Crash of a Piper PA-31T Cheyenne in Richlands: 3 killed

Date & Time: Jul 29, 1981 at 1030 LT
Type of aircraft:
Operator:
Registration:
N47CC
Survivors:
No
Site:
Schedule:
Birmingham - Asheboro - Richlands
MSN:
31-7820016
YOM:
1978
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
11000
Circumstances:
While descending to Richlands Airport, the pilot cancelled his IFR flight plan and continued under VFR in marginal weather conditions. About one minute later, the twin engine airplane struck the slope of an obscured mountain ridge and crashed. All three occupants were killed.
Probable cause:
Controlled collision with ground due to improper IFR operation. The following contributing factors were reported:
- Low ceiling,
- Fog,
- No published instrument approach at destination.
Final Report:

Crash of a Piper PA-61P Aerostar in Roanoke: 1 killed

Date & Time: Mar 23, 1981 at 1003 LT
Registration:
N3641U
Flight Phase:
Survivors:
No
Schedule:
Roanoke - Winchester
MSN:
61-0820-8063429
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4352
Captain / Total hours on type:
79.00
Circumstances:
After takeoff from Roanoke-Woodrum Field, while climbing, both engines lost power. The airplane stalled and crashed near the airport. The pilot, sole on board, was killed.
Probable cause:
Engine failure or malfunction due to improperly serviced aircraft by ground crew. The following contributing factors were reported:
- Improper fuel grade,
- Evasive maneuver to avoid collision,
- Inadequate supervision/training of ramp crews,
- Forced landing off airport on land,
- Aircraft refueled 8 of March with 100LL and 20 of March with Jet A by same individual on overtime due to supervisor illness.
Final Report:

Crash of a Piper PA-31-310 Navajo in Culpeper: 1 killed

Date & Time: Sep 10, 1980 at 0530 LT
Type of aircraft:
Registration:
N6702L
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Culpeper – Chantilly – Baltimore
MSN:
31-592
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4601
Captain / Total hours on type:
223.00
Circumstances:
Shortly after a night takeoff from Culpeper Airport, while in initial climb, the twin engine airplane baked right then lost height, struck trees and crashed in a wooded area, bursting into flames. The pilot, sole on board, was killed.
Probable cause:
Powerplant failure during initial climb for undetermined reasons. The following findings were reported:
- High obstructions,
- Still dark at the time of the accident,
- Right engine found shut down and its propeller feathered at impact.
Final Report:

Crash of a Learjet 23 in Richmond: 2 killed

Date & Time: May 6, 1980 at 0312 LT
Type of aircraft:
Registration:
N866JS
Flight Type:
Survivors:
No
Schedule:
Richmond – Louisville – Gainesville – Richmond
MSN:
23-018
YOM:
1965
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
2547
Captain / Total hours on type:
301.00
Copilot / Total flying hours:
905
Copilot / Total hours on type:
10
Aircraft flight hours:
4861
Circumstances:
On May 5, 1980, an unmodified Gates Learjet 23 (N866JS) was operated by Kennedy Flite Center, Richmond, Virginia, on a purported crew training flight. The pilot called the Newport News, Virginia, flight service station (FSS) about 2105 and received a weather briefing for a flight originating in Richmond to Louisville, Kentucky, continuing to Gainesville, Florida, and returning to Richmond. He filed three instrument flight rules (IFR) flight plans. The first flight plan called for a flight of 1+00 hour from Richmond to Louisville with the pilot and copilot aboard. The second flight plan called for a flight of 1+29 hours from Louisville to Gainesville with the pilot, copilot, and six passengers aboard. The third flight plan called for a flight of 1+10 hours from Gainesville to Richmond with the pilot and copilot aboard. All of the plans requested flight level (FL) 410 as an en route altitude. N866JS departed Richmond about 2128 with the two pilots aboard, and arrived at Standiford Field in Louisville at 2228 after a routine flight. The aircraft was refueled with 386 gallons of Jet A fuel costing $479.46, which was paid by check. The flightcrew boarded the six passengers, who were friends of the copilot according to the company's flight manager, and the aircraft departed Louisville at 2315. After a routine flight, the aircraft arrived at Gainesville Regional Airport at 0044, May 6, 1980, and the passengers deboarded. Charter Air Center service personnel "topped off" the fuel tanks with 404 gallons of Jet A fuel. The fuel bill was $596.63, which was paid in cash. The flight departed Gainesville at 0152. Initial climb was to 23,000 feet with further clearance to FL 370 and final clearance to the requested FL 410. The en route portion of the flight proceeded normally, and at 0257, during descent, the aircraft was handed off at 14,000 feet by the Washington Air Route Traffic Control Center to Richmond approach control. The Richmond approach controller acknowledged the handoff, gave current weather and wind conditions, and told the flightcrew to expect a visual approach to runway 2 at the Byrd International Airport. The flightcrew requested an instrument landing system (ILS) approach to runway 33. This request was acknowledged, and the approach controller vectored the aircraft to the ILS final approach course, outside of the outer marker, at 2,000 feet. The approach controller turned the aircraft over to the local control tower operator at 0308. Radio communication between the aircraft and the tower controller was established, and the aircraft was cleared to land at 0308:41. While on final approach at about 2 miles from the runway, the pilot asked for a wind check, and the controller responded that the winds were calm. About 0311:10, the flightcrew requested that the sequenced flashing approach lights be turned down and the controller asked that the message be repeated. The controller heard two garbled radio transmissions within 40 seconds referring to lights, and he dimmed the lights when the aircraft was about 0.5 mile from the runway. The tower controller stated that the aircraft's flightpath appeared higher than normal and that N866JS seemed, to float down the runway at about 50 feet altitude. He then'saw the wingtip lights rocking back and forth, the nose of the aircraft rising, and the aircraft starting to roll. He stated that he reached for the crash phone when he saw the wings rocking because he was concerned about the safety of the aircraft. He then saw a ball of fire on runway 33 and immediately sounded the crash alert; the time was 0311:58. A Virginia Air National Guard security guard on duty near an aircraft parking ramp and the "M" taxiway adjacent to runway 33 witnessed the accident. He stated that he was in a parked truck, engine off, with an unobstructed view of the runway approach zone and touchdown area. He said that the aircraft was "a bit high" on its approach, but descended to a normal touchdown attitude and altitude with the noise of the engines winding down. He did not hear the "screech" of the tires which would have been normal if the aircraft touched the runway. Instead, he said that the aircraft yawed right, the nose came up, and the aircraft started to roll to the right. The roll continued to the inverted position accompanied by a buildup of engine noise. He then saw the aircraft strike the ground inverted, catch fire, and explode. Another security guard on duty at the entrance to the Air National Guard base also witnessed part of the accident sequence. He observed the approach to runway 33 and stated that he thought the aircraft was landing farther down the runway than normal. He did not hear the aircraft touch down, but did hear a sudden rise of engine noise. He saw a white light traveling down the runway followed by an orange fireball and flames. The aircraft was totally destroyed and both pilots were killed.
Probable cause:
The pilot's failure to maintain proper airspeed and aircraft attitude while transitioning from final approach through flare to touchdown. The low-speed/high angle-of attack flight condition precipitated wing rolloff, wingtip strikes, and ultimate loss of aircraft control. The pilot's improper technique during roundout may have been due to fatigue, his limited knowledge, training, and experience regarding the flight characteristics of the Learjet aircraft, and distraction caused by concern over the intensity of the approach lighting.
Final Report:

Crash of a Piper PA-31-300 Navajo in Appomattox

Date & Time: Feb 29, 1980 at 1030 LT
Type of aircraft:
Operator:
Registration:
N77QC
Flight Phase:
Survivors:
Yes
Schedule:
Norfolk - Roanoke
MSN:
31-511
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3330
Captain / Total hours on type:
1027.00
Circumstances:
While in cruising altitude on a taxi flight from Norfolk to Roanoke, the pilot informed ATC about a double engine failure and elected to divert to the nearest airport. Shortly later, he decided to attempt an emergency landing when the airplane crashed in an open field. Both occupants were slightly injured and the aircraft was damaged beyond repair.
Probable cause:
Douglas engine failure in flight due to inadequate preflight preparation on part of the pilot. The following contributing factors were reported:
- Mismanagement of fuel,
- Fuel exhaustion,
- Powerplant-instruments: fuel quantity gauge, improperly alignment/adjustment,
- Forces landing off airport on land,
- Fuel gauges read 1/8 full, tanks empty.
Final Report:

Crash of a Cessna 421A Golden Eagle I in Norfolk

Date & Time: Aug 5, 1979 at 1630 LT
Type of aircraft:
Registration:
N3126K
Survivors:
Yes
Schedule:
Myrtle Beach - Farmingdale
MSN:
421A-0107
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8000
Circumstances:
En route from Myrtle Beach to Farmingdale, the pilot encountered engine problems, informed ATC about his situation and was vectored to Norfolk for an emergency landing. The aircraft descended from 8,000 to 3,000 feet when the pilot realized he could not reach Norfolk Airport. He attempted an emergency landing when the aircraft crash landed in an open field. Both occupants were seriously injured and the aircraft was destroyed.
Probable cause:
Engine failure during normal cruise due to piston rings failure. The following contributing factors were reported:
- Material failure,
- Failed to maintain flying speed,
- Improper in-flight decisions,
- Complete engine failure,
- Forced landing off airport on land,
- N° two cylinder piston failed,
- Pilot descended from 8,000 to 3,000 feet 12 miles from field with right engine shut down.
Final Report:

Crash of a Hawker-Siddeley HS.125-600A in McLean: 4 killed

Date & Time: Apr 28, 1977 at 2038 LT
Type of aircraft:
Registration:
N40PC
Flight Phase:
Survivors:
No
Site:
Schedule:
Washington DC - Birmingham
MSN:
256010
YOM:
1973
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
7807
Captain / Total hours on type:
1900.00
Copilot / Total flying hours:
4049
Copilot / Total hours on type:
114
Aircraft flight hours:
1904
Circumstances:
The airplane departed Washington-National Airport bound for Birmingham, Alabama. Four minutes later, while climbing to an altitude of 9,300 feet, monitoring radar stations lost continuous reception of the aircraft's primary and secondary radar target information. Shortly thereafter, ground witnesses saw an explosion in the sky followed by the wreckage of the aircraft falling to the ground. the sky was overcast and light rain was falling. The four persons aboard were killed and the aircraft was destroyed. One residence and two automobiles were destroyed by impact and fire and several other homes were damaged by falling debris.
Probable cause:
A failure or malfunction of an undetermined nature in the pilot's attitude indicating system which led to a loss of control and overstress of the aircraft structure.
Final Report:

Crash of a Cessna 401B in Hot Springs

Date & Time: Oct 24, 1976 at 0805 LT
Type of aircraft:
Registration:
N2WP
Survivors:
Yes
Schedule:
Columbia - Hot Springs
MSN:
401B-0104
YOM:
1969
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6400
Captain / Total hours on type:
1000.00
Circumstances:
While descending to Hot Springs-Ingalls Field Airport, the crew encountered poor weather conditions with low ceiling, rain falls and fog. The twin engine airplane passed below the decision height when it struck trees and crashed. All six occupants were rescued and the aircraft was destroyed.
Probable cause:
Collision with trees on final approach due to improper IFR operation. The following contributing factors were reported:
- Low ceiling,
- Rain,
- Fog,
- Descended below decision height.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain off Hampton: 4 killed

Date & Time: Oct 20, 1976 at 1908 LT
Registration:
N61436
Survivors:
No
Schedule:
Washington DC - Newport News - Baltimore
MSN:
31-7405465
YOM:
1974
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
2646
Captain / Total hours on type:
180.00
Circumstances:
While descending to Newport News-Williamsburg Airport on a schedule flight from Washington DC, the right engine failed. The crew lost control of the airplane that entered a dive and crashed into the sea off Hampton, about 12,5 miles southeast of the airport. The aircraft was lost and all four occupants were killed (the copilot's body was never recovered).
Probable cause:
Uncontrolled descent during initial approach due to engine structure failure (valve assemblies). The following contributing factors were reported:
- Diverted attention from operation of aircraft,
- Electrical system: generators/alternators,
- Failed to use or incorrectly used miscellaneous equipment,
- Aircraft came to rest in water,
- N°5 cylinder on right engine, exhaust valve would not seat,
- Right engine alternator bracket failed.
Final Report:

Crash of a Gulfstream GII in Hot Springs: 11 killed

Date & Time: Sep 26, 1976 at 1038 LT
Type of aircraft:
Operator:
Registration:
N500J
Survivors:
No
Schedule:
Trenton - Hot Springs
MSN:
60
YOM:
1969
Crew on board:
3
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
11
Captain / Total flying hours:
16982
Captain / Total hours on type:
523.00
Circumstances:
On approach to Hot Springs-Ingalls Field Airport, the crew encountered very poor weather conditions. On final, he failed to realize his altitude was too low when the airplane struck a mountain and crashed short of runway 24. The aircraft disintegrated on impact and all 11 occupants were killed. The wreckage was found 500 feet below the runway elevation. At the time of the accident, weather was poor with clouds down to 100 feet and fog.
Probable cause:
Controlled flight into terrain for undetermined reasons.
Final Report: