Crash of a Cessna 650 Citation III in Caico Seco: 3 killed

Date & Time: Feb 18, 2008 at 1815 LT
Type of aircraft:
Operator:
Registration:
N385EM
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Valencia – Puerto Ordaz
MSN:
650-0145
YOM:
1987
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
The aircraft departed Valencia-Arturo Michelana Airport on a private flight to Puerto Ordaz, carrying one passenger and two pilots. While cruising at an altitude of 30,000 feet, the aircraft entered an uncontrolled descent and crashed in a near vertical attitude. The aircraft disintegrated on impact and all three occupants were killed.
Probable cause:
The copilot probably gave his place on board to a passenger without any qualification to operate the aircraft, moments after takeoff. During the en-route flight phase, a failure of the primary pitch trim system was simulated by the activation of the secondary system, which would have resulted in an abnormal operation of the system, followed by violent loss of altitude and over speed condition.

Crash of a Cessna 340 in Port Clinton: 4 killed

Date & Time: Jan 12, 2008 at 1239 LT
Type of aircraft:
Operator:
Registration:
N2637Y
Flight Type:
Survivors:
No
Schedule:
Mansfield - Port Clinton
MSN:
340-0013
YOM:
1971
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
1160
Captain / Total hours on type:
13.00
Aircraft flight hours:
6820
Circumstances:
During the landing approach, a witness saw the twin-engine airplane slow and stall. The airplane crashed short of the runway, in a residential backyard. An airport manager flew with the pilot 8 days before the accident. The manager reported that during his flight the pilot flew the approach and landing with the aural stall warning horn activated. The manager advised the pilot of the aural warning, however no corrective action was taken by the pilot during that flight. An on-scene investigation revealed no preimpact mechanical anomalies. The pilot had about 12.6 hours of flight time in the accident airplane, of which 7.7 hours were dual instruction. Due to the lack of any mechanical problems with the airplane, the pilot's minimal experience in twin-engine airplanes, and his history of flying the airplane too slow, it is probable that he allowed the airspeed to decay below a safe speed, and inadvertently stalled it.
Probable cause:
The pilot's failure to maintain sufficient airspeed to avoid a stall during the landing approach.
Final Report:

Crash of a Cessna 401 in Narsarsuaq

Date & Time: Jan 31, 2007
Type of aircraft:
Operator:
Registration:
N6274Q
Flight Type:
Survivors:
Yes
Schedule:
Goose Bay - Narsarsuaq
MSN:
401-0074
YOM:
1969
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
For unknown reasons, the twin engine aircraft made a wheels up landing at Narsarsuaq Airport and came to rest. Both pilots escaped uninjured while the aircraft was damaged beyond repair. They were completing a flight from Goose Bay. The exact date of the occurrence remains unknown, somewhere in January 2007.

Crash of a Learjet 25D in Sacramento

Date & Time: Oct 26, 2005 at 1825 LT
Type of aircraft:
Operator:
Registration:
N888DV
Flight Type:
Survivors:
Yes
Schedule:
Sacramento - Sacramento
MSN:
25-370
YOM:
1984
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
17500
Captain / Total hours on type:
1100.00
Copilot / Total flying hours:
20000
Copilot / Total hours on type:
70
Circumstances:
The crew landed with the landing gear in the retracted position. While the airplane was on the base leg of the traffic pattern, the pilot heard a helicopter pilot make a transmission over the common radio frequency. As he completed the before landing checklist the pilot searched for the helicopter that he heard over the radio. During the landing flare he realized something was amiss and looked down at the instrument panel. He noticed that the landing gear lights were illuminated red. Just prior to contacting the runway surface he reached for the landing gear handle and manipulated it in the down position. The airplane made a smooth touchdown with the landing gear in the retracted position. The pilot stated that he did not make the proper check for the gear extension due to the timing of the helicopter distraction. The pilot reported no preimpact mechanical malfunctions or failures with the airplane or engine, stating that the accident was the result of pilot error.
Probable cause:
The pilot's failure to extend the landing gear and to verify they were in the down and locked position prior to touchdown. A related factor was his diverted attention.
Final Report:

Crash of a Rockwell Grand Commander 690 in El Gallito: 3 killed

Date & Time: Jun 3, 2005
Operator:
Registration:
N572L
Flight Phase:
Flight Type:
Survivors:
No
Site:
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
The twin engine aircraft was completing an illegal flight from Colombia to the US with three people on board. While flying at low height, it collided with trees and crashed in a wooded and hilly terrain near El Gallito. The aircraft was destroyed and all three occupants were killed. On scene were found one ton of cocaine in several boxes, large sums of money and guns. The registration N572L was probably a false one.

Crash of a Piper PA-61P Aerostar (Ted Smith 601) in Wheeling

Date & Time: Dec 18, 2004 at 2215 LT
Operator:
Registration:
N60CF
Flight Type:
Survivors:
Yes
MSN:
61-0415-149
YOM:
1977
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The pilot attempted a night landing on a taxiway in front of the control tower, which was closed at the time. The airplane overran the end of the taxiway, rolled down an embankment and struck trees. The pilot, whose identity was not confirmed, was believed to have incurred minor injuries. He subsequently paid a passerby to take him to a local hotel, and after a night's rest, he left the area. Ownership of the airplane could not be determined due to a recent sale. Approximately 250 kilos of cocaine were found onboard the airplane. Further investigation was being conducted by federal authorities and local law enforcement.
Probable cause:
The pilot misjudged his distance/speed, and his intentional landing on an unsuitable taxiway
at night. A factor in the accident was the night light conditions.
Final Report:

Crash of a Socata TBM-700 in Dundee

Date & Time: Oct 24, 2003 at 1742 LT
Type of aircraft:
Operator:
Registration:
N700VA
Flight Type:
Survivors:
Yes
Schedule:
Edinburgh – Dundee
MSN:
233
YOM:
2002
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3170
Captain / Total hours on type:
65.00
Circumstances:
After an uneventful flight from Edinburgh the pilot made a visual approach to Runway 28 (landing distance available 1,400 metres) at Dundee. The pilot reported that the aircraft floated down the runway in the flare and bounced lightly on touchdown. During the bounce the aircraft initially yawed left and then rolled left in a normal pitch attitude with no stall warning. Full right rudder was applied but this was unable to correct the yaw. Power was applied to initiate a go-around, whilst maintaining full right rudder, but the pilot was unable to prevent the left wing from hitting the ground. This caused the aircraft to yaw rapidly to the left bringing one of its wheels into contact with a low wall. The pilot then reduced power and ditched in the River Tay, approximately 10 metres from the shore. The air traffic controllers on duty reported that the aircraft achieved a high nose attitude during the go-around before the left wing dropped and the aircraft veered to the left. The aircraft came to rest with the top of the fuselage out of the water and the pilot and passengers were able to evacuate though the main door and stand on the wing to await rescue by the airport's hovercraft. The hovercraft could only carry two passengers at a time thus the process was delayed resulting in the pilot and passengers suffering from mild hypothermia.
Final Report: