Crash of a Fairchild C-123K Provider near Bruce: 4 killed

Date & Time:
Type of aircraft:
Operator:
Registration:
54-0602
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Hurlburt Field - Hurlburt Field
MSN:
20051
YOM:
1954
Flight number:
Moose 09
Location:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The airplane departed Hultburt Field AFB at 0800LT on a training mission under call sign Moose 09. The assigned mission was a routine SEA serial spray training flight. The formation proceeded to a point 25 nm northwest of Panama City, Florida (the designated spray training area), arriving there at 08:35 CST. At this time a series of simulated defoliation runs were conducted over an open field. At approximately 08:50 CST Aircraft 54-0602 assumed the number three position in a right echelon formation for practice defoliation runs along a series of roads. At the completion of the first run the lead aircraft gave a command to place the aircraft in a "piggy back" formation, then climbed from 150 feet AGL to approximately 300 feet AGL and executed a 270 degree turn to the right. While in this turn the Number Three aircraft contacted the ground in a left wing low position, cartwheeled, immediately caught fire and was destroyed. The instructor pilot, two student pilots, and the flight engineer sustained fatal injuries.

Crash of a Lockheed P-3B-95-LO Orion at Moffett AFB

Date & Time:
Type of aircraft:
Operator:
Registration:
A9-296
Flight Type:
Survivors:
Yes
Schedule:
Moffett - Moffett
MSN:
5406
YOM:
1968
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was completing a local test flight on this new aircraft which should be delivered to the Royal Australian Air Force. Upon landing, one of the main landing gear collapsed and the airplane came to rest in flames. While all four crew members escaped uninjured, the aircraft was destroyed by fire.
Probable cause:
Undercarriage collapsed upon landing.

Crash of a De Havilland U-6A Beaver near Bent: 3 killed

Date & Time:
Type of aircraft:
Operator:
Flight Phase:
Survivors:
No
Site:
Schedule:
Holloman - Holloman
Location:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
The crew was searching for a test balloon when the single engine aircraft crashed in unknown circumstances in a mountainous area located six miles southeast of Bent. All three crew members were killed.

Crash of a Rockwell Aero Commander 560 in Dilley

Date & Time:
Operator:
Registration:
N855LB
Flight Type:
Survivors:
Yes
MSN:
560-176
YOM:
1954
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2100
Captain / Total hours on type:
500.00
Circumstances:
On final approach to Dilley Airpark, both engines stopped simultaneously. The pilot lost control of the airplane that stalled, struck trees and crashed in Hilltop, northeast of the airport. Both occupants were seriously injured and the aircraft was destroyed.
Probable cause:
Complete failure of both engines due to fuel exhaustion. Inadequate preflight preparation on part of the pilot who was inattentive to fuel supply.
Final Report:

Crash of a Boeing 727-22C in Chicago

Date & Time:
Type of aircraft:
Operator:
Registration:
N7425U
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Chicago - San Francisco
MSN:
19200/416
YOM:
1967
Flight number:
UA9963
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10500
Captain / Total hours on type:
1033.00
Copilot / Total flying hours:
1280
Copilot / Total hours on type:
135
Aircraft flight hours:
2208
Circumstances:
The takeoff warning horn sounded shortly after commencing takeoff from runway 09R. The takeoff was continued as the crew tried to figure out what caused the warning. The horn ceased prior to reaching rotate speed. The stick shaker came on and thrust was added, but the aircraft failed to climb and the captain elected to discontinue the takeoff. The 727 settled back to the macadam shoulder off the right side of the runway and struck a ditch, coming to rest 1,100 feet beyond the runway end and 300 feet right of the extended centreline. The aircraft was destroyed by a post crash fire and all three crew members were injured. The flaps had been set at 2° instead of takeoff range of 5°-25°.
Probable cause:
The failure of the crew to abort the takeoff after being warned of an unsafe takeoff condition.
Final Report:

Crash of a Convair CV-340-38 in Evansville

Date & Time:
Type of aircraft:
Operator:
Registration:
N4820C
Survivors:
Yes
MSN:
152
YOM:
1954
Crew on board:
3
Crew fatalities:
Pax on board:
39
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7000
Captain / Total hours on type:
2000.00
Circumstances:
En route, the crew informed ATC about the failure of the left engine and was cleared to divert to Evansville-Dress Airport for an emergency landing. On short final, the captain decided to make a go-around when the airplane stalled and crashed short of runway threshold. All 42 occupants were evacuated among them 10 were injured. The aircraft was considered as damaged beyond repair.
Probable cause:
Failure of the left engine in flight following the rupture of an exhaust valve in number 15 cylinder. The pilot lost control of the airplane when he started a single engine go-around and aborted.
Final Report:

Crash of a Beechcraft G18S in Weston: 7 killed

Date & Time:
Type of aircraft:
Registration:
N172S
Flight Phase:
Survivors:
No
Site:
MSN:
BA-541
YOM:
1960
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
6221
Captain / Total hours on type:
711.00
Circumstances:
While cruising under VFR mode in foggy conditions, the crew failed to realize his altitude was insufficient when the airplane struck the slope of a mountain shrouded in clouds and located in the region of Weston. The aircraft was destroyed and all seven occupants have been killed.
Probable cause:
The crew continued under VFR mode in adverse weather conditions and became lost and disoriented. The crew attempted an IFR flight with know defective directional gyro.
Final Report:

Crash of a Beechcraft E18S in Rapid City: 9 killed

Date & Time:
Type of aircraft:
Registration:
N3400
Survivors:
No
MSN:
BA-212
YOM:
1956
Crew on board:
1
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
10000
Captain / Total hours on type:
135.00
Circumstances:
On final approach to Rapid City Airport, the pilot encountered gusty winds and lost control of the airplane that crashed in a huge explosion in a field. All nine occupants were killed.
Probable cause:
Improper compensation for wind conditions on part of the pilot who failed to maintain flying speed. Inadequate preflight preparation snf unfavorable wind component were also reported. Improperly loaded aircraft was considered as a contributing factor. Gusting wind up to 20 knots exceeded rearward CofG limits.
Final Report:

Crash of a Dassault Falcon 20C in Parkersburg: 6 killed

Date & Time:
Type of aircraft:
Operator:
Registration:
N1846
Flight Type:
Survivors:
No
Schedule:
Parkersburg - Parkersburg
MSN:
47
YOM:
1966
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
12704
Captain / Total hours on type:
695.00
Circumstances:
The aircraft was involved in a local training flight at Parkersburg-Wood County Wilson Airport, carrying four passengers and two pilots who were conducting touch-and-go maneuvers. Following a circuit, the pilot-in-command landed on a contaminated runway (slush, snow and ice). After touchdown, he attempted to takeoff when control was lost. The airplane veered off runway and crashed in flames on a dirt bank. It was destroyed and all six occupants were killed.
Probable cause:
The pilot made touch and go landing to check braking action and after touchdown, allowed insufficient runway distance to execute a go around as he misjudged the distance available.
Final Report:

Crash of a De Havilland DH.104 Riley Dove off Chicago: 6 killed

Date & Time:
Type of aircraft:
Operator:
Registration:
N999NJ
Flight Phase:
Flight Type:
Survivors:
No
MSN:
04456
YOM:
1955
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
8600
Circumstances:
While flying off Chicago, the twin engine aircraft owned by E. H. Litchfield went out of control and crashed in unknown circumstances into Lake Michigan. Five bodies were found while one was missing. The wreckage was not found.
Probable cause:
Due to lack of evidences, it was not possible to determined the exact cause of the accident.
Final Report: