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Crash of a Piper PA-46-500TP Malibu Meridian in San Antonio: 1 killed

Date & Time: Jan 18, 2008 at 1230 LT
Registration:
N169CA
Flight Type:
Survivors:
No
Schedule:
Waco – San Antonio
MSN:
46-97300
YOM:
2007
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1049
Captain / Total hours on type:
58.00
Aircraft flight hours:
111
Circumstances:
The pilot attempted to intercept an instrument landing system localizer three times without success. The pilot told Air Traffic Approach Control that he was having trouble performing a "coupled" approach and that he was trying to "get control" of the airplane. The airplane disappeared from radar, subsequently impacting a field and then a barn. The airplane came to rest in an upright position and a post crash fire ensued. A review of radar and voice data for the flight revealed that during the three approach attempts the pilot was able to turn to headings and climb to altitudes when assigned by air traffic control. Postmortem toxicology results were consistent with the regular use of a prescription antidepressant, and the recent use of a larger-than-maximal dose of an over-the-counter antihistamine known to cause impairment. There were no preimpact anomalies observed during the airframe and engine examinations that would have prevented normal operation.
Probable cause:
The pilot's failure to execute an instrument approach. Contributing to the accident was the pilot's impairment due to recent use of over-the-counter medication.
Final Report:

Crash of a Beechcraft 65-B80 Queen Air near O. H. Ivie Lake: 1 killed

Date & Time: Oct 26, 1995 at 0950 LT
Type of aircraft:
Operator:
Registration:
N9NP
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Waco - San Angelo
MSN:
LD-428
YOM:
1970
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2502
Captain / Total hours on type:
593.00
Aircraft flight hours:
8127
Circumstances:
Witnesses observed the airplane contact the water while buzzing a lake, 'emerge from a cloud of water,' and enter a climb trailing white vapor. As the airplane approached the lake shore, the right propeller 'quit turning,' then the airplane entered a steep right bank and impacted the ground. The right propeller lever was found in the feather position. Propeller teardowns revealed signatures indicating the right propeller was feathered and the left propeller was operating in the low pitch range at impact. Disassembly of the engines revealed no evidence of any pre-impact mechanical anomalies, and, in the opinion of the manufacturer, 'both engines appeared capable of producing power prior to impact.' Toxicological tests showed 178.000 mg/dl (0.178%) ethanol in vitreous fluid, 90.000 mg/dl (0.09%) ethanol in blood, 114.000 mg/dl (0.114%) ethanol in brain fluid, 3.000 mg/dl acetaldehyde in brain fluid, 22.000 mg/dl acetaldehyde in blood, and 4.000 mg/dl 2-propanol in brain fluid. The levels of ethanol found indicate ingestion of alcohol, and the levels of acetaldehyde and 2-propanol (metabolites of ethanol) detected support ingestion of alcohol.
Probable cause:
The pilot's impairment of judgment and performance due to alcohol which resulted in his improper decision to shutdown an engine, and his failure to maintain adequate airspeed for single-engine flight.
Final Report:

Crash of a Learjet 35 in Waco: 3 killed

Date & Time: Dec 20, 1984 at 1638 LT
Type of aircraft:
Operator:
Registration:
N95TC
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Waco - Dallas
MSN:
35-020
YOM:
1975
Location:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
2454
Captain / Total hours on type:
387.00
Aircraft flight hours:
5276
Circumstances:
No evidence of preimpact mechanical failure or malfunction was noted during wreckage examination. The FAA operations inspector who was on board at the time of the accident stated there were no aircraft problems involved. The pic, who was in the process of taking her type rating checkride in the aircraft, failed to maintain directional control during a simulated engine failure after reaching V1 speed during the takeoff run. The total flight experience for the pic was 2,454 hours, most of which was acquired in multi-engine aircraft, with 387 hours being in the make and model aircraft involved in the accident. All listed experience in this make and model was obtained as second-in-command. All three occupants were killed.
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: takeoff - initial climb
Findings
1. (f) emergency procedure - simulated - check pilot
2. (c) procedures/directives - not followed - pilot in command
3. (c) directional control - not maintained - pilot in command
----------
Occurrence #2: dragged wing, rotor, pod, float or tail/skid
Phase of operation: takeoff - initial climb
Findings
4. (f) emergency procedure - simulated - check pilot
5. (c) rotation - excessive - pilot in command
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: takeoff - initial climb
Final Report:

Crash of a Beechcraft C-45H Expeditor in Waco

Date & Time: Dec 20, 1973 at 2026 LT
Type of aircraft:
Registration:
N2122
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Waco - Dallas
MSN:
AF-480
YOM:
1953
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3116
Captain / Total hours on type:
930.00
Circumstances:
Shortly after takeoff from Waco-Madison Cooper Airport, while climbing, the pilot encountered technical problems and was cleared to return for an emergency landing. Few seconds later, he lost control of the airplane that crashed few miles from the airfield. The aircraft was destroyed and the pilot, sole on board, was seriously injured.
Probable cause:
The pilot failed to maintain flying speed during initial climb. The following factors were reported:
- Inadequate preflight preparation,
- Improperly loaded aircraft and CofG,
- Pilot reported after takeoff he would have to return and land,
- CofG 3.38 inches after the rear limit.
Final Report:

Crash of a Lockheed Vega 5C in Fort Worth: 1 killed

Date & Time: Nov 9, 1935 at 0445 LT
Type of aircraft:
Operator:
Registration:
NC980Y
Flight Type:
Survivors:
No
Schedule:
Dallas – Waco
MSN:
191
YOM:
1932
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
On November 9, 1935, at approximately 0445LT within the city limits of East Fort Worth, Texas, a commercially owned airplane, while being flown without passengers, crashed with resultant death of the pilot and the complete destruction of the aircraft. The airplane, a Lockheed Vega, model 5C, was owned and operated by Braniff Airway Inc., Oklahoma City, Oklahoma, and bore Department of Commerce licence n° NC980Y. At the time of the accident it was being ferried from Dallas to Waco, Texas, via Fort Worth, and no passengers were permitted to be carried. The pilot, William C. Maus of Waco, Texas, held a Department of Commerce transport pilot's licence and a scheduled air transport rating. The take-off was accomplished at 0410LT, the airplane carrying a 5-hour gasoline supply. The ceiling at Dallas was 1,000 feet with 8 miles visibility. Fort Worth at the time had a ceiling of 500 feet with 7 miles visibility. It had not been the intention of the pilot to land at Fort Worth but to fly beyond it to a lighted airway leading into Waco, Texas, his destination. By the time Fort Worth was reached the ceiling had dropped to about 75 feet and the visibility was zero. This change in weather was broadcast to the pilot from Fort Worth with instructions that he return to Dallas. Whether or not the pilot received this broadcast is not known inasmuch as his airplane was not equipped with two-way radio. However, he had plenty of fuel and could have easily returned to Dallas, where the weather had remained constant, or have flown on to Houston, where the ceiling was practically unlimited. Reports from various people who heard the airplane overhead and saw the accident indicate that the pilot was attempting to get under the 75-foot ceiling, presumably to locate the airport. He was heard flying around for some time and made two complete circles at a low altitude in the immediate vicinity of the accident. Immediately preceding the crash the airplane appeared diving out of the mist. The engine was heard to accelerate as through the pilot had just caught sight of the ground and was making an effort to pull the airplane out of the dive before striking. The aircraft was destroyed by impact forces and the pilot was killed.
Probable cause:
It is the opinion of the Accident Board that the probable cause of this accident was poor judgment on the part of the pilote for attempting to land at Fort Worth under existing weather conditions.