron - Akron
MSN:
501-0110
YOM:
1979
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
428
Captain / Total hours on type:
6.00
Aircraft flight hours:
43
Circumstances:
About 1607 e.d.t., on August 2, 1979, a Cessna Citation piloted by Mr. Thurman L. Munson crashed short of runway 19 at the Akron-Canton Airport near Canton, Ohio. The pilot was practicing touch-and-go landings during a local flight with two passengers aboard. The aircraft first touched down in a relatively level, clear area about 870 feet short of the runway. The aircraft slid through a small clump of trees, hit a large stump, and came to rest on a road adjacent to the airport boundary fence. Fire erupted immediately after the aircraft came to rest. The two passengers escaped from the wreckage; the pilot was killed. Thurman Lee Munson, aged 32, an American Major League Baseball catcher, was killed.
Probable cause:
The pilot's failure to recognize the need for, and to take action to maintain, sufficient airspeed to prevent a stall into the ground during an attempted landing. The pilot also failed to recognize the need for timely and sufficient power application to prevent the stall during an approach conducted inadvertently without flaps extended. Contributing to the pilot's inability to recognize the problem and to take proper action was his failure to use the appropriate checklist, and his nonstandard pattern procedures which resulted in an abnormal approach profile.
Final Report:

Crash of a Lockheed 18-56-23 LodeStar in Brunswick

Date & Time: Jul 24, 1979 at 1600 LT
Type of aircraft:
Registration:
N33LM
Flight Type:
Survivors:
Yes
Schedule:
Rockmart - Brunswick
MSN:
2341
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
11500
Captain / Total hours on type:
85.00
Circumstances:
Upon landing at Brunswick-Glynco Jetport Airport, the twin engine airplane bounced. The gear collapsed and the airplane went out of control and came to rest on its belly. All three occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
Ground loop/swerve and subsequent gear collapsed upon landing due to improper recovery from bounced landing and improper operation of brakes and flight controls. The following contributing factors were reported:
- Overload failure,
- Pilot-in-command previously held commercial mel and agricultural operator certificates.
Final Report:

Crash of a Rockwell Aero Commander 560A in Pavilion: 1 killed

Date & Time: Jul 21, 1979 at 0905 LT
Operator:
Registration:
N2748B
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Pavilion - Pavilion
MSN:
560-0248
YOM:
1955
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4405
Captain / Total hours on type:
217.00
Circumstances:
The pilot, sole on board, was taking part to a local air show when, flying at low height, the airplane banked right and crashed following the failure of the right engine. The aircraft was destroyed and the pilot was killed.
Probable cause:
Engine failure and subsequent stall after the left engine failed due to valve assemblies failure. The following contributing factors were reported:
- Material failure,
- The pilot failed to maintain flying speed,
- High vegetation,
- Forced landing off airport on land,
- Exhaust valve, second cylinder on right engine failed.
Final Report:

Crash of a Douglas C-47B-50-DK off Honolulu: 2 killed

Date & Time: Jul 20, 1979 at 1930 LT
Registration:
N63250
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
San Jose - Honolulu
MSN:
17062/34329
YOM:
1945
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
8000
Circumstances:
While approaching Honolulu on a ferry flight from San jose, California, the crew declared an emergency via an auxiliary emergency system that all communication and navigation systems failed. Few minutes later, the airplane crashed into the ocean off Honolulu. SAR operations were initiated but eventually abandoned few days later as no trace of the aircraft nor the two crew members was found.
Probable cause:
Double engine failure in flight following a fuel exhaustion. The following contributing factors were reported:
- The crew became lost/disoriented,
- Failure of the communications and navigations equipment,
- Failure of the Loran receiver,
- Communications failure,
- Failure of both engines,
- Forced landing off airport on water,
- Aircraft not recovered,
- Pilot reported HF radio and Loran inoperative,
- Lost,
- No fuel.
Final Report:

Crash of a Piper PA-31-310 Navajo near Naples

Date & Time: Jul 20, 1979
Type of aircraft:
Registration:
N101MC
Flight Type:
Survivors:
Yes
MSN:
31-219
YOM:
1964
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
After being stolen for an illegal mission, the twin engine airplane crash landed near Naples. The pilot selected an unsuitable terrain and the gear collapsed upon landing. The aircraft was then destroyed by a deliberate fire.
Probable cause:
Gear collapsed upon landing after the pilot selected an unsuitable terrain. The following contributing factors were reported:
- Stolen aircraft,
- Illegal flight,
- Found on 20JUL1979,
- Destroyed by deliberate fire.
Final Report: