Crash of a Piper PA-31T Cheyenne II near Flat Rock: 5 killed

Date & Time: Aug 23, 1985 at 2155 LT
Type of aircraft:
Registration:
N600CM
Flight Phase:
Survivors:
No
Site:
Schedule:
Louisville - Greer
MSN:
31-7720024
YOM:
1977
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
1700
Aircraft flight hours:
4077
Circumstances:
Aircraft hit northwest side of ridge in level attitude, cruise speed, heading southeast. Conditions were dark night and the cloud ceiling was about 40 feet above the ridge. Pilot received weather brief before take off and en route which reported a ceiling of 10,000 feet at destination. Aircraft was flown at 17,500 feet en route. Pilot-in-command radioed GSP approach control, said he was VFR for landing, passing 6,000 feet. Two way communication not established but discrete tx code assigned. Controller saw tx code change northwest of crash site then radar target disappeared at accident site. All five occupants were killed.
Probable cause:
Occurrence #1: in flight collision with terrain/water
Phase of operation: cruise
Findings
1. (c) ifr procedure - disregarded - pilot in command
2. (c) descent - premature - pilot in command
Final Report:

Crash of a Beechcraft E18S in Huntington

Date & Time: Jan 31, 1985 at 2045 LT
Type of aircraft:
Operator:
Registration:
N95HA
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Huntington - Louisville
MSN:
BA-148
YOM:
1956
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7022
Captain / Total hours on type:
3000.00
Aircraft flight hours:
5877
Circumstances:
3-4 inch snow accumulation on aircraft prior to flight. Pilot said he swept snow off except an area he could not reach. Heavy snowfall, wet snow reported as aircraft was prepared for departure, during runup, taxi and takeoff. Pilot advised by tower that visibility was 1/8 mile with fog and snow. Published takeoff minimum for far 135 opn was 1/2 mile. After riking snowplow located 150 feet left of runway, aircraft continued over embankment and came to rest inverted. Ice and snow fnd on upper tail surface. Elevator trim indicated full nose down. Aileron trim ind left bank. Witnesses said engines sounded normal, landing lights on, 600 feet visibility from position of snowplow. Pilot said 35 inches map when descending. Map increased with additional throttle. No engine roughness.
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: takeoff - initial climb
Findings
1. (f) light condition - dark night
2. (f) weather condition - fog
3. (f) weather condition - snow
4. (c) ice/frost removal from aircraft - inadequate - pilot in command
5. (f) proper assistance - not obtained - pilot in command
6. (f) weather condition - below approach/landing minimums
7. (f) ifr procedure - disregarded - pilot in command
8. Terrain condition - snow covered
9. Airspeed(vs) - not maintained - pilot in command
----------
Occurrence #2: in flight collision with object
Phase of operation: takeoff - initial climb
Findings
10. Object - vehicle
Final Report:

Crash of a Piper PA-31T Cheyenne in Madison

Date & Time: Nov 30, 1981 at 1715 LT
Type of aircraft:
Operator:
Registration:
N15SS
Flight Phase:
Survivors:
Yes
Schedule:
Peru - Louisville
MSN:
31T-7820068
YOM:
1978
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7126
Captain / Total hours on type:
1305.00
Circumstances:
While in cruising altitude from Peru to Louisville, both engines failed. The pilot reduced his altitude and attempted an emergency landing in an open field. Upon landing, the undercarriage collapsed and the airplane came to rest on its belly. All five occupants were seriously injured and the aircraft was damaged beyond repair.
Probable cause:
Engine failure in normal cruise due to inadequate preflight preparation. The following contributing factors were reported:
- Mismanagement of fuel,
- Fuel exhaustion,
- Instruments: fuel quantity gauge, erratic,
- Rough/uneven terrain,
- Complete failure of both engines,
- Forced landing off airport on land.
Final Report:

Crash of a Cessna 411 in Columbus: 1 killed

Date & Time: Jan 24, 1980 at 0241 LT
Type of aircraft:
Registration:
N23RJ
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Columbus - Louisville
MSN:
411-0287
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3300
Captain / Total hours on type:
20.00
Circumstances:
After takeoff from Columbus-Port Columbus Airport, while in initial climb, both engines suffered a partial loss of power. The airplane stalled, entered a spin and crashed in flames. The pilot, sole on board, was killed.
Probable cause:
Engine failure during initial climb after fuel system: pumps sheared. The following contributing factors were reported:
- The pilot failed to maintain flying speed,
- Inadequate preflight preparation on part of the pilot,
- Partial loss of power on both engines,
- Left engine fuel pump sheared,
- Left and right auxiliary fuel pumps found in low position.
Final Report:

Crash of a Rockwell Grand Commander 690A in Columbus

Date & Time: Oct 1, 1979 at 0803 LT
Operator:
Registration:
N57233
Survivors:
Yes
Schedule:
Louisville - Columbus
MSN:
690-11247
YOM:
1975
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
18341
Captain / Total hours on type:
2175.00
Circumstances:
On approach to Columbus-Ohio State University Airport, the pilot encountered limited visibility due to fog. On short final, the airplane struck a fence and crashed in flames short of runway threshold. The aircraft was destroyed and the pilot, sole on board, was injured.
Probable cause:
Collision with fence and subsequent crash on final approach due to improper IFR operation. The following contributing factors were reported:
- Fog,
- Visibility 3/4 mile or less.
Final Report:

Crash of a Beechcraft E18S in Indianapolis

Date & Time: Feb 27, 1979 at 0718 LT
Type of aircraft:
Operator:
Registration:
N711TL
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Indianapolis – Louisville
MSN:
BA-317
YOM:
1957
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1920
Captain / Total hours on type:
100.00
Circumstances:
Just after liftoff at Indianapolis Airport, while in initial climb, the twin engine airplane stalled and crashed. Both occupants were injured and the aircraft was destroyed.
Probable cause:
It was determined that the loss of control was the consequence of wake turbulences coming from a preceding Boeing 727 that just took off from the same runway. Uncontrolled collision with ground due to vortex turbulences.
Final Report:

Crash of a Beechcraft E18S in Toledo: 2 killed

Date & Time: Jun 26, 1975 at 2228 LT
Type of aircraft:
Registration:
N791A
Flight Type:
Survivors:
No
Schedule:
Detroit - Louisville - Paducah
MSN:
BA-103
YOM:
1955
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
6062
Captain / Total hours on type:
2890.00
Circumstances:
While cruising by night on a cargo flight, the crew encountered technical problems and the copilot informed ATC about the failure of an engine. The crew was cleared to divert to Toledo-Express for an emergency landing when, on final approach, the airplane struck power cables and crashed in flames. The aircraft was destroyed and both occupants were killed.
Probable cause:
Powerplant failure following cylinder assembly failure. The following contributing factors were reported:
- Fatigue fracture,
- Improper maintenance,
- Unapproved modification,
- Oil exhaustion on engine lubrication system,
- Oil exhaustion on propeller system,
- Fatigue of the cylinder head,
- Standpipe cut off flush with bottom of oil tank.
Final Report:

Crash of a Beechcraft D18S in Nashville: 1 killed

Date & Time: Jun 10, 1972 at 0200 LT
Type of aircraft:
Registration:
N7526
Flight Type:
Survivors:
Yes
Schedule:
Detroit - Louisville - Nashville
MSN:
A-995
YOM:
1953
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1875
Captain / Total hours on type:
50.00
Circumstances:
Upon landing, the twin engine airplane landed hard and bounced. Out of control, it veered off runway and came to rest in flames. A pilot was killed while the second occupant was seriously injured. The aircraft was destroyed by a post crash fire.
Probable cause:
Loss of control upon landing caused by a spontaneous and improper action on part of the copilot who was the pilot-in-command. The following factors were reported:
- Inadequate supervision of flight,
- Poor crew coordination,
- Improper level off,
- Full power recovery from bounced landing,
- Pilot later said that power was for go-around.
Final Report:

Crash of a Curtiss C-46A-30-CU Commando at McGuire AFB

Date & Time: Feb 13, 1960
Type of aircraft:
Registration:
N46Q
Survivors:
Yes
Schedule:
Louisville – McGuire
MSN:
26684
YOM:
1943
Crew on board:
3
Crew fatalities:
Pax on board:
54
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The Curtiss was being used for a civil air movement of military personnel from Louisville to McGuire AFB. En route, in the Elkins-Charleston area light to moderate icing occurred. This required the use of wing deicers and propeller anti-icers. Shortly after passing Baltimore the same weather conditions were encountered which required a power setting of 2400 rpm and 38" manifold pressure. The plane lost altitude, which forced the crew to apply METO power setting of 2600 rpm and 45" manifold pressure. During the final (GCA) approach to McGuire AFB the plane stalled and crash-landed 1200 feet short of the runway threshold. Both engines were sheared off on impact.
Probable cause:
Crew failed to maintain an accurate log of the flight as pertains to flight planning/fuel consumption/fuel requirements.

Crash of a Martin 404 in Louisville

Date & Time: Mar 10, 1957 at 1138 LT
Type of aircraft:
Operator:
Registration:
N453A
Survivors:
Yes
Schedule:
Chicago – Indianapolis – Louisville – Miami
MSN:
14144
YOM:
1952
Flight number:
EA181
Crew on board:
3
Crew fatalities:
Pax on board:
31
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7795
Captain / Total hours on type:
2151.00
Copilot / Total flying hours:
1201
Copilot / Total hours on type:
652
Aircraft flight hours:
15365
Circumstances:
Flight 181 originated at Midway Airport, Chicago, Illinois, for Miami, Florida. Several stops were scheduled including Indianapolis, Indiana, and Louisville, Kentucky, the latter a point of crew change. Departure, scheduled for 0955, was at 1001, with a crew of Captain Clarence G. Chambers, Pilot Harold D. Bingham, and Stewardess Shirley Michael. To Indianapolis the flight was routine, with Captain Chambers flying, and arrival was on schedule. Departure from Indianapolis was on schedule, at 1105, with 31 passengers and 450 gallons of fuel. The aircraft’s gross weight was 41,126 pounds, 3,774 less than the maximum takeoff allowable of 44,900, and its center of gravity was located within prescribed limits. Captain Chambers instructed Pilot Bingham to do the flying and, accordingly, Bingham, seated on the right, made the takeoff and flew this segment of the flight. The aircraft proceeded along V-53 airway at 5,000 feet altitude on a VFR flight plan in clear weather. At 1133 the flight advised Standiford (Louisville) tower that it was over New Albany, Indiana, eight miles to the north-northwest, and requested clearance to the airport. At 1134 the flight asked landing information of its company radio station and was given the Louisville pressure altitude as 340 feet and the Louisville altimeter setting as 30.10 inches. A minute later the flight advised the tower that it was over the city and received clearance to land on runway 11. Wind conditions were given as southeast five to eight knots, variable both sides. Ceiling and visibility were unlimited. The “Fasten Seat Belt” sign had been put on. Pilot Bingham descended from 5,000 feet to 2,000 feet and then reduced both rate of descent and power. An airspeed of 165 knots was established, the landing gear was lowered, and the flaps were placed in takeoff position. Bingham then started a turn for final approach, and the flaps were placed in approach position. Captain Chambers saw that the aircraft was too high and reduced power still further; Bingham lowered the flaps to full down. The pre-landing checklist had been accomplished. At this point (the altitude was then 1,000 to 1,500 feet higher than the runway) the captain took over control. He nosed down sharply, holding as closely as possible to an airspeed of 100 knots. The landing gear remained down, flaps remained fully down, and throttles were pulled fully back. Neither pilot read the rate-of-climb (descent) indicator during the approach. When approximately over the threshold of the runway and while about 100 feet above it, the captain pulled back on the yoke to flare out. No power was used. The aircraft’s attitude was observed to change from nose-down to nose-up but its rate of descent did not seem to lessen markedly. The aircraft struck the runway on its main landing gear, the left wing separated inboard of the left engine nacelle, and the remainder of the aircraft half rolled to an inverted position. It slid along in that attitude, turning and coming to rest headed nearly opposite its direction at touchdown. Two minutes later, by estimate, all occupants were out of their inverted seats, in which they were belted, and away from the wreckage which had developed a small fire. This was confined by a passenger using a hand extinguisher until emergency apparatus, which had been alerted by the tower, arrived quickly and took the necessary steps to prevent further fire.
Probable cause:
The Board determines that the probable cause of this accident was the captain’s faulty landing approach technique, resulting in an excessively high rate of sink at the instant of touchdown imposing load beyond the design strength of the wing stricture. The following findings were reported:
- An approach was started from a paint too close and too high in relation to the approach end of the runway,
- The speed and configuration of the aircraft in conjunction with the retarded throttle during this approach resulted in an inordinately high rate of descent,
- This high descent rate was not sufficiently checked during the attempted flareout,
- Touchdown imposed loads beyond the design strength of the wing structure, which failed.
Final Report: