Crash of a Cessna 411 in Chilcoot: 4 killed

Date & Time: Mar 3, 1978 at 1940 LT
Type of aircraft:
Registration:
N3212R
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
San Jose - Truckee
MSN:
411-0212
YOM:
1966
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
151
Captain / Total hours on type:
69.00
Circumstances:
While flying in poor weather conditions, the pilot lost control of the airplane that entered an uncontrolled descent and crashed in flames in an uninhabited area located in the region of Chilcoot. The aircraft was destroyed and all four occupants were killed.
Probable cause:
Uncontrolled descent and subsequent uncontrolled collision with ground after the pilot initiated flight in adverse weather conditions and suffered a spatial disorientation. The following contributing factors were reported:
- Low ceiling,
- IFR flight conditions,
- VFR flight not recommended.
Final Report:

Crash of a Douglas DC-10-10 in Los Angeles: 2 killed

Date & Time: Mar 1, 1978 at 0925 LT
Type of aircraft:
Operator:
Registration:
N68045
Flight Phase:
Survivors:
Yes
Schedule:
Los Angeles - Honolulu
MSN:
46904
YOM:
1972
Flight number:
CO603
Crew on board:
14
Crew fatalities:
Pax on board:
186
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
29000
Captain / Total hours on type:
2911.00
Copilot / Total flying hours:
10000
Copilot / Total hours on type:
1249
Aircraft flight hours:
21358
Circumstances:
On March 1, 1978, Continental Air Lines, Inc., Flight 603, a McDonnell Douglas DC-10-10 (N68045), was a scheduled flight from Los Angeles International Airport, California, to Honolulu, Hawaii. At 0857:18, Flight 603 called Los Angeles clearance delivery and was cleared for the route of flight which was to have been flown. About 2 min later, the flight received permission from Los Angeles ground control to push back from the gate. At 0901:37, Flight 603 was cleared by ground control to taxi to runway 6R. The runway was wet, but there was no standing water. At 0922:29, Los Angeles local control cleared Flight 603 to taxi into position on runway 6R and hold. At 0923:17, local control cleared Flight 603 for takeoff; however, the flightcrew did not acknowledge the instructions and did not comply with them. At 0923:57, local acknowledged the instructions. The captain stated that he delayed control, again, cleared the flight for takeoff. This time the flightcrew acknowledgment of the takeoff clearance because he believed that he had initially been given the clearance too soon after a heavy jet aircraft had made its takeoff. The flightcrew stated that acceleration was normal and that all engine instruments were in the normal range for takeoff. As the airspeed approached the V1 speed of 156 kns, the captain heard a loud "metallic bang" which was followed immediately by "a kind of quivering of the plane." The flightcrew noticed that the left wing dropped slightly. A rejected takeoff was begun immediately; however, according to the digital flight data recorder (DFDR), the airspeed continued to increase to about 159 kns as the rejected takeoff procedures were begun. The captain stated that he applied full brake pressure while simultaneously bringing the thrust levers back to idle power. Reverse thrust levers were actuated and full reverse thrust was used. The flightcrew stated that they noted good reverse thrust. First, the aircraft moved to the left of the runway centerline and appeared tb the flightcrew to be decelerating normally. With about of deceleration had decreased, and they believed that the aircraft would 2,000 ft of runway remaining, the flightcrew became aware that the rate not be able to stop on the runway surface. The captain stated that he maintained maximum brake pedal force and full reverse thrust as he steered the aircraft to the right of the runway centerline in an effort "to go beside the stanchions holding the runway lights" immediately off of the departure end of runway 6R. He stated further that he encountered no problems with directional control of the aircraft throughout the rejected takeoff maneuver. The aircraft departed the right corner of the departure end of runway 6R. About 100 ft beyond the runway, the left main landing gear broke through the nonload-bearing tar-macadam (tarmac) surface and failed rearward. Fire erupted immediately from this area. The aircraft dropped onto the left wing and the No. 1 (left) engine and rotated to the left as it continued its slide along the surface. It stopped between two of the approach light stanchions for runway 24L about 664 ft from the departure end of runway 6R and about 40 ft to the right of the runway 6R extended centerline; it came to rest on a heading of 008°, in an 11° left wing low, 1.3° noseup attitude. When the aircraft came to a stop, the evacuation was begun immediately. Two passengers were killed while all other occupants were evacuated, some of them with serious injuries.
Probable cause:
The National Transportation Safety Board determined that the probable cause of the accident was the sequential failure of two tires on the left main landing gear and the resultant failure of another tire on the same landing gear at a critical time during the takeoff roll. These failures resulted in the captain's decision to reject the takeoff. Contributing to the accident was the cumulative effect of the partial loss of aircraft braking because of the failed tires and the reduced braking friction achievable on the wet runway surface which increased the accelerate-stop distance to a value greater than the available runway length. These factors prevented the captain from stopping the aircraft within the runway confines. The failure of the left main landing gear and the consequent rupture of the left wing fuel tanks resulted in an intense fire which added to the severity of the accident.
Final Report:

Crash of a Rockwell Aero Commander 500A near Solvang: 7 killed

Date & Time: Feb 28, 1978 at 1030 LT
Registration:
N6143X
Flight Phase:
Survivors:
No
Site:
Schedule:
Visalia – Santa Maria – Santa Barbara
MSN:
500-931-26
YOM:
1960
Crew on board:
3
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
17770
Captain / Total hours on type:
2440.00
Circumstances:
While cruising under VFR mode, the crew encountered limited visibility due to low ceiling and ground fog when the airplane struck the slope of a mountain located near Solvang. The aircraft was destroyed upon impact and all seven occupants were killed.
Probable cause:
Controlled flight into terrain after the crew continued VFR flight into adverse weather conditions. The following contributing factors were reported:
- Low ceiling,
- Ground fog.
Final Report:

Crash of a Douglas A-26A Invader in Chino

Date & Time: Feb 9, 1978 at 1300 LT
Type of aircraft:
Operator:
Registration:
N99218
Flight Type:
Survivors:
Yes
Schedule:
Mojave - Chino
MSN:
18796
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10000
Captain / Total hours on type:
1200.00
Circumstances:
On final approach to Chino Airport, the crew lost control of the airplane that crashed short of runway threshold. The aircraft was destroyed and both pilots were seriously injured. They were completing a ferry flight from Mojave.
Probable cause:
Loss of control on final approach after the n°2 propeller went into reverse thrust for undetermined reasons. The following contributing factors were reported:
- Thrust reversal unwanted,
- Material failure.
Final Report:

Crash of a Beechcraft 65-88 Queen Air in Camarillo: 3 killed

Date & Time: Aug 25, 1977 at 1600 LT
Type of aircraft:
Operator:
Registration:
N711KW
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Van Nuys - Van Nuys
MSN:
LP-38
YOM:
1966
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
5610
Captain / Total hours on type:
30.00
Circumstances:
The crew departed Van Nuys for a local test flight. En route, a fire erupted in the left wheel well and spread to the left wing that detached in flight. Out of control, the airplane entered a dive and crashed in flames. All three occupants were killed.
Probable cause:
In-flight fire during normal cruise for undetermined reasons. The following findings were reported:
- Fire in brakes, wheel assembly, wheel well,
- Fire in wing,
- Separation in flight,
- In-flight loss of left wing,
- Severe fire in left wheel well aft of left engine firewall, source undetermined.
Final Report:

Crash of a Beechcraft E18S on Catalina Island: 2 killed

Date & Time: Aug 22, 1977 at 2106 LT
Type of aircraft:
Registration:
N979SB
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Catalina Island - Long Beach
MSN:
BA-302
YOM:
1957
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
2460
Circumstances:
Shortly after takeoff from Catalina Island Airport, while in initial climb, the twin engine airplane went out of control and crashed on a mountainous area near the airport. The aircraft was destroyed and both occupants were killed.
Probable cause:
Uncontrolled collision with ground during initial climb after the crew suffered incapacitation. The following contributing factors were reported:
- Physical impairment,
- Failure of the air condition, heating and pressurization system,
- Fatigue fracture,
- Fog,
- 45% carbon monoxide in pilot, 16,8% in copilot,
- Cabin heater, cracks in the combustion chamber.
Final Report:

Crash of a Piper PA-31P Pressurized Navajo in Modesto: 3 killed

Date & Time: Aug 19, 1977 at 1153 LT
Type of aircraft:
Registration:
N7670L
Survivors:
Yes
Schedule:
San Francisco - Modesto
MSN:
31-7300151
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
6912
Captain / Total hours on type:
31.00
Circumstances:
On approach to Modesto City-County Airport, both engines failed simultaneously. The pilot attempted an emergency landing on a highway when the airplane struck an automobile and crashed. Both occupants on board the aircraft were slightly injured while three people were killed in the car.
Probable cause:
Double engine failure on final approach due to fuel exhaustion. The following contributing factors were reported:
- Inadequate preflight preparation,
- Mismanagement of fuel,
- Miscalculated fuel consumption,
- Fuel exhaustion,
- Forced landing off airport on land.
Final Report:

Crash of a Cessna 421A Golden Eagle I in San Rafael: 1 killed

Date & Time: Jul 7, 1977 at 1847 LT
Type of aircraft:
Operator:
Registration:
N29760
Flight Phase:
Flight Type:
Survivors:
No
MSN:
421A-0076
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
650
Captain / Total hours on type:
30.00
Circumstances:
At takeoff, the twin engine airplane stalled and crashed in flames. The pilot, sole on board, was killed.
Probable cause:
Stall on takeoff due to inadequate preflight preparation on part of the pilot. The following contributing factors were reported:
- Selected wrong runway relative to existing wind,
- Downwind,
- 2,000 feet runway, 15 knots tailwind.
Final Report:

Crash of a Rockwell Grand Commander 680FL in Upland: 5 killed

Date & Time: Jun 7, 1977 at 0740 LT
Registration:
N6853S
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Upland - San Diego
MSN:
680-367-53
YOM:
1956
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
1675
Captain / Total hours on type:
320.00
Circumstances:
After takeoff from Upland-Cable Airport in marginal weather conditions, the pilot reported problems with gyro when cruising at low in low ceiling, the airplane crashed into an airport complex. Four employees of the complex were injured while all five occupants of the airplane were killed.
Probable cause:
The airplane crashed after the pilot continued VFR flight into adverse weather conditions. The following contributing factors were reported:
- Improper in-flight decisions,
- Inadequate preflight preparation,
- Instruments/equipment and accessories - flight and navigation instruments: attitude gyro,
- Low ceiling,
- Fog,
- Low altitude flight in low ceiling area,
- Pilot declared gyros out, reason undetermined.
Final Report:

Crash of a Lockheed 18-56-23 LodeStar near Lone Pine

Date & Time: May 20, 1977
Type of aircraft:
Registration:
N20GY
Flight Type:
Survivors:
Yes
MSN:
2437
YOM:
1943
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Following an improper level off, the twin engine airplane crash landed near Lone Pine. The undercarriage collapsed on landing then the airplane slid on its belly and came to rest in flames. The pilot disappeared and was not found while the aircraft was destroyed by fire. It was engaged in a contraband flight.
Probable cause:
Improper level off and hard landing caused the undercarriage to fail.
Final Report: