Crash of an IAI-1124A Westwind II near Gouldsboro: 3 killed

Date & Time: Dec 12, 1999 at 1635 LT
Type of aircraft:
Registration:
N50PL
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Seattle - Teterboro
MSN:
338
YOM:
1981
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
10250
Captain / Total hours on type:
1500.00
Aircraft flight hours:
5035
Circumstances:
After a 5-hour flight, the Westwind jet began its descent to the airport. Air traffic control instructed the flight crew to cross a VOR at 18,000 feet. The flight crew was then instructed to cross an intersection at 6,000 feet. The flight crew needed to descend the airplane 12,000 feet, in 36 nautical miles, to make the crossing restriction. The flight crew acknowledged the clearance, and no further transmissions were received from the airplane. The airplane struck treetops and impacted the ground in a wooded area. The accident flight was the airplane's first flight after maintenance. Work that was accomplished during the maintenance included disassembly and reassembly of the horizontal stabilizer trim actuator. Examination of the actuator at the accident site revealed that components of the actuator were separated and that they displayed no damage where they would have been attached. Examination of the actuator by the Safety Board revealed that the actuator had not been properly assembled in the airplane. A similar actuator was improperly assembled and installed in a static airplane for a ground test. When the actuator was run, the jackscrews of the actuator were observed backing out of the rod end caps within the first few actuations of the pitch trim toward the nose-down position. As the pitch trim continued to be actuated toward the nose-down position, the jackscrews became disconnected from the rod end caps, and the horizontal stabilizer became disconnected from the actuator. The passenger was Peter Lahaye, founder and owner of the Lahaye Laboratories and the aircraft.
Probable cause:
The improper assembly of the horizontal stabilizer trim actuator unit by maintenance personnel.
Final Report:

Crash of a Beechcraft C90 King Air in Burlington: 2 killed

Date & Time: Feb 13, 1990 at 1830 LT
Type of aircraft:
Operator:
Registration:
N110LT
Survivors:
No
Schedule:
Teterboro - Burlington
MSN:
LJ-729
YOM:
1977
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
13800
Aircraft flight hours:
5976
Circumstances:
The pilot transmitted on unicom that he was on final for runway 24. Following a double fuel starvation power loss the airplane impacted nose low with trees and terrain about 2.6 miles from runway 24. Last fueling occurred on the previous day at Albermarle, NC, the pilot's primary source of fuel, 50 miles from Burlington. The flight proceeded to Burlington, Teterboro, and was returning to Burlington. Total estimated flight time was 4 hours 32 minutes. Fuel burn was calculated to be 361 gallons. Usable fuel was 384 gallons and 24 gallons were recovered from the right center tank. If the fuel transfer pump does not operate 28 gallons will be unusable. That pump was found in the off position. No fuel spillage occurred at the scene. On 2/8/90 the pilot purchased 361 gallons of fuel for N110LT. Lower fuel prices at the favored location were the pilot's reason for fueling there. Examination of engines, propellers, fuel pumps, and other relative components did not reveal any significant discrepancy. Both occupants were killed.
Probable cause:
The double engine power loss due to fuel starvation, the pilot's failure to follow procedures and directives by not engaging the right fuel transfer pump, and the inadvertent stall during the forced landing approach. A factor was the pilot's failure to refuel before adequate fuel reserves were exhausted.
Final Report:

Crash of a Piper PA-60 Aerostar (Ted Smith 602P) in Frenchtown: 1 killed

Date & Time: Dec 21, 1989 at 1035 LT
Registration:
N6894Y
Flight Phase:
Survivors:
No
Schedule:
Teterboro – Reading
MSN:
62-0909-8165036
YOM:
1981
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2061
Captain / Total hours on type:
312.00
Circumstances:
On January 16, 1989, Machen nacelle mounted induction air intercoolers were installed on N6894Y. On December 14, 1989, an annual inspection was performed, and a Machen superstar i-680 kit was installed. On December 21, 1989, N6894Y was at 6,000 feet when the pilot reported a problem with the right engine. The pilot reported a fire in the right engine. A couple of minutes later, he radioed he could not shut down the right engine. At 1034:37 the pilot advised his 'right engine just tore off' and that he was 'in a spin heading down.' The exhaust tailpipe of the left turbocharger on the right engine was found to have separated. Metallurgical examination revealed the tailpipe failed due to fatigue cracking. Records showed that part I of piper service bulletin 920 (engine tailpipe inspection) had been completed, while part II (addition of fire detection system) had not been accomplished due to the lack of available kits. The pilot, sole on board, was killed.
Probable cause:
The inadequate maintenance and inspection of the turbocharger tailpipe exhaust stack on the right engine by the mechanic(s). The failure of the tailpipe permitted heat from the exhaust to weaken the main spar of the right wing resulting in a catastrophic failure.
Final Report:

Crash of a Learjet 35A in Teterboro: 4 killed

Date & Time: May 24, 1988 at 0316 LT
Type of aircraft:
Registration:
N500RW
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Teterboro - Morristown
MSN:
35-148
YOM:
1978
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
8910
Captain / Total hours on type:
759.00
Aircraft flight hours:
4735
Circumstances:
Witnesses reported a normal takeoff. Radar indicated the aircraft turned right as cleared and began cruise at 1900 feet, heading northwest at 235 knots. 65 seconds after calling clear of the control zone the aircraft's radar track ended. The aircraft was fragmented by the impact with all flight control surfaces and aircraft extremities found at the impact site. Pitch trim was found in the normal cruise setting with gear, flaps, and spoilers in the retracted position. Examination of the engines indicated operation at impact. Aircraft struck the terrain in approx 80° nose down, wings level attitude and heading opposite to the previous direction of flight. In flight simulator tests, with the aircraft initially in level flight at 1,900 feet and then rolled inverted and the pitch control moved aft, the aircraft attitude was similar to the attitude at impact. There were two unauthorized passengers on board, one was the copilot's wife. The impact point was in a very small region of uncontrolled airspace very near the copilot's and relative's homes. The copilot was new to jet operations. The aircraft departed with several discrepancies uncleared. All four occupants were killed.
Probable cause:
Occurrence #1: in flight collision with terrain/water
Phase of operation: maneuvering
Findings
1. (f) light condition - dark night
2. (c) maneuver - attempted - pilot in command
3. (c) judgment - poor - pilot in command
4. (c) altitude - misjudged - pilot in command
5. (f) lack of total experience in type operation - pilot in command
6. (f) lack of total experience in type operation - copilot/second pilot
7. Operation with known deficiencies in equipment - attempted - company maintenance personnel
Final Report:

Crash of a Learjet 35A in Pittsburgh: 2 killed

Date & Time: May 12, 1987 at 1057 LT
Type of aircraft:
Operator:
Registration:
N100EP
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Pittsburgh - Teterboro
MSN:
35-150
YOM:
1978
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
10211
Captain / Total hours on type:
3838.00
Aircraft flight hours:
4203
Circumstances:
The copilot (dual student) was to get a prof check on the 1st leg of the flight with a simulated single engine power loss on takeoff. According to witnesses, the takeoff was normal until lift off approximately 3,200 feet down the runway; but after lift-off, the aircraft climbed only about 50 feet and didn't seem to accelerate. They reported the nose pitched up and the aircraft went in a steep bank attitude near the departure end of the runway. Subsequently, it descended and crashed in wooded terrain in a right wing down, nose high attitude. A bystander tried to get in the aircraft to rescue the pilots, but the door was jammed and he was unable to break the cabin windows. A fire erupted and engulfed the aircraft. Due to rough terrain, there was a delay in getting fire fighting equipment to the accident site. No preimpact mechanical failures were found. The gear, flaps and spoilers were found in the retracted position. For takeoff, the flaps should have been extended to the 8° or 20° position. The stall speeds for 20°, 8° and no flaps were 104.5, 109.0 and 119.5 knots, respectively. The captain was an FAA designated flight examiner and a certified flight instructor (cfi).
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: takeoff - initial climb
Findings
1. Emergency procedure - simulated - pilot in command (cfi)
2. (c) raising of flaps - premature - copilot/second pilot
3. (c) airspeed - inadequate
4. (c) stall - inadvertent
5. (c) supervision - inadequate - pilot in command (cfi)
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: takeoff
Final Report:

Crash of a Learjet 55 Longhorn in Rutland

Date & Time: Aug 6, 1986 at 1455 LT
Type of aircraft:
Registration:
N921FP
Flight Phase:
Survivors:
Yes
Schedule:
Rutland - Teterboro
MSN:
55-103
YOM:
1984
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7900
Captain / Total hours on type:
1800.00
Aircraft flight hours:
901
Circumstances:
The Lear 55 taxied out for takeoff and inadvertently attempted a takeoff on the wrong runway. When he realized his mistake, he aborted the takeoff because he knew the runway length was significantly less than his required field length. Insufficient runway also remained for the aborted takeoff and the aircraft ran off the end of the runway and hit a stone wall. The aircraft was destroyed by fire and the copilot received minor injuries while the pilot and the passenger were not injured.
Probable cause:
Occurrence #1: overrun
Phase of operation: takeoff - roll/run
Findings
1. Light condition - daylight
2. (c) wrong runway - selected - pilot in command
3. (f) complacency - pilot in command
4. (c) checklist - not used - pilot in command
5. Aborted takeoff - performed - pilot in command
6. (c) procedures/directives - not followed - pilot in command
----------
Occurrence #2: on ground/water collision with object
Phase of operation: takeoff - roll/run
Findings
7. (f) object - fence
Final Report:

Crash of an IAI 1124A Westwind in Redwater: 7 killed

Date & Time: Apr 4, 1986 at 1922 LT
Type of aircraft:
Registration:
N50SK
Flight Phase:
Survivors:
No
Schedule:
Dallas - Teterboro
MSN:
309
YOM:
1980
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
7353
Captain / Total hours on type:
657.00
Aircraft flight hours:
2745
Circumstances:
Airplane crashed during a uncontrolled descent, following a turbulence upset at FL370. The upset occurred as a result of clear air turbulences associated with a vip level 6 thunderstorm located within 7 miles of the last position of the airplane. After the upset, the airplane penetrated and descended thru the cell which contained lightning, extreme turbulences and severe icing. During the upset/descent both engines flamed out and the crew's attempts to recover the airplane were unsuccessful due to conditions in the cell. Crew received an improper briefing from FSS and reported their radar was malfunctioning to the deputy controller. Sigmet and AWW info was not given during the briefing. As the airplane came out of the bottom of the cell at 4,000 feet, the crew overstressed the airplane causing the left main landing door to separate and hit the left horizontal stab which subsequently separated in overload. Impact was 82° nose down. Nature of the airplane radar malfunction could not be determined. All seven occupants were killed.
Probable cause:
Occurrence #1: airframe/component/system failure/malfunction
Phase of operation: climb - to cruise
Findings
1. (c) flight/nav instruments, weather radar system - failure, partial
2. (f) operation with known deficiencies in equipment - continued - pilot in command
----------
Occurrence #2: in flight encounter with weather
Phase of operation: cruise - normal
Findings
3. (c) weather condition - thunderstorm
4. (c) weather condition - turbulence, clear air
5. (c) weather condition - gusts
6. (c) weather condition - downdraft
7. (f) light condition - dark night
8. (c) preflight briefing service - improper - atc personnel (fss)
9. (c) hazardous weather advisory - not issued - atc personnel (fss)
----------
Occurrence #3: in flight encounter with weather
Phase of operation: cruise - normal
Findings
10. (c) in-flight weather advisories - not issued - atc personnel (fss)
11. (c) information unclear - atc personnel (fss)
----------
Occurrence #4: loss of control - in flight
Phase of operation: cruise - normal
Findings
12. Remedial action - attempted - pilot in command
13. (f) excessive workload (task overload) - pilot in command
14. (f) excessive workload (task overload) - copilot/second pilot
----------
Occurrence #5: loss of engine power (total) - nonmechanical
Phase of operation: descent - uncontrolled
----------
Occurrence #6: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of a Cessna 340A in Peru: 1 killed

Date & Time: Dec 8, 1985 at 1815 LT
Type of aircraft:
Registration:
N36888
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Portland – Teterboro
MSN:
340A-0950
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2500
Captain / Total hours on type:
32.00
Aircraft flight hours:
2545
Circumstances:
During IFR flight at 12,000 feet both aircraft vacuum pumps failed. Aircraft descended in right turn off radar. Witnesses observed aircraft at low altitude above trees, circle, make steep left turn, climb and descend to ground. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: cruise
Findings
1. (c) vacuum system - failure, total
2. (c) ifr procedure - improper - pilot in command
3. (c) flight/nav instruments, attitude gyro - inoperative
4. (c) stall - inadvertent - pilot in command
5. (f) spatial disorientation - pilot in command
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of a Cessna 402C in Detroit: 1 killed

Date & Time: Nov 12, 1985 at 0208 LT
Type of aircraft:
Registration:
N6788Y
Flight Type:
Survivors:
No
Schedule:
Teterboro - Detroit - Chicago
MSN:
402C-0433
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4900
Captain / Total hours on type:
350.00
Aircraft flight hours:
2607
Circumstances:
A 100-feet ceiling with 3,000 feet RVR existed at Detroit. The pilot attempted an ILS approach with a 200 feet dh when he struck trees one mile from the runway. He flew the aircraft to the airfield but crashed near the threshold. The only approach plates found onboard were for Detroit and Midway in Chicago. Midway was his final destination after Detroit. He did not have enough fuel to get to Midway. The rest of his approach plates were later found in his personal vehicle back in Pennsylvania. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: in flight collision with object
Phase of operation: approach - faf/outer marker to threshold (ifr)
Findings
1. (f) object - tree(s)
2. (c) ifr procedure - improper use of - pilot in command
3. (f) information unavailable - pilot in command
4. (f) weather condition - low ceiling
5. (c) preflight planning/preparation - inattentive - pilot in command
6. (f) self-induced pressure - pilot in command
7. (c) not performed - pilot in command
8. (c) visual lookout - reduced - pilot in command
9. (c) minimum descent altitude - not followed - pilot in command
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Findings
10. (f) flt control syst, aileron control - loss, partial
11. (f) directional control - not possible - pilot in command
12. (f) flight control, aileron surface - loss, partial
13. (f) wing,wingtip - loss, total
Final Report:

Crash of a Dassault Falcon 50 in Teterboro: 3 killed

Date & Time: Nov 10, 1985 at 1722 LT
Type of aircraft:
Operator:
Registration:
N784B
Flight Type:
Survivors:
No
Site:
Schedule:
Morristown - Teterboro
MSN:
118
YOM:
1982
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
8265
Captain / Total hours on type:
817.00
Circumstances:
A Dassault Falcon 50 jet (N784B) and an Air Pegasus Piper PA-28-181 Archer (N1977H) collided about 1500 feet over the towns of Fairview and Cliffside Park, New Jersey, USA. The Falcon 50 was cleared for a standard instrument approach procedure in visual meteorological conditions and was in a left turn to position itself on the downwind leg to runway 19 at the Teterboro Airport, and the PA-28 was transiting the airport traffic area from west to east when they collided. The accident occurred 4 1/2 miles east-southeast at the edge of the airport traffic area in visual meteorological conditions. Both airplanes had been in radio contact with the Teterboro control tower. The flightcrew, the only occupants aboard the Falcon 50, and the pilot and two passengers onboard the PA-28 were killed. The Falcon 50 crashed into an apartment building killing one resident and seriously injuring two bystanders.
Probable cause:
A breakdown in air traffic control coordination which resulted in an air traffic conflict and the inability of the DA50 flightcrew to ‘see and avoid' the other aircraft due to:
- An erroneous and inadequate traffic advisory and
- The physiological limitations of human vision and reaction time at night.
Air traffic control management contributed to the accident by failing to insure that controllers were following prescribed procedures and by failing to recognize and correct operational deficiencies.
Final Report: