Crash of a Lockheed L-188AF Electra in Kansas City: 3 killed

Date & Time: Jan 9, 1985 at 0701 LT
Type of aircraft:
Registration:
N357Q
Flight Type:
Survivors:
No
Schedule:
Detroit - Kansas City
MSN:
1044
YOM:
1959
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
14500
Captain / Total hours on type:
5000.00
Circumstances:
During arrival to the Kansas City Downtown Airport, the flight was vectored for a VOR runway 03 approach, then was cleared for the approach and to circle and land on runway 36. On final approach, the aircraft was high and was not in a position to land, so the flight was cleared to circle left for another approach to land. The aircrew acknowledged and began circling left which took them in the vicinity of the Fairfax Airport. A short time later, the ATC controller cautioned that the flight might be lining up for the Fairfax Airport. Subsequently, the crew initiated a missed approach and were instructed to turn to 360° and climb to 3,000 feet. The aircraft began a steep climb to 3,100 feet, stalled and entered a steep descent. Before the descent was arrested, the aircraft impacted in a public water treatment plant. CVR recordings indicated that the 1st officer was flying the aircraft during the en route descent, VOR approach and circling approach, then the captain took control during the missed approach. An exam of the wreckage revealed no evidence of an airframe or powerplant problem. Also, there was no evidence that the cargo had shifted. All three crew members were killed.
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: missed approach (ifr)
Findings
1. (f) weather condition - low ceiling
2. (f) weather condition - fog
3. (f) light condition - dawn
4. (f) ifr procedure - improper - copilot/second pilot
5. (f) supervision - inadequate - pilot in command
6. Maneuver - performed - copilot/second pilot
7. (f) became lost/disoriented - inadvertent - copilot/second pilot
8. (f) became lost/disoriented - inadvertent - pilot in command
9. Missed approach - initiated
10. (c) airspeed - not maintained - pilot in command
11. (c) stall - inadvertent - pilot in command
12. Remedial action - delayed
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of a Mitsubishi MU-2B-25 Marquise in West Point: 1 killed

Date & Time: Jan 4, 1985 at 1852 LT
Type of aircraft:
Registration:
N275MA
Flight Type:
Survivors:
No
Schedule:
Youngstown - West Point
MSN:
255
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
28818
Captain / Total hours on type:
1500.00
Aircraft flight hours:
45804
Circumstances:
After being delayed at least 2 days at Youngstown, OH, due to maintenance problems the pilot departed at approximately 1725 hours with the knowledge that the weather at his destination was ift to lifr. In addition, the pilot was scheduled for a vacation and had expressed hopes of departing on it that evening. The aircraft was seen circling West Point Municipal Airport in and out of low clouds, fog, and/or smoke from a nearby mill. Immediately before the aircraft collided with trees 6.5 miles west of the airport, a witness saw red lights, one on the rear and one close to the front of the aircraft, which was estimated to be flying at approximately tree top level. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: in flight encounter with weather
Phase of operation: circling (ifr)
Findings
1. (f) weather condition - below approach/landing minimums
2. (c) became lost/disoriented - inadvertent - pilot in command
3. Self-induced pressure - pilot in command
4. (f) weather condition - low ceiling
5. (f) weather condition - fog
6. (f) weather condition - obscuration
----------
Occurrence #2: in flight collision with object
Phase of operation: circling (ifr)
Findings
7. (f) light condition - dark night
8. (f) object - tree(s)
9. (c) missed approach - not performed - pilot in command
Final Report:

Crash of a Cessna 402C in Troy

Date & Time: Dec 26, 1984 at 2130 LT
Type of aircraft:
Operator:
Registration:
N115EA
Flight Phase:
Survivors:
Yes
Schedule:
Troy - Pikeville
MSN:
402C-0090
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
11158
Captain / Total hours on type:
2700.00
Aircraft flight hours:
1593
Circumstances:
The aircraft collided with trees during the initial takeoff climb from runway 27 at Oakland-Troy Airport, Troy, MI, while on a corporate flight. Investigation revealed that approximately 3 to 5 inches of snow had fallen at the airport during the day and the snow had not been removed from the runway that evening. A witness reported there was 5 inches of snow on the runway and it was snowing at the time of the accident. The pilot reported that 'shortly after takeoff the aircraft yawed, then veered right. Upon correcting this condition left wing struck the ground.' When the right engine was tested a small leak was discovered at the air intake manifold. The left engine was severely damaged by fire and could not be tested. All four occupants escaped uninjured.
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: takeoff - initial climb
Findings
1. (f) terrain condition - turbulence
2. (c) proper climb rate - not attained - pilot in command
3. (c) overconfidence in aircraft's ability - pilot in command
4. (f) aircraft performance, takeoff capability - undetermined
5. (f) airport snow removal - not performed - airport personnel
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: takeoff - initial climb
Final Report:

Crash of a Cessna 441 Conquest in Marble Falls: 1 killed

Date & Time: Dec 25, 1984 at 2020 LT
Type of aircraft:
Registration:
N441CM
Survivors:
No
Schedule:
Aspen - Marble Falls
MSN:
441-0169
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
9165
Captain / Total hours on type:
608.00
Aircraft flight hours:
2799
Circumstances:
The aircraft crashed approximately 1.5 miles south of the departure end of runway 17 during an attempted runway 17 NDB approach. The aircraft was cleared for the approach at 2012 cst and the pilot canceled IFR reporting the airport in sight at 2014. A witness located approximately 1 mile south of the airport reported seeing the aircraft lights through the clouds, mist and fog as it was traveling south-southeast. The aircraft impacted the ground on a heading of 035° in a 10° to 15° left bank. Radar data indicates the aircraft was approximately 8 miles from the airport when IFR was canceled. Witnesses stated visibility in the area was about 1/8 of a mile during the time of the accident. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: in flight collision with terrain/water
Phase of operation: maneuvering - turn to reverse direction
Findings
1. (f) weather condition - low ceiling
2. (f) weather condition - fog
3. (c) in-flight planning/decision - poor - pilot in command
4. (c) ifr procedure - not followed - pilot in command
5. (f) missed approach - not performed - pilot in command
6. (c) proper altitude - not maintained - pilot in command
Final Report:

Crash of a Cessna 402B in Rochester: 1 killed

Date & Time: Dec 22, 1984 at 1733 LT
Type of aircraft:
Operator:
Registration:
N8064Q
Flight Phase:
Survivors:
No
Schedule:
Rochester - Teterboro
MSN:
402-0400
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2066
Aircraft flight hours:
6194
Circumstances:
Prior to takeoff the pilot was informed of wind shear as centerfield winds as 270° at 25 knots gust to 46 knots and northwest boundary winds as 280° at 13 knots. During takeoff the pilot reported an opened door and requested to return to land. The aircraft turned left and descended to the ground. Examination of the aircraft did not disclose evidence of malfunction. Examination of the aircraft doors revealed the right side cargo door securing mechanisms were relatively undamaged. Flight test conducted to evaluate the effects of a opened door disclosed in part the following. The door will open and remain open during rotation; results in noise and vibration; no abnormal flight characteristics; no significant change in multi-engine climb performance. Pilot landing in jet aircraft prior to accident reported moderate turbulence with a plus or minus 10 to 15 knots change in airspeed from 2,000 feet msl to the surface. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: miscellaneous/other
Phase of operation: takeoff - initial climb
Findings
1. (f) door, cargo/baggage - fire
2. (c) preflight planning/preparation - inadequate - pilot in command
----------
Occurrence #2: loss of control - in flight
Phase of operation: takeoff - initial climb
Findings
3. (f) weather condition - windshear
4. (f) weather condition - unfavorable wind
5. (c) airspeed - not maintained - pilot in command
6. (c) inattentive - pilot in command
7. (c) stall - inadvertent - pilot in command
----------
Occurrence #3: on ground/water encounter with terrain/water
Phase of operation: descent
Final Report:

Crash of a Rockwell Grand Commander 690A in Pea Ridge: 1 killed

Date & Time: Dec 20, 1984 at 1920 LT
Registration:
N9229Y
Survivors:
Yes
Schedule:
Baton Rouge - Pea Ridge
MSN:
690-11122
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4900
Aircraft flight hours:
2857
Circumstances:
Pilot was cleared for VOR/DME approach to Rogers airport by Fayetteville approach control; Fayetteville altimeter setting of 29.85 (confirmed by recorded transcript) furnished. Pilot did not read back. During approach, aircraft impacted trees 25 feet agl at approximately 1,320 feet msl, 3 miles short of airport. Investigation showed pilot's altimeter set at 30.14 (altimeter would read 290 feet higher than aircraft actual altitude). Pilots's recall was that the 30.14 setting was furnished by approach control. Pilot further stated last recalled altitude reading was 1,750 feet. Approach plate shows 1,700 feet mda with Rogers altimeter setting; increase mda by 100 feet if using Fayetteville setting. The pilot was seriously injured and the passenger was killed.
Probable cause:
Occurrence #1: in flight collision with terrain/water
Phase of operation: approach - faf/outer marker to threshold (ifr)
Findings
1. (f) air/ground communications - inattentive - pilot in command
2. (f) complacency - pilot in command
3. (f) altimeter setting - inaccurate - pilot in command
4. (f) ifr procedure - not followed - pilot in command
5. (c) minimum descent altitude - below - pilot in command
6. (f) terrain condition - high vegetation
Final Report:

Crash of a Learjet 35 in Waco: 3 killed

Date & Time: Dec 20, 1984 at 1638 LT
Type of aircraft:
Operator:
Registration:
N95TC
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Waco - Dallas
MSN:
35-020
YOM:
1975
Location:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
2454
Captain / Total hours on type:
387.00
Aircraft flight hours:
5276
Circumstances:
No evidence of preimpact mechanical failure or malfunction was noted during wreckage examination. The FAA operations inspector who was on board at the time of the accident stated there were no aircraft problems involved. The pic, who was in the process of taking her type rating checkride in the aircraft, failed to maintain directional control during a simulated engine failure after reaching V1 speed during the takeoff run. The total flight experience for the pic was 2,454 hours, most of which was acquired in multi-engine aircraft, with 387 hours being in the make and model aircraft involved in the accident. All listed experience in this make and model was obtained as second-in-command. All three occupants were killed.
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: takeoff - initial climb
Findings
1. (f) emergency procedure - simulated - check pilot
2. (c) procedures/directives - not followed - pilot in command
3. (c) directional control - not maintained - pilot in command
----------
Occurrence #2: dragged wing, rotor, pod, float or tail/skid
Phase of operation: takeoff - initial climb
Findings
4. (f) emergency procedure - simulated - check pilot
5. (c) rotation - excessive - pilot in command
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: takeoff - initial climb
Final Report:

Crash of a De Havilland DHC-3T Otter in Seattle

Date & Time: Dec 19, 1984 at 1108 LT
Type of aircraft:
Registration:
N4247A
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Seattle - Seattle
MSN:
421
YOM:
1964
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8500
Captain / Total hours on type:
15.00
Aircraft flight hours:
7445
Circumstances:
Aircraft was performing test flight maneuvers when problems with the modified fuel system occurred. Ice blocking a fuel vent line caused a partial collapse of the main (engine feed) fuel cell which produced an erroneous fuel quantity reading. In addition, the main tank overflow shut off valve was leaking, so tank overflow occurred. The fuel overflow caution light illuminated and auxiliary tank fuel pump feed to main automatically shut down. Due to miscalibration, this system overrode pilot attempts to restart aux fuel pumps. Pilot remained in test area troubleshooting rather than immediate return to base, finally noted main tank gage continuing to read 'full.' En route to Boeing Field, fuel starvation occurred. Pilot opted to attempt forced landing in small athletic field in residential area rather than ditch in puget sound. The aircraft touched down in intended landing area, then bounced across an adjacent street. The arresting action of telephone wires on the vertical fin brought the aircraft to rest in a residential backyard. All three occupants were injured, one seriously.
Probable cause:
Occurrence #1: airframe/component/system failure/malfunction
Phase of operation: maneuvering
Findings
1. (c) fuel system, vent - blocked (total)
2. (f) fuel system, tank - distorted
3. (f) engine instruments, fuel quantity gage - false indication
4. (f) fuel system, fuel shutoff - leak
----------
Occurrence #2: airframe/component/system failure/malfunction
Phase of operation: maneuvering
Findings
5. Fuel system, pump - switched off
6. Remedial action - not possible
----------
Occurrence #3: loss of engine power (total) - nonmechanical
Phase of operation: cruise
Findings
7. (f) precautionary landing - delayed - pilot in command
8. (f) fuel supply - misjudged - pilot in command
9. (c) fluid, fuel - starvation
----------
Occurrence #4: forced landing
Phase of operation: descent - emergency
----------
Occurrence #5: in flight collision with terrain/water
Phase of operation: landing
Findings
10. (f) terrain condition - none suitable
Final Report:

Crash of a Cessna 401A in Raton

Date & Time: Dec 17, 1984 at 1030 LT
Type of aircraft:
Registration:
N365AA
Survivors:
Yes
Schedule:
North Platte - Albuquerque
MSN:
401A-0047
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4256
Captain / Total hours on type:
460.00
Aircraft flight hours:
47426
Circumstances:
About 2 hours after departure, at 13,000 feet, the right engine fuel flow went to zero. The engine continued to operate indicating 24 inches of manifold pressure. All other instruments were normal but what looked like a brown stain developed on top of the right wing along the spar cap near the tip tank. Artcc was advised that a precautionary landing would be made at Raton and a rapid descent was begun. On final the right engine nacelle and wing locker turned brown. As the aircraft landed flames appeared on the right side of the fuselage and smoke entered the cabin. Both engines were secured and brakes applied. The brakes were inoperative therefore, the pilot steered the aircraft off the runway into a snowbank collapsing the nose gear. Within 15 mins most of the wreckage was consumed by the fire. Ignition source and fire origination point were not determined. All three occupants escaped uninjured.
Probable cause:
Occurrence #1: loss of engine power(partial) - mech failure/malf
Phase of operation: cruise - normal
Findings
1. (f) engine instruments, fuel flow gage - no pressure
2. (f) engine instruments, manifold pressure gage - loss, partial
----------
Occurrence #2: fire/explosion
Phase of operation: cruise - normal
Findings
3. (f) wing, skin - burned
----------
Occurrence #3: forced landing
Phase of operation: descent - emergency
Findings
4. (c) precautionary landing - performed - pilot in command
5. (c) landing gear, normal brake system - failure, total
----------
Occurrence #4: on ground/water collision with object
Phase of operation: landing - roll
Findings
6. (f) terrain condition - snowbank
7. (c) ground loop/swerve - intentional - pilot in command
----------
Occurrence #5: nose gear collapsed
Phase of operation: landing - roll
Findings
8. (f) landing gear, nose gear assembly - overload
Final Report:

Crash of a Piper PA-61 Aerostar (Ted Smith 601P) in Mammoth Lakes: 1 killed

Date & Time: Dec 16, 1984 at 1600 LT
Registration:
N601FP
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Mammoth Lakes - Burbank
MSN:
61P-0597-7963266
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
7408
Captain / Total hours on type:
533.00
Aircraft flight hours:
15974
Circumstances:
The aircraft took off from an airport whose runways had been closed for snow removal. A notam had been filed with the Fresno FSS by the Mammoth Lakes Airport Manager at 0900 hours for taxi and runway snow removal. The pilot was aware of the notam because the manager and a lineman both said they advised him of it. Several witnesses saw the pilot enter the aircraft after declining engine pre-heat or aircraft de-icing. When advised by the lineman that the 2 qts of oil that the pilot requested did not 'register on the dipstick.' The pilot ordered another qt to be 'thrown' in and 'hurry up.' No preflight or warm up or before takeoff check was noted by observers. Turning immediately onto the runway and rolling for takeoff the pilot passed a snow plow. The aircraft used 7,000 feet (all of the runway) and left the ground in a nose high attitude. The airport elevation is 7,128 feet msl. The aircraft first struck a dirt mound 3/4 of a mile after takeoff. After maintaining further flight for approximately 280 feet which crossed a small ravine the aircraft collided with the far side of the ravine and started to break apart, stopping 144 feet further east. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: takeoff - initial climb
Findings
1. (c) preflight planning/preparation - improper - pilot in command
2. (c) ice/frost removal from aircraft - inadequate - pilot in command
3. (c) checklist - improper - pilot in command
4. (c) judgment - poor - pilot in command
5. (f) wing - ice
6. (c) rotation - delayed - pilot in command
7. (f) misc eqpt/furnishings, shoulder harness - not engaged
8. (f) aircraft performance, climb capability - disabled
9. (c) stall/mush - not understood - pilot in command
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: takeoff - initial climb
Findings
10. (f) notams - issued - airport personnel
11. (c) airport snow removal - not identified - pilot in command
12. (c) proper climb rate - not possible - pilot in command
13. (c) notams - disregarded - pilot in command
Final Report: