Crash of a Piper PA-31-350 Navajo Chieftain near Lake Tiberias

Date & Time: May 2, 1976
Registration:
4X-CCA
Flight Phase:
Survivors:
Yes
MSN:
31-7405140
YOM:
1974
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
En route, the pilot informed ATC that he lost a flap and elected to make an emergency landing. The twin engine airplane crash landed north of Lake Tiberias (Sea of Galilee) and was damaged beyond repair. All occupants escaped with no or minor injuries.

Crash of a Boeing 727-95 in Charlotte Amalie: 37 killed

Date & Time: Apr 27, 1976 at 1510 LT
Type of aircraft:
Operator:
Registration:
N1963
Survivors:
Yes
Schedule:
Providence - New York - Charlotte Amalie
MSN:
19837/499
YOM:
1967
Flight number:
AA625
Crew on board:
7
Crew fatalities:
Pax on board:
81
Pax fatalities:
Other fatalities:
Total fatalities:
37
Captain / Total flying hours:
22225
Captain / Total hours on type:
10000.00
Copilot / Total flying hours:
8000
Copilot / Total hours on type:
2500
Aircraft flight hours:
21926
Circumstances:
American Airlines Flight 625 was a scheduled flight from Providence Airport (PVD) to St.Thomas (STT) on the U.S Virgin Islands with an intermediate stop in New York (JFK). The Boeing 727 departed New York at 12:00 AST. On approach to St. Thomas, at 15:04, the flight crew cancelled their IFR flight plan and proceeded VFR. The captain elected to use the runway 09 ILS for vertical guidance. The glide slope was intercepted at 1500 feet msl (flaps 15° and at a 160 KIAS airspeed). The flaps were lowered to 25 and later to 30 degrees. The company prescribed 40 degrees was never selected. The speed was still 10 KIAS above Vref when the aircraft passed the threshold at an estimated altitude of 30-40 feet. At 1000 feet down the runway, while initiating the flare, turbulence caused the right wing to drop. The wings were leveled and the aircraft floated a while until touchdown 2200-2300 feet down the runway. The captain decided that the aircraft couldn't be stopped on the remaining runway. He immediately initiated a go-around. Because of the absence of any sensation either of power being applied or of aircraft acceleration, the throttles were closed again. The aircraft, in a 11 degree nose up attitude, ran off the runway and struck a localizer antenna. The right wingtip clipped a hillside just south of the antenna and the aircraft continued, hit an embankment, became airborne and contacted the ground on the opposite side of the perimeter road. The aircraft continued and came to rest 83 feet past the perimeter road, bursting into flames.
Probable cause:
The captain's actions and his judgment in initiating a go-around maneuver with insufficient runway remaining after a long touchdown. The long touchdown is attributed to a deviation from prescribed landing techniques and an encounter with an adverse wind condition, common at the airport. The non-availability of information about the aircraft's go-around performance capabilities may have been a factor in the captain's abortive attempt to go-around a long landing.
Final Report:

Crash of a Cessna 207 Skywagon near Anaktuvuk Pass: 5 killed

Date & Time: Apr 27, 1976 at 1115 LT
Operator:
Registration:
N1707U
Flight Phase:
Survivors:
No
Site:
Schedule:
Anaktuvuk Pass - Bettles
MSN:
207-0307
YOM:
1975
Flight number:
FTA528
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
1744
Captain / Total hours on type:
35.00
Circumstances:
Few minutes after it departed Anaktuvuk Pass Airstrip, while cruising in poor weather conditions, the single engine airplane struck the ground and crashed. The aircraft was destroyed and all five occupants were killed. The flight was completed on behalf of Wien Air Alaska.
Probable cause:
Controlled flight into terrain during normal cruise after the pilot initiated flight in adverse weather conditions. The following contributing factors were reported:
- Low ceiling,
- Snow,
- Whiteout conditions,
- Weather slightly worse than forecast,
- Overcast,
- Visibility 1/2 mile or less,
- Blowing snow,
- Weather conditions below minimus,
- The pilot had just flown thru same weather.
Final Report:

Crash of a PZL-Mielec AN-2R in Tula

Date & Time: Apr 22, 1976
Type of aircraft:
Operator:
Registration:
CCCP-01626
Flight Phase:
Survivors:
Yes
MSN:
1G82-20
YOM:
1967
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
En route, the pilot made a mistake in handling the fuel system, causing the engine to flame out. The aircraft crash landed in a field near Tula and was damaged beyond repair. There were no casualties.
Probable cause:
Pilot error.

Crash of a Beechcraft B60 Duke in Palm Desert: 6 killed

Date & Time: Apr 15, 1976 at 1455 LT
Type of aircraft:
Operator:
Registration:
N37D
Flight Phase:
Survivors:
No
Schedule:
San Diego – Palm Springs
MSN:
P-335
YOM:
1975
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
4900
Captain / Total hours on type:
38.00
Circumstances:
En route from San Diego to Palm Springs, weather conditions deteriorated and the twin engine airplane entered a thunderstorm area with severe turbulences and strong winds. The right empennage assembly and the right outboard wing panel failed in flight, causing the airplane to enter an uncontrolled descent and to crash in flames near Palm Desert. The aircraft was destroyed and all six occupants were killed.
Probable cause:
Airframe failure in flight and uncontrolled descent after the pilot exceeded the designed stress limits of the aircraft. The following contributing factors were reported:
- Windshear,
- Turbulences associated with clouds and thunderstorms,
- Overload failure,
- Continued VFR flight in adverse weather conditions,
- Separation in flight,
- Weather slightly worse than forecast,
- Gusts 80 knots,
- Severe turbulence was reported in area.
Final Report:

Crash of a Grumman G-21A Goose off Santa Catalina Island

Date & Time: Apr 10, 1976 at 1620 LT
Type of aircraft:
Operator:
Registration:
N18CS
Flight Phase:
Survivors:
Yes
Schedule:
Camp Fox - San Pedro
MSN:
B059
YOM:
1944
Crew on board:
1
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
11517
Captain / Total hours on type:
1376.00
Circumstances:
After takeoff from Camp Fox (Santa Catalina Island), while cruising at low height, the left engine failed. The pilot elected to make an emergency landing but unstable, the seaplane struck the water surface, lost its left float and came to rest upside down. All 10 occupants were quickly rescued while the aircraft sank and was not recovered.
Probable cause:
Powerplant failure for undetermined reasons. The following contributing factors were reported:
- Improper in-flight decisions,
- Failed to follow approved procedures,
- Improper operation of flight controls,
- Improper emergency procedures,
- Incorrect trim setting,
- Left engine lost power,
- Did not feather left propeller,
- Un maintain altitude,
- Landed cross swell,
- Float separated,
- Sank in ocean.
Final Report:

Crash of a Boeing 727-81 in Ketchikan: 1 killed

Date & Time: Apr 5, 1976 at 0819 LT
Type of aircraft:
Operator:
Registration:
N124AS
Survivors:
Yes
Schedule:
Anchorage - Juneau - Ketchikan - Seattle
MSN:
18821/124
YOM:
1965
Flight number:
AS060
Crew on board:
7
Crew fatalities:
Pax on board:
43
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
19813
Captain / Total hours on type:
2140.00
Copilot / Total flying hours:
3193
Copilot / Total hours on type:
1980
Aircraft flight hours:
25360
Circumstances:
About 0738LT on April 5, 1976, Alaska Airlines, Inc., Flight 60, a B-727-81, N124AS, departed Juneau, Alaska, on a regularly scheduled passenger flight to Seattle, Washington; an en route stop was scheduled for Ketchikan International Airport, Ketchikan, Alaska. There were 43 passengers and a crew of 7 on board. Anchorage air route traffic control center (ARTCC) cleared Flight 60 on an instrument flight rules (IFR) flight plan to the Ketchikan International Airport; the flight was routine en route. At 0805, Anchorage ARTCC cleared Flight 60 for an approach to runway 11 at Ketchikan. At 0807, the flight was 30 DME miles from the airport. At 0811, Flight 60 reported out of 10,000 feet and was cleared to contact Ketchikan Flight Service Station (FSS); the FSS advised the flight that the 0805 weather was: ceiling 800 ft., obscured, visibility 2 mi, light snow, fog, wind 330° at 5 kt. The FSS also advised the flight that braking action on runway 11 was poor; this report was based on braking tests performed by the airport manager. The captain testified that he did not recall hearing the braking condition report. Upon receipt of the clearance, the crew of Flight 60 began an ILS approach to Ketchikan. Near the 17-mile DME fix, as the flight descended through 4,000 feet, the crew acquired visual contact with the ground and water. As the flight approached Guard Island, the captain had the Island in sight and decided to abandon the ILS approach and to continue the approach visually. The captain testified that he established a 'visual glide slope of my own' at an altitude of about 1,000 feet, and stated that his eyes were '... the most reliable thing I have.' Visual contact with the approach lights was established about 2 miles from the runway threshold. The airport was visible shortly thereafter. The captain did not recall the airspeed at touchdown, but estimated that he touched down about 1,500 feet past the threshold of runway 11. He also testified that he did not see the yellow, 1,000-foot markers on the runway; he further testified that the runway '... was just wet.' A passenger on Flight 60, who was seated in seat 5A (just forward of the wing's leading edge), stated that the yellow runway marks were visible to him. The first officer has no recollection of the sequence of events leading to the accident; however, the second officer testified that airspeeds and descent rates were called out during the last 1,000 feet. The captain could not recall the flap setting either on approach or at touchdown. However, the second officer testified that after the landing gear was extended the first officer remarked, 'We're high,' and lowered the flaps from 30° to 40°. None of the cockpit crew remembered the airspeeds, descent rates, or altitudes of the aircraft during the approach and touchdown. Reference speed was calculated to be 117 kns with 40° flaps and 121 kns with 30° flaps. The captain testified that after touchdown he deployed the ground spoilers, reversed the engines, and applied the wheel brakes. Upon discovering that the braking action was poor, he decided to execute a go-around. He retracted the ground spoilers, called for 25° flaps, and attempted to obtain takeoff thrust. The thrust reverser mechanism did not disengage fully and the forward thrust could not be obtained. He then applied full reversing and quickly moved the thrust levers to 'idle.' This attempt to obtain forward thrust also was not successful. The captain then reapplied reverse thrust and again deployed the ground spoilers in an attempt to slow the aircraft. When he realized that the aircraft could not be stopped on the runway, he turned the aircraft to the right, raised the nose, and passed over a gully and a service road beyond the departure end of the runway. The aircraft came to rest in a ravine, 700 feet past the departure end of runway 11 and 125 feet to the right of the runway centerline. Flight attendants reported nothing unusual about the approach and touchdown, except for the relatively short time between the illumination of the no-smoking sign and the touchdown. The two flight attendants assigned to the rear jumpseats and the attendant assigned to the forward jumpseat did not have sufficient time to reach their assigned seats and had to sit in passenger seats. None of the flight attendants felt the aircraft decelerate or heard normal reverse thrust. Many passengers anticipated the accident because of the high speed of the aircraft after touchdown and the lack of deceleration. Two ground witnesses, who are also pilots, saw the aircraft when it was at an altitude of 500 to 700 feet and in level flight. The witnesses were located about 7,000 feet northwest of the threshold of runway 11. They stated that the landing gear was up and that the aircraft seemed to be 'fast' for that portion of the approach. When the aircraft disappeared behind an obstruction, these witnesses moved to another location to continue watching the aircraft. They saw the nose gear in transit and stated that it appeared to be completely down as the aircraft crossed over the first two approach lights. The first two approach lights are located about 3,000 feet from the runway threshold. A witness, who was located on the fifth floor of the airport terminal, saw the aircraft when it was about 25 feet over the runway. The witness stated that the aircraft was in a level attitude, but that it appeared 'very fast.' He stated that the aircraft touched down about one-quarter way down the runway, that it bounced slightly, and that it landed again on the nose gear only. It then began a porpoising motion which continued until the aircraft was past midfield. Most witnesses placed the touchdown between one-quarter and one-half way down the runway and reported that the aircraft seemed faster-than-normal during the landing roll. Witnesses reported varying degrees of reverse thrust, but most reported only a short burst of reverse thrust as the aircraft passed the airport terminal, about 3,800 feet past the threshold of runway 11.
Probable cause:
The captain's faulty judgement in initiating a go-around after he was committed to a full stop landing following an excessively long and fast touchdown from an unstabilized approach. Contributing to the accident was the pilot's unprofessional decision to abandon the precision approach. The following findings were reported:
- There is no evidence of aircraft structure or component failure or malfunction before the aircraft crashed.
- The flight crew was aware of the airport and weather conditions at Ketchikan.
- The weather conditions and runway conditions dictated that a precision approach should have been flown.
- The approach was not made according to prescribed procedures and was not stabilized. The aircraft was not in the proper position at decision height to assure a safe landing because of excessive airspeed, excessive altitude, and improperly configured flaps and landing gear.
- The aircraft's altitude was higher-than-normal when it crossed the threshold of runway 11 and its airspeed was excessively high.
- The captain did not use good judgment when he initiated a go-around after he was committed to full-stop landing following the touchdown.
- There is no evidence that the first and second officers apprised the captain of his departure from prescribed procedures and safe practices, or that they acted in any way to assure a more professional performance, except for the comment by the first officer, when near the threshold, that they were high after which he lowered the flaps to 40°.
- After applying reverse thrust shortly after touchdown, the captain was unable to regain forward thrust because the high speed of the aircraft produced higher-than-normal airloads on the thrust deflector doors.
- Braking action on runway 11 was adequate for stopping the aircraft before it reached the departure end of the runway.
- Before the accident the FAA had not determined adequately the airport's firefighting capabilities.
- Postaccident hearing tests conducted on the captain indicated a medically disqualifying hearing loss; however, the evidence was inadequate to conclude that this condition had any bearing on the accident.
Final Report:

Crash of a Douglas C-47 in Puerto Asís: 5 killed

Date & Time: Apr 2, 1976
Operator:
Registration:
FAC-676
Survivors:
Yes
Schedule:
Florencia - Puerto Asís
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
14
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
On approach to Puerto Asís Airport, the crew encountered heavy rain falls when the airplane crashed into a lake located few km short of runway. A crew member and four passengers were killed while 11 other occupants were rescued.

Crash of a Douglas DC-8-43 in Havana

Date & Time: Mar 18, 1976
Type of aircraft:
Operator:
Registration:
CU-T1200
Survivors:
Yes
Schedule:
Montreal - Havana
MSN:
45638/156
YOM:
1961
Flight number:
CU455
Country:
Crew on board:
16
Crew fatalities:
Pax on board:
13
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
While approaching Havana-José Martí-Rancho Boyeros Airport following an uneventful flight from Montreal, the four engine airplane collided with a Cubana Antonov AN-24B that was completing a local training flight with a crew of five on board. While the DC-8 was able to continue the approach and to land without further problems, the Antonov crashed, killing its entire crew.

Crash of a Beechcraft 99A Airliner in Poughkeepsie

Date & Time: Mar 16, 1976 at 1630 LT
Type of aircraft:
Operator:
Registration:
N7997R
Flight Phase:
Survivors:
Yes
Schedule:
Poughkeepsie - New York
MSN:
U-119
YOM:
1969
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
14159
Captain / Total hours on type:
3343.00
Circumstances:
Just after liftoff from an ice/slush covered runway, the airplane shuddered then rolled left and right, causing the wings to drop. The airplane leveled, crash landed and came to rest in flames. All seven passengers and a pilot were evacuated to safety while a pilot was seriously injured.
Probable cause:
Stall during initial climb after the crew exercised poor judgment. The following contributing factors were reported:
- Inadequate preflight preparation,
- Initiated flight in adverse weather conditions,
- Failed to abort takeoff,
- Failed to maintain flying speed,
- Airport conditions: ice/slush on runway,
- Snow,
- Icing conditions including sleet and freezing rain,
- Visibility 1/2 mile or less,
- Fog,
- Aircraft approximately 368 lbs over gross weight.
Final Report: