Crash of an Antonov AN-8RU in Kiev: 7 killed

Date & Time: Sep 16, 1964 at 1645 LT
Type of aircraft:
Operator:
Registration:
CCCP-55517
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Kiev - Kiev
MSN:
133470
Country:
Region:
Crew on board:
7
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
7
Circumstances:
The crew (pilots, technicians and engineers) were involved in a local test flight at Kiev-Gostomel Airport. The goal of the mission was to test the JATO propulsion system in case of an engine failure on the Antonov AN-8. For this test program, the aircraft was renamed AN-8RU version. Twenty seconds after takeoff, while climbing to a speed of 220 km/h, the JATO system was ignited. Six seconds later, once the speed of 264 km/h was reached, the left engine was voluntarily shut down. At this time, the crew was unable to feather the propeller that went into auto-rotation. The airplane banked left to a 70-80° angle then dove into the ground and crashed in a field located 1,850 meters past the runway end. The aircraft was totally destroyed and all seven crew members were killed.
Probable cause:
The exact cause of the accident could not be determined with certainty. However, the crew encountered difficulties, was unable to and/or forgot to feather the propeller on the left engine. This caused an asymmetric thrust and high drag which caused the aircraft to be uncontrollable and to crash.

Crash of a Lockheed L-1649 Starliner in Deer Valley

Date & Time: Sep 3, 1964
Type of aircraft:
Operator:
Registration:
LV-GLI
Flight Phase:
Flight Type:
MSN:
1008
YOM:
1957
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft was deliberately crashed on takeoff at Deer Valley Airport for a FAA experimental program. During the takeoff roll, the aircraft hit several obstacles and eventually crashed onto a hill, broken in three. Both wings and all four engine were sheared off at impact.
Special thanks to Chris Baird - www.arizonawrecks.com

Crash of a Beechcraft C-45F Expeditor in Kankakee

Date & Time: Aug 15, 1964 at 1045 LT
Type of aircraft:
Operator:
Registration:
N12068
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Kankakee - Kankakee
MSN:
6608
YOM:
1944
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7000
Captain / Total hours on type:
100.00
Circumstances:
The pilot, sole on board, was involved in a local test flight. Shortly after takeoff from Kankakee-Greater Kankakee Airport, while climbing, both engines failed simultaneously. The pilot reduced his altitude and was able to complete an emergency belly landing in a field. The airplane slid for several yards and came to rest. The pilot was unhurt while the aircraft was damaged beyond repair.
Probable cause:
Failure of both engines due to a fuel starvation.
Final Report:

Crash of a Douglas DC-7 in Washington DC

Date & Time: Jul 30, 1964 at 2102 LT
Type of aircraft:
Operator:
Registration:
N464
Flight Type:
Survivors:
Yes
Schedule:
Washington DC - Washington DC
MSN:
44127
YOM:
1953
Crew on board:
3
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
14375
Captain / Total hours on type:
260.00
Circumstances:
The crew was completing a local test flight at Washington-Dulles Airport. Upon landing, the nose gear collapsed and the airplane slid for several yards before coming to rest. All eight occupants were uninjured while the aircraft was considered as damaged beyond repair.
Probable cause:
The crew failed to maintain directional control and the pilot-in-command made an inadequate supervision of flight.
Final Report:

Crash of a Learjet 23 in Wichita

Date & Time: Jun 4, 1964 at 0800 LT
Type of aircraft:
Operator:
Registration:
N801L
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Wichita - Wichita
MSN:
23-001
YOM:
1963
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5700
Captain / Total hours on type:
30.00
Aircraft flight hours:
194
Aircraft flight cycles:
167
Circumstances:
The crew was engaged in a local test flight at Wichita Airport on this first model of the Lear 23. At liftoff, the airplane encountered difficulties to gain height. Out of control, it struck the ground, rolled for several yards and came to rest in flames in a wasteland. Both pilots were seriously injured and the aircraft was destroyed.
Probable cause:
Inadequate pre-flight preparation and/or planning on part of the flying crew who failed to use or incorrectly used miscellaneous equipment. It was determined that during a test flight, while simulating a failure of the left engine, the crew attempted to takeoff with spoilers extended.
Final Report:

Crash of a Douglas DC-7 in Deer Valley

Date & Time: Apr 24, 1964
Type of aircraft:
Operator:
Registration:
N68N
Flight Phase:
Flight Type:
Site:
MSN:
44275/496
YOM:
1954
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft was voluntarily crashed by FAA for experimental purposes. The 'accident' occurred on takeoff from Deer Valley, at a speed of 140 knots, when the aircraft hit a hill and disintegrated. There were no occupants on board.
Thanks to Chris Baird - www.arizonawrecks.com

Crash of a Douglas C-47A-25-DK in Addis Ababa

Date & Time: Nov 30, 1963 at 1433 LT
Operator:
Registration:
ET-AAT
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Addis Ababa - Addis Ababa
MSN:
13483
YOM:
1944
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
18245
Circumstances:
The crew was engaged in a local post-maintenance test flight. At liftoff, the airplane banked left, struck the ground and came to rest. All three crew members were uninjured while the aircraft was damaged beyond repair.
Probable cause:
It was determined that the loss of control was the consequence of a poor maintenance check on part of the company technicians who wrongly reconnected the ailerons cables prior to the test flight.

Crash of a BAc 111-200AB in Chicklade: 7 killed

Date & Time: Oct 22, 1963 at 1040 LT
Type of aircraft:
Operator:
Registration:
G-ASHG
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Wisley - Wisley
MSN:
001
YOM:
1963
Region:
Crew on board:
7
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
5385
Captain / Total hours on type:
78.00
Copilot / Total flying hours:
9648
Aircraft flight hours:
81
Aircraft flight cycles:
52
Circumstances:
The aircraft took off at 1017 hours GMT from runway 10, at Wisley Aerodrome on its fifty third test flight. It was to carry out stalling tests in all configurations with the centre of gravity at 0.38 SMC (standard mean chord), the furthest aft limit for which the aircraft had then been cleared. Based on the radio-telephony conversations recorded in the Wisley Tower and the flight recorders carried aboard the aircraft, the flight was reconstructed. Following take-off the aircraft climbed in visual meteorological conditions on a westerly heading to 17 000 ft while monitored by Wisley radar. At 1026 the co-pilot reported that they were about to commence tests at flight level 170. By 1035, four stalls had been completed with the undercarriage and flaps up. The co-pilot acknowledged a fix from Wisley at 1036 hours and nothing further was heard from the aircraft. The flaps were then lowered to to investigate the stalling characteristics in this configuration. The stall was initiated about two minutes after the last contact, when the aircraft was between 15 000 and 16 000 ft. Approach to the stall appears to have been normal. When attempting recovery, the elevators responded initially to the control movement but subsequently floated to the fully up position in spite of a large push force on the control column. The aircraft then descended in a substantially horizontal fore and aft attitude at about 180 ft/sec (54 meters per sec). During the descent it banked twice to the right and once to the left and at one stage the engines were opened up to full power. This action resulted in a large nose-up pitch which was followed by a pitch down when power was taken off. The aircraft then assumed the substantially horizontal attitude in which it made impact with the ground. The final portion of the flight was observed by numerous eye witnesses who commented on the low level of engine noise and a sharp report from the aircraft which was heard while it was in the air. The aircraft had approached from the southwest, in a stable stalled condition, and crashed at about 1040 hours in a flat attitude. Following impact, the aircraft moved forward about 70 ft and some 15 ft to the right before coming to rest. It exploded and caught fire. All seven crew members, four engineers and three test pilots, were killed.
Probable cause:
The nose-down pitching moment (elevator neutral) just beyond the stall was insufficient to rotate the aeroplane at the rate required to counteract the increase of incidence due to the g-break. During the fifth stall the angle of incidence reached a value at which the elevator effectiveness was insufficient to effect recovery. During a stalling test the aircraft entered a stable stalled condition recovery from which was impossible.
Final Report:

Crash of a Vickers 651 Valetta C.1 in London-Gatwick

Date & Time: Sep 21, 1963
Type of aircraft:
Operator:
Registration:
G-APKR
Flight Type:
Survivors:
Yes
Schedule:
London - London
MSN:
338
YOM:
1949
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
After a flight of some two hours, made for the purpose of testing radio navigation equipment, the aircraft returned to London-Gatwick Airport, U.K.. Before, and during, the flight, undercarriage operation was normal, as was the functioning of the undercarriage light and horn warning system. During the approach, the undercarriage extended normally, and the green lights indicated that it was locked down. Some 50 yards after touch down, the aircraft began to sink on the starboard side and the captain noticed that the starboard green light was no longer showing. There were, however, no reds, and the horn was not sounding. The starboard main undercarriage leg eventually retracted and the aircraft swung off the runway to the right, on to the grass.

Crash of a PZL-Mielec MD-12 in Białobrzegi: 5 killed

Date & Time: Sep 17, 1963
Type of aircraft:
Operator:
Registration:
SP-PAL
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Warsaw - Warsaw
MSN:
1
YOM:
1959
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
The crew departed the WSK-Okęcie factory at Warsaw-Okęcie Airport for a test flight on this first prototype built on 21 of July 1959. The goal of the mission was to measure the pressure distribution on the hull in order to select the optimal position of the static pressure sensor. En route, in unknown circumstances, control was lost and the airplane crashed in a field, killing all five crew members.
Probable cause:
Flutter of tail control surfaces caused the plane to crash.