Crash of a De Havilland DHC-2 Beaver near Kincolith: 5 killed

Date & Time: Aug 4, 1998 at 1758 LT
Type of aircraft:
Operator:
Registration:
C-FOCJ
Survivors:
No
Schedule:
Prince Rupert - Kincolith
MSN:
39
YOM:
1949
Flight number:
H3709
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
1700
Captain / Total hours on type:
1250.00
Aircraft flight hours:
22369
Circumstances:
The float-equipped de Havilland DHC-2 Beaver, serial number 0039, departed Prince Rupert, British Columbia, at 1719 Pacific daylight time on a visual flight rules flight to Kincolith, British Columbia, with the pilot and four passengers on board. When the aircraft arrived at Kincolith at about 1750, witnesses watched it carry out three low approaches to the water landing area, each time descending to a few feet above the water before climbing away. On the fourth approach, at about 1758, the aircraft touched down, apparently in a controlled manner, and skipped on the water surface. The floats then dug into the water followed by the right wing, which was severed from the fuselage on water impact. The aircraft quickly overturned and came to rest inverted with only the bottom of the floats visible. Several members of the village community, who had been waiting for the aircraft on the Government Dock, rushed to the sunken aircraft in small boats but were unable to rescue the pilot or passengers inside the submerged cabin. The five occupants drowned in the accident, and the aircraft was substantially damaged.
Probable cause:
On touchdown, the float(s) struck the water and caused a flying attitude that the pilot could not control before the right wing dug in and the aircraft overturned. Contributing to the accident were conflicting wind and water conditions at the time of the occurrence.
Final Report:

Crash of a Cessna 340A in Chicago: 1 killed

Date & Time: Aug 1, 1998 at 2200 LT
Type of aircraft:
Registration:
N5340F
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Chicago - Louisville
MSN:
340A-0667
YOM:
1978
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1600
Captain / Total hours on type:
500.00
Aircraft flight hours:
3036
Circumstances:
The pilot reported the airplane decelerated during the takeoff roll. He applied the brakes and as he advanced the throttles to full power the airplane accelerated. The airplane cleared the end of the runway then stalled into Lake Michigan, flipped inverted and sank. One passenger reported that it felt as if someone put on the brakes. One passenger drowned. The pilot used 32' of manifold pressure for takeoff versus 37.3' as placarded. The pilot operating handbook lists normal takeoff speed as 91 KIAS, however the airplane was equipped with vortex generators. The pilot reported looking for 105 to 110 KIAS for takeoff. No evidence was found of the pilot having a multi-engine rating. No evidence of a mechanical failure/malfunction was found.
Probable cause:
The pilot's improper use of the throttle in not using full power for takeoff, the pilot's failure to use proper aborted takeoff procedures, and the inadvertent stall/mush. A factor associated with the accident was inadequate preflight/planning by the pilot.
Final Report:

Crash of a Beechcraft 1900D off Quiberon: 14 killed

Date & Time: Jul 30, 1998 at 1558 LT
Type of aircraft:
Operator:
Registration:
F-GSJM
Flight Phase:
Survivors:
No
Schedule:
Lyon - Lorient
MSN:
UE-238
YOM:
1996
Flight number:
PRB706
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
12
Pax fatalities:
Other fatalities:
Total fatalities:
14
Captain / Total flying hours:
3072
Captain / Total hours on type:
1356.00
Copilot / Total flying hours:
1016
Copilot / Total hours on type:
361
Aircraft flight hours:
3342
Circumstances:
Following an uneventful flight from Lyon-Satolas Airport, the crew was approaching Lorient-Lann-Bihoué Airport when he contacted ATC and requested a special clearance to cancel his IFR flight plan for a visual circuit over the Bay of Quiberon to show the 'Norway' ship (ex France) to the passengers. While cruising under VFR mode in excellent weather conditions at an altitude of 2,000 feet, the twin engine aircraft collided with a private Cessna 177 Cardinal registered F-GAJE and owned by the Aéro Club de Vannes. Following the collision, both aircraft entered an uncontrolled descent and crashed in the Bay of Quiberon about 1,500 metres from the ship and 10 km off Quiberon. All 14 people on board the Beech 1900D as well as the pilot of the Cessna 177 were killed.
Probable cause:
The collision was due to the absence of visual detection of the other aircraft by each of the two crews in an uncontrolled Class G Airspace where collision avoidance relies exclusively on external vigilance ("See and Avoid" rule). The decision to change the flight regime and trajectory placed the crew of the Beech 1900D in an improvised and unusual flight situation with a public transport aircraft. The following contributing factors have been identified:
- The pilots, on different frequencies, were unaware of their mutual presence,
- The pilots had their attention focused on the ship 'Norway',
- The organization of the activity in the cockpit of the Beech 1900D and its ergonomics did not allow effective monitoring, particularly towards the outside of the turn,
- The dead angles of the Cessna 177 probably masked the Beech 1900D from its pilot while both aircraft were approaching each other,
- The position of the sun may have hampered the pilot of the Cessna 177,
- The Cessna 177 transponder was off, thus the aircraft could not be viewed on the ATC radar based in Lorient. As a result, he was unable to provide traffic information to the crew of the Beech 1900D.
Final Report:

Crash of an Embraer EMB-110P1 Bandeirante near Manacapuru: 12 killed

Date & Time: Jul 29, 1998 at 1300 LT
Registration:
PT-LGN
Flight Phase:
Survivors:
Yes
Schedule:
Manaus – Tefé
MSN:
110-343
YOM:
1982
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
24
Pax fatalities:
Other fatalities:
Total fatalities:
12
Captain / Total flying hours:
15000
Captain / Total hours on type:
8000.00
Copilot / Total flying hours:
2500
Copilot / Total hours on type:
2000
Circumstances:
The EMB-110 Bandeirante operated on a domestic flight from Manaus to Tefé, Brazil. Although the airplane was certificated for a maximum of 19 passengers, there were 25 passengers on board. Also, for financial reasons the crew decided to take more fuel than necessary for this flight. This resulted in the airplane departing with an excess of weight of 852 kg. About 20 minutes into the flight the oil pressure of the no. 2 engine dropped. The crew reduced engine power to 72% and continued to Tefé. When the flight was 185 km from Manaus at FL85 the oil pressure dropped to 40psi and the TGT increased. The copilot shut down the engine and the captain turned the airplane around, back to Manaus. At 13:15 the crew contacted Manaus ACC reporting that they were returning on one engine. The overloaded airplane flying on one engine, began to lose height. During the descent the speed was kept around 105 kts which occasionally caused activated stick shaker. To lose weight, the left overwing exit was opened and luggage of the passengers was jettisoned. The airplane did not make it to Manaus and an emergency landing on the Manacapuru River was made. The Bandeirante landed hard on the water, causing an opening in the fuselage. It sank quickly.
Probable cause:
The following factors were identified:
- It was not possible to examine the debris of the aircraft to determine the contribution of this factor to the failure of the left engine.
- It is possible that the failure to carry out a type B2 inspection and/or to carry out a type A1 inspection by an unqualified person may have contributed to the occurrence of a low oil pressure emergency, due to material deterioration or inadequate services. The impossibility of examining the aircraft could not determine this aspect.
- The owner of the air taxi company participated due to lack of adequate supervision in the planning of operations, at the technical, operational and administrative levels. This deficiency can be characterized, among other things, by the owner of the company that allowed the aircraft to fly with the type B2 inspection expired; by the excessive amount of fuel, when refueling in Manaus; by the unreasonable number of people on board, causing the aircraft to fly with excess weight, and still, by the receipt of pilots' salary to be conditioned to the accomplishment of the fateful flight.
- Errors were made by the aircraft crew due to the improper use of the resources available in the cabin, intended for the operation of the aircraft, due to non-compliance with operational rules.
- There was a mistake made by the crew due to the inadequate preparation for the flight, assuming numerous failures, such as: the non conference, by the pilots, of the cargo and passengers manifest; the lack of the realization of a briefing and still, to accept an aircraft for a flight, being the same with its inspection not carried out.
- An error was made by the crew due to inadequate evaluation of certain aspects of the flight. Such deficiency was evidenced when the first sign of failure of the lubrication system occurred, after twenty minutes of flight, and even so, they decided to proceed with the flight, when the most sensible and safe would be the return, immediately, to Manaus.
- The airline's support staff participated in the planning of weight and balance of the aircraft and the number of passengers on board, providing incorrect information to the aircraft's crew members. In addition, the mechanic who performed the A1 type inspection was not qualified for the function.
- There has been intentional non-compliance by the crew members with the operational rules established by the aircraft manufacturer.
- The Commander did not foresee what was predictable, for lack of caution, thus intentionally increasing the risk margin of the mission.
Final Report:

Crash of a Consolidated PBY-5A Catalina off Southampton: 2 killed

Date & Time: Jul 27, 1998 at 1444 LT
Type of aircraft:
Registration:
VP-BPS
Flight Type:
Survivors:
Yes
Schedule:
Southampton - Southampton
MSN:
1997
YOM:
1944
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
14
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
9935
Captain / Total hours on type:
151.00
Circumstances:
The aircraft had been booked for a static display and press 'photocall' at Southampton Airport, as part of the official launch of a project known as Seawings 2000. The aircraft operator had offered some short flights, free of charge, for the event organisers to use as they felt appropriate. Initial seat allocation was to the press, and members and officers of Southampton City Council. The remaining seats were offered to individuals representing organisations assisting the running of the project. The crew consisted of two pilots and two rear crew; one of the latter was designated 'crew chief'. There were two passenger compartments separated by a central compartment which had a door in the front bulkhead. Each passenger compartment was configured with eight seats, four either side of a central aisle. The front seats in each compartment were aft facing. The seats were typical airline type and had a standard lap belt restraint; a lifejacket was stowed under each seat. There was a bench type seat in each rear blister; however, these did not have restraint belts. On land, the aircraft is normally entered/vacated via ventral stairs, however, this access is not available when on water. There is a window type hatch between the seats on the left side of the front compartment. This is hinged at the top and opens upwards and outwards. To the rear and either side of the aft compartment there are two observation blisters which open upward in an 'eyelid' fashion. All three exits can be used for emergency egress. Emergency egress from the flight deck is through a removable hatch above the co-pilot's head.
Probable cause:
Because the nose gear doors were not recovered, it is not possible to exclude the possibility that the aircraft encountered a significant piece of flotsam which caused the doors to collapse inwards. Regardless of this, the presence of the severe corrosion in the nose gear operating mechanism torque tube can only have served to compromise the ability of the left door to resist the range of loads which might have been imposed during a water landing. The corrosion found in the torque tube had clearly developed over a long time but it went undetected because it was inside a closed area and no specific inspection of the inside of the tubes was called for. When looking at another Catalina, it was observed that there were no bungs in the aft ends of the torque tubes and it would have been possible, with suitable apparatus, to inspect the whole of the inside of the tube assemblies, particularly in the zone where the tube failed on this occasion. The Maintenance Manual and Schedule for the Catalina were developed and written in a different age when these aircraft were very differently utilised. Although both the Manual and Schedule have been developed as a result of the Catalina's continued amphibious operation, for probably much longer than originally envisaged, there are now likely to be some time related maintenance considerations which did not previously exist.
Final Report:

Crash of an Ilyushin II-76MD off Ra's al-Khaimah: 8 killed

Date & Time: Jul 13, 1998 at 2315 LT
Type of aircraft:
Operator:
Registration:
UR-76424
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Ra's al-Khaimah - Mykolaiv
MSN:
00834 81440
YOM:
1988
Flight number:
TII2570
Region:
Crew on board:
8
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
8
Aircraft flight hours:
3569
Aircraft flight cycles:
1978
Circumstances:
The aircraft was engaged in a cargo flight from Ras al-Khaimah to Mykolaiv, carrying eight crew members and a load of various goods among them few tons of water melons. Following a night takeoff from runway 34 at a speed of 235 km/h, the aircraft reached the altitude of 150 metres at a speed of 365 km/h then continued to 160 metres at a speed of 400 km/h. The crew raised the flaps in five steps when the aircraft entered an uncontrolled descent with a rate of 12 metres per second until it impacted the sea at a speed of 485 km/h about 16 km from the airport, some 800 metres offshore. The aircraft disintegrated on impact and all eight occupants were killed.
Probable cause:
It was determined that the aircraft was overloaded by 15-25 tons regarding the actual flight conditions and 13-23 tons regarding the MTOW as published in the manuals. At the time of the accident, the OAT was +37° C, reducing climb and flight performances.

Crash of a Piper PA-31-350 Navajo Chieftain off Jersey: 1 killed

Date & Time: Jun 12, 1998 at 1842 LT
Operator:
Registration:
CN-TFP
Flight Type:
Survivors:
No
Schedule:
Tangier - Saint Peter
MSN:
31-7552086
YOM:
1975
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
9100
Aircraft flight hours:
5253
Circumstances:
The pilot, sole on board, departed Tangier on a delivery flight to Saint Peter-La Villiaze, Guernsey Island, where the aircraft should be taken over by another crew to be ferried to Iceland. While approaching the Channel Islands, the pilot informed ATC about technical problems and elected to divert to Jersey Airport. Shortly later, after both engines stopped due to a fuel exhaustion, the plane lost height and crashed in the sea about 3 nm northwest of Jersey Island. The aircraft was destroyed and the pilot was killed.
Probable cause:
The following causal factors were identified:
- The commander had not made an appropriate allowance for adverse headwind components before or during the flight.
- The aircraft was not carrying sufficient fuel for the intended flight.
- The commander apparently ignored pre-flight and in-flight indications that he should land and refuel in France.
- The commander's chances of survival were adversely affected by not adopting the optimum configuration and heading for ditching.
Final Report:

Crash of a Cessna 421B Golden Eagle II in Nassau

Date & Time: May 11, 1998 at 1349 LT
Registration:
N17BN
Survivors:
Yes
Schedule:
Charlotte Amalie – Nassau
MSN:
421B-0396
YOM:
1973
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On May 11, 1998, about 1349 eastern daylight time, a Cessna 421B, N17BN, registered to Quinn Industries, Inc., operating as a 14 CFR 91 personal flight, crashed into Lake Killarney, New Providence Island, Bahamas, while on approach for landing to Nassau International Airport. Visual meteorological conditions prevailed and no flight plan was filed. The airplane received unknown damage, the pilot suffered serious injuries, and two passengers suffered minor injuries. The flight originated about 26 minutes before the accident. According to initial reports, the flight originated earlier that day from St. Thomas, Virgin Islands, with a stop at Governor's Harbour, Eleuthera, for refueling. Upon landing at Governor's Harbour, the pilot was advised no fuel was available and elected to proceed to Nassau for refueling. Some time during the straight-in approach the pilot transmitted he was "low on fuel", and N17BN crashed about 400 yards short of the runway into a swamp.

Crash of a Cessna 421C Golden Eagle III off Monaco: 4 killed

Date & Time: Apr 10, 1998 at 1320 LT
Operator:
Registration:
D-IALE
Flight Type:
Survivors:
Yes
Schedule:
Bad Vöslau - Nice
MSN:
421C-0635
YOM:
1974
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The twin engine aircraft departed Bad Vöslau Airport at 0900LT on a private flight to Nice. While approaching Nice-Côte d'Azur Airport in poor weather conditions, the aircraft suffered a double engine failure. The pilot attempted to ditch the aircraft that crashed one nautical mile off Monaco. Four passengers were killed while four other occupants were rescued, among them the pilot, his wife and daughter. The aircraft sank and its wreckage was found four days later at a depth of 165 metres. At the time of the accident, weather conditions were poor with heavy rain falls and hail.
Probable cause:
Double engine failure due to fuel exhaustion.

Crash of a Rockwell Grand Commander 680 in the Atlantic Ocean: 1 killed

Date & Time: Apr 9, 1998
Operator:
Registration:
4X-CCS
Flight Phase:
Flight Type:
Survivors:
No
MSN:
680-1731-138
YOM:
1968
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The pilot, sole on board, departed Southend on a ferry flight to Canada with an intermediate stop in Greenland. En route, he reported to ATC severe icing conditions. Shortly later, the aircraft entered an uncontrolled descent and crashed in the Atlantic Ocean about 167 km southeast of the Greenland coast. The pilot was killed.