Zone

Crash of a Cessna 340A in Chandler

Date & Time: Jun 1, 2007 at 1600 LT
Type of aircraft:
Registration:
N8688K
Flight Type:
Survivors:
Yes
Site:
Schedule:
Chandler - Chandler
MSN:
340A-0619
YOM:
1978
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2799
Captain / Total hours on type:
62.00
Aircraft flight hours:
4790
Circumstances:
While on downwind the airplane experienced a loss of engine power and collided with houses and other obstacles during a forced landing on a residential neighborhood street. The pilot stated that he took off to troubleshoot a landing gear anomaly. He departed the airport area to the south. He cycled the landing gear and upon getting questionable indications in the cockpit of gear position he requested another aircraft confirm his landing gear configuration. Once he got the confirmation that all three wheels were down he proceeded back to the airport. About 2 miles away and approximately 1,800 feet agl the right engine began to lose power. He troubleshot the engine by attempting a restart, cycling the fuel pump off then on, and selected the right auxiliary fuel tank. The right engine did regain some power. He had lost some altitude during the process of troubleshooting the engine. He raised the landing gear to reduce drag, and entered right hand traffic for runway 17. At this point the left engine lost power, the airplane turned left, and he entered a descent to help maintain airspeed. He put the left propeller in feather, and switched to a new fuel tank, but the engine did not regain power. He did not have any altitude to exchange for airspeed and steered the airplane towards a clear residential street. The airplane impacted the roofs of at least two houses before colliding with the street. The pilot egressed through the rear of the airplane. An FAA inspector that examined the airplane wreckage stated that there was very little evidence of fuel onboard the airplane. The pilot stated that the left engine had failed due to fuel starvation and that he had fuel onboard but it was not in the right places.
Probable cause:
Fuel starvation due to the pilot's failure to adequately manage and monitor his fuel supply.
Final Report:

Crash of a Douglas C-118A Liftmaster in San Manuel

Date & Time: Apr 28, 1984 at 1630 LT
Type of aircraft:
Registration:
N92860
Flight Type:
Survivors:
Yes
Schedule:
Saint Petersburg – Chandler
MSN:
44619/549
YOM:
1955
Crew on board:
3
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6983
Captain / Total hours on type:
3200.00
Circumstances:
The aircraft skidded off the departure end of the runway collapsing the landing gear in a ditch as it caught on fire. This aircraft was on a ferry flight and had several mechanical problems. Among these was the prop reversers which failed on landing. The anti-ice/de-ice systems failed to work properly which contributed to the need to land short of destination. The copilot reported that she did not check the anti-icing equipment on pre-flight. She was also not qualified to be a copilot on this flight. The airspeed indicators were malfunctioning during landing. The crew members all said that they knew the airspeed was much too high. The copilot said she could not understand how the pilot thought he could land at such a high speed. She also said he called for reverse and applied brakes too late in the rollout.
Probable cause:
Occurrence #1: overrun
Phase of operation: landing - roll
Findings
1. (f) weather condition - tailwind
2. (c) wrong runway - selected - pilot in command
3. (f) pressure induced by others - pilot in command
4. (f) propeller system/accessories,reversing system - failure,partial
5. (c) airspeed - excessive - pilot in command
6. (f) anti-ice/deice system,windshield - inoperative
7. (c) proper touchdown point - not attained - pilot in command
8. (c) operation with known deficiencies in equipment - performed - pilot in command
9. (f) precautionary landing - premature - pilot in command
10. (c) judgment - poor - pilot in command
11. (f) procedures/directives - not followed - pilot in command
----------
Occurrence #2: main gear collapsed
Phase of operation: landing - roll
Findings
12. (f) landing gear, main gear - overload
Final Report:

Crash of a Fairchild C-119L Flying Boxcar near Casa Grande: 4 killed

Date & Time: Jul 8, 1979 at 2100 LT
Operator:
Registration:
N1040E
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Chandler - Chandler
MSN:
11270
YOM:
1953
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The crew departed Chandler-Stellar Airpark on a local flight. En route, one of the engine failed. The pilot attempted an emergency landing when the airplane crashed in flames in an open field. The aircraft was destroyed and all four occupants were killed.
Probable cause:
Controlled collision with ground after pilot attempted an emergency landing due to engine problems. The following contributing factors were reported:
- Engine structure: master and connecting rods,
- Engine structure: piston, piston rings,
- Material failure,
- Intentional wheels-up landing,
- Complete failure of one engine,
- Forced landing off airport on land.
Final Report:

Crash of a Douglas C-54S Skymaster in Mesa

Date & Time: May 15, 1979 at 1455 LT
Type of aircraft:
Operator:
Registration:
N44905
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Mesa - Chandler
MSN:
22159
YOM:
1945
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
12127
Captain / Total hours on type:
4399.00
Circumstances:
During the takeoff roll at Mesa-Falcon Field Airport, the crew started the rotation but the aircraft did not liftoff. It overran, struck a 10 feet high dirt bank, crossed a road where it hit a truck and eventually came to rest in flames in an orange grove. Both pilots, en route to Chandler-Stellar Airpark on a test flight, were seriously injured and the aircraft was destroyed by fire.
Probable cause:
Collision with dirt bank on takeoff due to inadequate preflight preparation. The following contributing factors were reported:
- Failed to abort takeoff,
- Failed to use the checklist,
- Gust locks engaged.
Final Report: