Crash of a Cessna 402B in Ocean Ridge

Date & Time: Jul 22, 2008 at 1350 LT
Type of aircraft:
Registration:
N3990C
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Lantana - Pompano Beach
MSN:
402B-0857
YOM:
1975
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1565
Aircraft flight hours:
7222
Circumstances:
The commercial pilot, who was also the former owner of the twin-engine airplane, stated that the purpose of the flight was to reposition the airplane to an airport approximately 22 miles south of the departure airport. Just prior to the flight, he purchased 10 gallons of fuel for each of the two main tanks. The pilot reported that about 5 minutes after takeoff, at an altitude of approximately 1,000 feet, he experienced a "loss of engine power." However, his three separate accounts of the event were inconsistent with respect to which engine had a problem, or the specific nature of the problem. The pilot reported that the airplane started to lose altitude "rapidly," and that he attempted to "wag the wings" in order to "get all the fuel to be useable." The airplane struck a building and terrain approximately 8 miles south of the departure airport. The pilot sustained serious injuries, but there was no fire. Damage to the left engine and propeller was consistent with the engine running at impact, and precluded an attempt to run the left engine in a test cell. Damage to the right engine and propeller was consistent with low or no power at impact. The right engine was subsequently successfully run in a test cell. No evidence of any pre-accident anomalies that could have contributed to the accident was noted with the airframe, engines, or propellers. The fuel selector valve placards did not accurately depict the fuel system configuration. The fuel quantity and its distribution in the tanks, either at the beginning of the flight or at the time of the accident, could not be determined.
Probable cause:
A partial loss of engine power due to fuel starvation. Contributing to the accident was the pilot’s decision to add only a limited amount of fuel prior to the flight, and the fuel selector valve placards' inaccurate depiction of the airplane fuel tank configuration.
Final Report:

Crash of a Piper PA-31-310 Navajo in Caracas: 6 killed

Date & Time: Apr 28, 2008 at 0955 LT
Type of aircraft:
Registration:
N6463L
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Caracas – Willemstad
MSN:
31-421
YOM:
1969
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
The twin engine aircraft departed Caracas-Maiquetía-Simón Bolívar Airport on a private flight to Willemstad-Hato Airport, Curaçao, with two passengers and one pilot on board. During initial climb, the pilot reported engine problems and was cleared for an immediate return when he lost control of the airplane that crashed onto several buildings located in the district of Catia La Mar, about 6 km short of runway 09 threshold. The aircraft burst into flames and was totally destroyed. All three occupants as well as three people on the ground were killed. Five other people were injured.

Crash of a Douglas DC-9-51 in Goma: 40 killed

Date & Time: Apr 15, 2008 at 1430 LT
Type of aircraft:
Operator:
Registration:
9Q-CHN
Flight Phase:
Survivors:
Yes
Site:
Schedule:
Goma – Kisangani
MSN:
47731/860
YOM:
1977
Location:
Region:
Crew on board:
8
Crew fatalities:
Pax on board:
86
Pax fatalities:
Other fatalities:
Total fatalities:
40
Circumstances:
During the takeoff roll from runway 18 at Goma Airport, the crew started the rotation but the aircraft failed to respond. The aircraft continued, overran and crashed in the Birere District, about 100 metres past the runway end, bursting into flames. Three passengers were killed as well as 37 people on the ground. All other occupants were injured. The aircraft was totally destroyed by impact forces and a post crash fire.
Probable cause:
It is possible that one of the engine or maybe both suffered a loss of power during takeoff after the aircraft passed through a puddle.

Crash of a Cessna 500 Citation I in Biggin Hill: 5 killed

Date & Time: Mar 30, 2008 at 1438 LT
Type of aircraft:
Registration:
VP-BGE
Flight Phase:
Survivors:
No
Site:
Schedule:
Biggin Hill – Pau
MSN:
500-0287
YOM:
1975
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
8278
Captain / Total hours on type:
18.00
Copilot / Total flying hours:
4533
Copilot / Total hours on type:
70
Aircraft flight hours:
5844
Aircraft flight cycles:
5352
Circumstances:
Pilot B arrived at Biggin Hill Airport, Kent, at about 1100 hrs for the planned flight to Pau, France. At about 1130 hrs he helped tow the aircraft from its overnight parking position on the Southern Apron to a nearby handling agent whose services were being used for the flight. A member of staff employed by the handling agent saw Pilot B carry out what was believed to be an external pre-flight check of the aircraft. Pilot B also asked another member of staff to provide a print out of the weather information for the flight. Pilot A arrived at about 1145 hrs and joined Pilot B at the aircraft. Witnesses described nothing unusual in either pilots’ demeanour. Three passengers arrived at the handling agent at about 1300 hrs and waited in a lounge whilst their bags were taken to the aircraft and loaded into the baggage hold in the nose. A member of the handling agency, who later took the passengers to the aircraft, reported that Pilot B met them outside the aircraft. After they had all boarded, the agent heard Pilot B say that he would give them a safety brief. Pilot B then closed the aircraft door. Pilot A called for start at 1317 hrs. He called for taxi at 1320 hrs and the aircraft was cleared to taxi to the holding point A1. No one could be identified as a witness to the aircraft’s start or subsequent taxi to the holding point. At 1331 hrs ATC cleared the aircraft to line up on Runway 21 and at 1332 hrs cleared it to take off. Both clearances were acknowledged by Pilot A. The takeoff was observed by the tower controller who stated that everything appeared normal. No transmissions were made between the aircraft and ATC until one minute after takeoff when, at 1334 hrs, the following exchange was made. Numerous witnesses reported seeing the aircraft at around this time flying over a built-up area, about 2 nm north-north-east of Biggin Hill Airport, where it was observed flying low, passing over playing fields and nearby houses. Witnesses reported that the aircraft was maintaining a normal flying attitude with some reporting that the landing gear was up and others that it was down. Some described seeing it adopt a nose-high attitude and banking away from the houses just before it crashed. Some witnesses stated that there was no engine noise coming from the aircraft whilst others stated that they became aware of the aircraft as it flew low overhead due to the loud noise it was making, as if the engines were at high thrust. Two witnesses described hearing the aircraft make a pulsing, intermittent noise. The location of witnesses and the description of the aircraft noise they heard are also shown in Figure 1. Having flown over several houses at an extremely low height the aircraft’s left wing clipped a house which bordered a small area of woodland. The aircraft then impacted the ground between this and another house and caught fire. There were no injuries to anyone on the ground but all those on board the aircraft were fatally injured.
Probable cause:
The following contributory factors were identified:
1. It is probable that a mechanical failure within the air cycle machine caused the vibration which led to the crew attempting to return to the departure airfield.
2. A missing rivet head on the left engine fuel shut-off lever may have led to an inadvertent shut-down of that engine.
3. Approximately 70 seconds prior to impact neither engine was producing any thrust.
4. A relight attempt on the second engine was probably started before the relit first engine had reached idle speed, resulting in insufficient time for enough thrust to be developed to arrest the aircraft’s rate of descent before ground impact.
Final Report:

Crash of a Learjet 35A in Campo de Marte: 8 killed

Date & Time: Nov 4, 2007 at 1410 LT
Type of aircraft:
Operator:
Registration:
PT-OVC
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Campo de Marte - Rio de Janeiro
MSN:
35A-399
YOM:
1981
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
8
Captain / Total flying hours:
10049
Captain / Total hours on type:
3749.00
Copilot / Total flying hours:
643
Copilot / Total hours on type:
125
Aircraft flight hours:
10583
Circumstances:
The aircraft was returning to its base in Rio de Janeiro-Santos Dumont following an ambulance flight to Campo de Marte AFB. Shortly after takeoff from runway 30, while climbing to an altitude of 1,400 feet, the aircraft rolled to the right to an angle of 90° then entered an uncontrolled descent and crashed onto several houses located on Bernardino de Sena Street, bursting into flames. Both pilots as well as six people on the ground were killed. Six others people were seriously injured.
Probable cause:
A possible loss of control during initial climb consecutive to a fuel imbalance. The following contributing factors were identified:
- Crew fatigue,
- Non-compliance with published procedures,
- Poor distribution of tasks prior to the flight and during the initial climb,
- Overconfidence on part of the crew,
- Poor flight preparation,
- Loss of situational awareness,
- Incorrect application of controls,
- The crew failed to follow the pre-takeoff checklist.
Final Report:

Crash of a Beechcraft B200 Super King Air in Bogotá: 7 killed

Date & Time: Oct 11, 2007 at 2022 LT
Registration:
HK-4422
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Bogotá – Leticia
MSN:
BB-377
YOM:
1978
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
4088
Captain / Total hours on type:
324.00
Copilot / Total flying hours:
2127
Copilot / Total hours on type:
202
Aircraft flight hours:
10934
Circumstances:
The twin engine aircraft departed Bogotá-El Dorado Airport runway 13L on an ambulance flight to Leticia, carrying three doctors and two pilots. Shortly after takeoff, during initial climb, the crew contacted ATC and declared an emergency. The aircraft rolled to the right then entered an uncontrolled descent and crashed onto several houses located in the Fontibón neighborhood, bursting into flames. All five occupants were killed as well as two people on the ground.
Probable cause:
The exact cause of the accident could not be determined.
Final Report:

Crash of an Antonov AN-26B in Kinshasa: 49 killed

Date & Time: Oct 4, 2007 at 1040 LT
Type of aircraft:
Operator:
Registration:
9Q-COS
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Kinshasa – Tshikapa – Kananga
MSN:
8807
YOM:
1979
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
17
Pax fatalities:
Other fatalities:
Total fatalities:
49
Circumstances:
After takeoff from Kinshasa-N'Djili Airport, while climbing, the right engine failed. The aircraft stalled, hit tree tops and crashed onto several houses located in Kingasani neighbourhood. A crew member survived while 21 other occupants and at least 28 people on ground were killed. The Ministry of Transport was sacked after the accident due to inability to reform all aviation problem existing in DRC. The present accident is the worst occurring in DRC since 8 January 1996 when an Antonov AN-32 crashed also in Kinshasa, killing 237 people.
Probable cause:
Failure of the right engine during initial climb for unknown reasons.

Crash of an Airbus A320-233 in São Paulo: 199 killed

Date & Time: Jul 17, 2007 at 1854 LT
Type of aircraft:
Operator:
Registration:
PR-MBK
Survivors:
No
Site:
Schedule:
Porto Alegre – São Paulo
MSN:
789
YOM:
1998
Flight number:
JJ3054
Country:
Crew on board:
6
Crew fatalities:
Pax on board:
181
Pax fatalities:
Other fatalities:
Total fatalities:
199
Captain / Total flying hours:
13654
Captain / Total hours on type:
2236.00
Copilot / Total flying hours:
14760
Copilot / Total hours on type:
237
Aircraft flight hours:
20000
Aircraft flight cycles:
9300
Circumstances:
On 17 July 2007, at 17:19 local time (20:19 UTC), the Airbus aircraft, model A320, registration PR-MBK, operating as flight JJ3054, departed from Porto Alegre (SBPA) destined to Congonhas Airport (SBSP) in São Paulo city, São Paulo State. There were a total of 187 souls on board the aircraft, being six active crew members and 181 passengers, including 2 infants and 5 extra crew members (not on duty). The weather prevailing along the route and at the destination was adverse, and the crew had to make a few deviations. Up to the moment of the landing, the flight occurred within the expected routine. The aircraft was operating with the number 2 engine reverser de-activated, in accordance with the Minimum Equipment List (MEL). According to information provided to the TWR by crews that had landed earlier, the active runway at Congonhas (35L) was wet and slippery. During the landing, at 18:54 local time (21:54 UTC), the crew noticed that the ground spoilers had not deflected, and the aircraft, which was not slowing down as expected, veered to the left, overran the left edge of the runway near the departure end, crossed over the Washington Luís Avenue, and collided with a building in which the cargo express service of the very operator (TAM Express) functioned, and with a fuel service station. All the persons on board perished. The accident also caused 12 fatalities on the ground among the people that were in the TAM Express building. The aircraft was completely destroyed as a result of the impact and of the raging fire, which lasted for several hours. The accident caused severe damage to the convenience shop area of the service station and to some vehicles that were parked there. The TAM Express building sustained structural damages that determined its demolition. The aircraft was completely destroyed.
Probable cause:
Human factors
1.1 Medical aspect
a. Pain - Undetermined
At a certain moment, during the approach, the PIC reported having a mild headache. Although it was not possible to verify which type of headache it was, or even to evaluate its intensity, it is possible that this trouble may have influenced his cognitive and psychomotor capabilities during the final moments of the flight, when the unpredictability of the situation demanded a higher effectiveness of performance. This factor was considered undetermined due to the impossibility of confirming its contribution in factual terms.

1.2 Operational aspect
a. Training - A contributor
The theoretical qualification of their pilots was founded on the exclusive use of computer interactive courses (CBT), which allowed a massive training, but did not ensure the quality of the training received. In addition, the formation of the SIC was restricted to the “Right Seat Certification”, something that proved insufficient for him to deal with the critical situation experienced after the landing. Lastly, there was a perception among the crews interviewed that the training through the years and on account of the high demand resulting from the company’s growth was being abbreviated.

b. Application of the commands - Undetermined
One of the hypotheses considered in this investigation was that the pilot may have attempted to perform a procedure no longer in force at the time of the accident for the landing with a pinned reverser. This procedure consisted in the receding of both levers to the “IDLE” position during the flare at about a 10-foot altitude, and, after touching down, in activating the only reverser available, maintaining the thrust lever of the other engine in the “IDLE” position.
This procedure, though being more efficient from a braking perspective, could induce the crew to making mistakes, as there were several reports of occurrences in which there was a wrong setting of the levers, motivating the manufacturer to establish a new procedure, months before the accident. Thus, there is a high probability that the PIC inadvertently left one of the thrust levers in the “CL” position, placing the other one first in “IDLE” and later in the “REV” position. This factor was considered undetermined due to the impossibility of confirming its contribution in factual terms.

c. Cockpit coordination - A contributor
Independently of the hypothesis considered, the monitoring of the flight at the landing was not appropriate, since the crew did not have perception of what was happening in the moments that preceded the impact. This loss of situational awareness hindered the adoption of an efficient and timely corrective action.

d. Forgetfulness by the pilot - Undetermined
It is possible that the pilot has inadvertently left one of the levers at the “CL” position, while trying to perform a procedure no longer in force for the operation with a pinned reverser. This factor was considered undetermined due to the impossibility of confirming its contribution in factual terms.

e. Flight indiscipline - Undetermined
The procedure prescribed for the operation with a pinned reverser had been modified by the manufacturer and, according to the FDR recordings, the procedure in force was known to the crew and executed by them on the leg that preceded the accident. However, as this procedure imposed an increase of up to 55 meters in the calculations of runway distance required for landing, it is possible that the PIC deliberately tried to perform adoption of a procedure no longer in force would characterize flight indiscipline. This factor was considered undetermined due to the impossibility of confirming its contribution in factual terms.

f. Influence from the environment - Undetermined
The operating conditions of the Congonhas runway, may have affected the crew’s performance from a psychological perspective, considering the state of anxiety that was present in the cockpit.
In addition, the lack of luminosity resulting from the operation at night time, associated with the size and color of the thrust levers may have hindered the verification of a contingent inappropriate positioning of those controls during the landing. This factor was considered undetermined due to the impossibility of confirming, in factual terms, the psychological influence of the runway operating conditions and/or lack of luminosity on the performance of the crew.

g. Judgment of pilotage - Undetermined
In view of all the operation scenario - the 55 meters added on account of the reverser procedure, the 2.4 extra tons of fuel on account of the tankering, the crowded aircraft, the pressure to proceed to Congonhas, the PIC’s physiological condition (headache), a SIC with little experience in the A-320 and in its autothrust system, the wet and slippery runway, the occurrences of the preceding days - there is a high probability that the PIC deliberately tried to perform the procedure no longer in force for the operation with a pinned reverser, in order to increase the braking efficiency, inadvertently leaving the number 2 engine thrust lever in the “CL” position. Considering this hypothesis, the diversion to an alternate airport would be desirable, instead of trying to perform a procedure that was not prescribed. This factor was considered undetermined due to the impossibility of confirming its contribution in factual terms.

h. Management planning - A contributor
At the time of the accident, the operator had a disproportional number of captains in comparison with the number of co-pilots, a fact that obliged the scheduling sector to form crews with 2 captains. Thus, although complying with the minimum requirements of the regulation in force, such a practice may have contributed to the creation of a climate of complacency in the cockpit of the JJ3054. Besides, the long experience of the SIC as a captain was not a guarantee of his competence in the co-pilot function - for which he had done only the “Right Seat Certification” training - and, added to his little experience in that aircraft, it contributed to the loss of situational awareness in the most critical moments of the flight.

i. Flight planning - Undetermined
Thus, considering the hypothesis that the PIC deliberately tried to perform the old procedure for a landing with a pinned reverser to increase the braking efficiency, it is possible that the use of that procedure was not appropriately prepared, something that could have favored the wrong positioning of the levers (according to the hypothesis mentioned above, it is possible that the PIC inadvertently left the nº2 engine thrust lever in the “CL” position.). The lack of a briefing for the descent in the CVR recording hindered the confirmation of a possible intention of applying the old procedure, no longer in force at the time. This factor was considered undetermined due to the impossibility of confirming its contribution in factual terms.

j. Little experience of the pilot - A contributor
Despite his long experience in commercial jets, the SIC possessed only about 200 flight hours in aircraft of the A320 type. Besides, his experience in the function of co-pilot was restricted to the “Right Seat Certification” training, which proved insufficient to deal with the emergency situation.

k. Management oversight - A contributor
The operator allowed the crew to be composed of two captains, with the occupant of the right-hand seat having done only the “Right Seat Certification” training. Besides, the lack of coordination between the several sectors of the company, especially between the sectors of operation and training, determined the lack of an appropriate monitoring of the processes and of the quality of the pilots’ professional formation.

Psychological aspect
a. Anxiety - Undetermined
The CVR recording allows to perceive that the PIC was showing anxiety in relation to the runway conditions for landing, and on two different occasions he asked the SIC to request from the TWR-SP the rain and runway conditions, and on one of them specifically, whether the runway was slippery. It is possible that the state of anxiety present in the PIC may have influenced the performance of the crew to some extent. This factor was considered undetermined due to the impossibility to confirm that this anxiety has effectively influenced the performance of the crew.

b. Perception error - A contributor
Although perceiving that the ground spoilers had not deflected, the pilots were not able to associate the non-deflection with the positioning of the thrust levers. In addition, there is a high probability that the pilots were led to believe that the lack of the expected deceleration after landing was a result of the conditions of operation with a wet runway, the influence of which, from a psychological aspect perspective in the field of individual variables, was perceived along the investigation.

c. Stress - Undetermined
The stress has effect on the cognitive level (diminution of the concentration, diminution of the response speed, degradation of the memory, etc.), emotional level (alteration of the characteristics of personality, weakening of the emotional control, lowering of the self-esteem, etc.), behavioral level (alterations of the sleep pattern, diminution of interests, verbal articulation problems, etc.), and physiological level (sudoresis, tachycardia, sleep pattern alterations, gastric and dermatologic symptoms, etc.). The presence of stress triggering stimuli was perceived, such as the state of anxiety on the part of the pilots, especially regarding the runway conditions, the cephalalgia of the PIC, the issues concerning the operation in Congonhas with a wet runway, the crowded aircraft and the inoperative reverser. However, it was not possible to determine whether those stimuli effectively led any of the two pilots to a high level of stress. This factor was considered undetermined due to the impossibility to confirm its contribution in factual terms.

d. Lack of perception - A contributor
Considering the hypothesis of a failure in the thrust control system, the contingent stimulus generated from the loss of resistance to the movement of the thrust levers may not have been perceived by the pilot(s), according to the CVR recordings. On the other hand, if one considers the hypothesis that the nº 2 engine thrust lever was inadvertently left in the “CL” position, while the pilots were trying to perform a procedure no longer in force, the characteristics of the autothrust system, which keep the levers motionless during the variations of thrust, in addition to the size and color of those control levers, hard to be observed on a night flight, were not sufficiently evident to be perceived by the pilots. This situation was aggravated by the lack of a warning device relative to the conflicting positioning of the thrust levers.

e. Loss of situational awareness - A contributor
Thus, no matter which hypothesis is considered, the loss of the situational awareness emerged as a result of the very lack of perception on the part of the pilots. In this sense, the automation of the aircraft, however complex, was not capable of providing the pilots with sufficiently clear and accurate stimuli, to the point of favoring their understanding of what was happening in the moments just after the landing in Congonhas.

f. Organizational climate - Undetermined
In relation to the crews of the company, the investigation identified the perception that there was a pressure on the part of the management against diversions, on account of the inconvenience they could arise for the passengers and for the company itself. If the pilots of the JJ3054 shared that perception, it is possible that this factor could have some influence on the pilot’s decision to proceed for the landing in Congonhas, in spite of his concern with the runway operating conditions. This factor was considered undetermined due to the impossibility to confirm its contribution in factual terms.

g. Regulation - A contributor
The regulatory organization, although having already considered the availability of the reversers as a requirement for the operation in Congonhas, at least since April 2006, such a requirement was only formalized as a norm in May 2008. The opportune regulation of this requisite would have prevented the aircraft from operating in Congonhas with a wet runway condition.

h. Training - Undetermined
In relation to the training, the investigation identified in the crews a perception that the company seemed to have reduced the contact hours applied to it, although in formal terms those contact hours had remained unaltered. In relation to crew professional formation, the investigation identified a tendency on the part of the company to reduce the number of hours assigned to training, which remained unaltered in formal terms. Moreover, the FDR recordings showed that, during the period in which the aircraft operated with the pinned reverser, 5 different types of landing procedures were performed by the various crews who operated it. This factor was considered undetermined due to the impossibility to confirm, in factual terms, that the crews’ perception of a shortening in the training processes being applied was consistent with reality and/or whether such alleged shortening effectively influenced the performance of the crew, contributing to the accident.

2 Material factors
a. Design - A contributor
It was verified that, for an A320 airplane proceeding to land, it is possible to place one of the thrust levers at the “REV” position and the other at “CL”, and no alerting device will advise the pilots in an efficient way. This situation may put the aircraft in a critical condition and, depending on the time it takes the crew to identify this configuration, and on the runway parameters, a catastrophic situation may occur. In the specific case of this accident, even with the aircraft on the ground (Weight on Wheels - WOW), with the number 1 engine thrust lever at the “REV” position, with the ground spoilers armed, with the autobrake selected, and with application of maximum braking pressure on the pedals, the power control system gave priority to the information that one of the levers was at “CL”, and this lever did not have any safety devices regarding a possible inadvertent setting.
Final Report:

Crash of a Cessna 340A in Chandler

Date & Time: Jun 1, 2007 at 1600 LT
Type of aircraft:
Registration:
N8688K
Flight Type:
Survivors:
Yes
Site:
Schedule:
Chandler - Chandler
MSN:
340A-0619
YOM:
1978
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2799
Captain / Total hours on type:
62.00
Aircraft flight hours:
4790
Circumstances:
While on downwind the airplane experienced a loss of engine power and collided with houses and other obstacles during a forced landing on a residential neighborhood street. The pilot stated that he took off to troubleshoot a landing gear anomaly. He departed the airport area to the south. He cycled the landing gear and upon getting questionable indications in the cockpit of gear position he requested another aircraft confirm his landing gear configuration. Once he got the confirmation that all three wheels were down he proceeded back to the airport. About 2 miles away and approximately 1,800 feet agl the right engine began to lose power. He troubleshot the engine by attempting a restart, cycling the fuel pump off then on, and selected the right auxiliary fuel tank. The right engine did regain some power. He had lost some altitude during the process of troubleshooting the engine. He raised the landing gear to reduce drag, and entered right hand traffic for runway 17. At this point the left engine lost power, the airplane turned left, and he entered a descent to help maintain airspeed. He put the left propeller in feather, and switched to a new fuel tank, but the engine did not regain power. He did not have any altitude to exchange for airspeed and steered the airplane towards a clear residential street. The airplane impacted the roofs of at least two houses before colliding with the street. The pilot egressed through the rear of the airplane. An FAA inspector that examined the airplane wreckage stated that there was very little evidence of fuel onboard the airplane. The pilot stated that the left engine had failed due to fuel starvation and that he had fuel onboard but it was not in the right places.
Probable cause:
Fuel starvation due to the pilot's failure to adequately manage and monitor his fuel supply.
Final Report:

Crash of a Cessna 525 CJ1 in Van Nuys: 2 killed

Date & Time: Jan 12, 2007 at 1107 LT
Type of aircraft:
Operator:
Registration:
N77215
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Van Nuys - Long Beach
MSN:
525-0149
YOM:
1996
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
38000
Captain / Total hours on type:
800.00
Aircraft flight hours:
3001
Circumstances:
Line personnel reported that as the airplane was being fueled, the second pilot loaded more than one bag in the left front baggage compartment. With fueling complete, line personnel saw the second pilot pull the front left baggage door down, but not lock or latch it. Witnesses near midfield of the 8,001-foot long runway, reported that the airplane was airborne, and the front left baggage door was closed. Witnesses near the end of the runway, reported that the airplane was about 200 feet above ground level (agl) and they noted that the front left baggage door was open and standing straight up. All of the witnesses reported that the airplane turned slightly left, leveled off, and was slow. The airplane began to descend, and the wings were slightly rocking before it stalled, broke right, and collided with the terrain. Investigators found no anomalies with the airframe or engines that would have precluded normal operation. The forward baggage doors' design incorporates a key lock in the lower center of each door, and two latches in the left and right bottom section of the doors. There are two hinges in the upper left and right sections of the door. The handles latched the door to the door frame in the fuselage. The key would be in the horizontal position in an unlocked condition, and in the vertical position in a locked condition. The front left baggage door was found within the main wreckage debris field and had sustained mechanical and thermal damage. The key lock was in the horizontal position. Several instances of a baggage door opening in flight have been recorded in Cessna Citation airplanes. In some cases, the door separated, and in others it remained attached. The crews of these other airplanes returned to the airport and landed successfully.
Probable cause:
The pilot's failure to maintain an adequate airspeed during the initial climb resulting in an inadvertent stall/spin. Contributing to the accident were the second pilots inadequate preflight, failure to properly secure the front baggage door, and the front left baggage door opening in flight, which likely distracted the first pilot.
Final Report: