Crash of a Beechcraft D18S in Huntington: 1 killed

Date & Time: Sep 25, 1985 at 0537 LT
Type of aircraft:
Registration:
N25Q
Flight Type:
Survivors:
No
Schedule:
Indianapolis - Huntington
MSN:
A-823
YOM:
1952
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3900
Captain / Total hours on type:
20.00
Circumstances:
The aircraft contacted the terrain with the left wing tip, cartwheeled and came to rest inverted during an ILS runway 12 approach at Huntington (HTS). Minimum approach visibility for the ILS is 3/4 of a mile. While en route the pilot was informed the HTS visibility was 1/8 of a mile. A missed approach was performed on the first ILS. During the missed approach climb the transponder code in the aircraft was changed to 7600. Radar data indicated that after the 2nd ILS approach, the aircraft made a climbing left turn. When approximately 2 miles southeast of the airport, at 2,100 feet, the aircraft made a sharp right turn. The radar target disappeared shortly thereafter. The aircraft contacted the terrain on a heading of 260° between runway 30 and the parallel taxiway. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: in flight collision with terrain/water
Phase of operation: circling (ifr)
Findings
1. Weather condition - below approach/landing minimums
2. (c) ifr procedure - improper - pilot in command
3. (c) procedures/directives - not followed - pilot in command
4. (c) missed approach - not performed - pilot in command
5. Air/ground communications - improper use of - pilot in command
Final Report:

Crash of a Beechcraft E18S in Huntington

Date & Time: Jan 31, 1985 at 2045 LT
Type of aircraft:
Operator:
Registration:
N95HA
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Huntington - Louisville
MSN:
BA-148
YOM:
1956
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7022
Captain / Total hours on type:
3000.00
Aircraft flight hours:
5877
Circumstances:
3-4 inch snow accumulation on aircraft prior to flight. Pilot said he swept snow off except an area he could not reach. Heavy snowfall, wet snow reported as aircraft was prepared for departure, during runup, taxi and takeoff. Pilot advised by tower that visibility was 1/8 mile with fog and snow. Published takeoff minimum for far 135 opn was 1/2 mile. After riking snowplow located 150 feet left of runway, aircraft continued over embankment and came to rest inverted. Ice and snow fnd on upper tail surface. Elevator trim indicated full nose down. Aileron trim ind left bank. Witnesses said engines sounded normal, landing lights on, 600 feet visibility from position of snowplow. Pilot said 35 inches map when descending. Map increased with additional throttle. No engine roughness.
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: takeoff - initial climb
Findings
1. (f) light condition - dark night
2. (f) weather condition - fog
3. (f) weather condition - snow
4. (c) ice/frost removal from aircraft - inadequate - pilot in command
5. (f) proper assistance - not obtained - pilot in command
6. (f) weather condition - below approach/landing minimums
7. (f) ifr procedure - disregarded - pilot in command
8. Terrain condition - snow covered
9. Airspeed(vs) - not maintained - pilot in command
----------
Occurrence #2: in flight collision with object
Phase of operation: takeoff - initial climb
Findings
10. Object - vehicle
Final Report:

Crash of a Douglas DC-9-31 in Huntington: 75 killed

Date & Time: Nov 14, 1970 at 1936 LT
Type of aircraft:
Operator:
Registration:
N97S
Survivors:
No
Schedule:
Kinston - Huntington
MSN:
47245/510
YOM:
1969
Flight number:
SO932
Crew on board:
4
Crew fatalities:
Pax on board:
71
Pax fatalities:
Other fatalities:
Total fatalities:
75
Captain / Total flying hours:
18557
Captain / Total hours on type:
2194.00
Copilot / Total flying hours:
5872
Copilot / Total hours on type:
1196
Aircraft flight hours:
3667
Circumstances:
The airplane departed Kinston-Stallings Field, North Carolina, at 1838LT on a charter flight to Huntington, West Virginia, carrying players and fans of the Marshall University Football Team based in Huntington. Following an uneventful flight, the crew contacted Huntington Approach Control at 1923LT and was cleared for a runway 11 localizer approach. At 1934LT, the airplane passed the Outer Marker and the crew was cleared to land. In marginal weather conditions (mist and rain), the airplane descended below the minimum descent altitude and the crew failed to realize his altitude was too low when the aircraft struck trees and crashed in flames on the slope of a hill located one mile short of runway 11 threshold. The aircraft was totally destroyed by impact forces and a post crash fire and none of the 75 occupants survived the crash. At the time of the accident, there were scattered clouds at 300 feet, broken overcast at 500 feet and solid overcast at 1,000 feet. Among the 75 occupants were 36 players, nine coaches and administrators, 26 fans and four crew members.
Probable cause:
The descent below Minimum Descent Altitude during a non precision approach under adverse weather conditions, without visual contact with the runway environment. The Board has been unable to determine the reason for this descent, although the two most likely explanations are: a) improper use of cockpit instrument data; or b) an altimetry system error.
Final Report:

Crash of a Beechcraft U-8F Seminole in Huntington: 3 killed

Date & Time: Oct 29, 1970
Type of aircraft:
Operator:
Registration:
62-3865
Flight Type:
Survivors:
Yes
Schedule:
Fort Meade - Huntington
MSN:
LF-63
YOM:
1962
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
The twin engine airplane was completing a liaison flight from Fort Meade, MD, to Huntington, WV. While approaching Huntington-Tri-State Airport by night and in heavy rain falls, the aircraft went out of control and crashed on final. One passenger was injured while three other occupants were killed, among them Major General Edwin H. Burba, Deputy Commander of the 1st Army.
Crew:
Cw2 Paul R. Burtt, pilot,
Cw3 Maynard V. Reisinger, copilot.
Passengers:
MG Edwin H. Burba +1.
Probable cause:
The accident was the consequence of a fatal design flaw in the fuel cross feed system.