Crash of a Rockwell Aero Commander 560E in Dallas: 7 killed

Date & Time: Sep 27, 1967 at 1536 LT
Operator:
Registration:
N3831C
Survivors:
No
Site:
MSN:
560-747
YOM:
1959
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
13247
Captain / Total hours on type:
2010.00
Circumstances:
While on approach to Dallas-Love Field Airport, the left wing broke away and control was lost. The airplane entered a dive and crashed on the elementary school of Bradfield. All seven occupants on board the airplane were killed while no one on the ground was injured. The school was partially destroyed as well as several vehicles. The airplane was operated on behalf of LTV Electrosystems (Ling-Temco-Vought).
Probable cause:
Uncontrolled descent following the structural failure of the left wing due to fatigue fracture. Two overlapping rivet holes found in aft leg of the spar cap.
Final Report:

Crash of a Douglas DC-3A-197D in La Paz: 5 killed

Date & Time: Jun 12, 1967
Type of aircraft:
Operator:
Registration:
XA-FUW
Flight Phase:
Survivors:
Yes
Site:
Schedule:
La Paz - Mazatlán
MSN:
3260
YOM:
1940
Country:
Crew on board:
4
Crew fatalities:
Pax on board:
24
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
Shortly after takeoff from La Paz-Manuel Márquez de León Airport, while climbing, one of the engine failed. The pilot-in-command lost control of the airplane that stalled and crashed in a residential area. Three crew members and two people on the ground were killed while 25 other occupants were injured.
Probable cause:
Engine failure after takeoff.

Crash of a Tupolev TU-16 in Afula: 17 killed

Date & Time: Jun 6, 1967
Type of aircraft:
Operator:
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Habbaniyah - Habbaniyah
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
17
Circumstances:
On a mission against the Israeli air base of Ramat David when missed the target, bombed the town of Netanya instead (hitting the main street and injuring a number of civilians). Was shot down by 40 mm Bofors L/70 anti-aircraft guns of the Israeli Unit 881 while at low altitude and crashed into a military storage complex hidden within a pine forest located west of Afula. All 6 crew, among them Captain Hussein Mohammad Husseini, and 11 or 14 Israeli reservists on the ground were killed.
Probable cause:
Shot down by Israel antiaircraft battery.

Crash of a Canadair C-4 Argonaut in Manchester: 72 killed

Date & Time: Jun 4, 1967 at 0909 LT
Type of aircraft:
Operator:
Registration:
G-ALHG
Survivors:
Yes
Site:
Schedule:
Palma de Majorca - Manchester
MSN:
153
YOM:
1949
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
79
Pax fatalities:
Other fatalities:
Total fatalities:
72
Captain / Total flying hours:
10197
Captain / Total hours on type:
2009.00
Copilot / Total flying hours:
1001
Copilot / Total hours on type:
136
Circumstances:
The aircraft was on a non-scheduled international flight from Manchester to Palma and return. It landed at Palma at 0220 hours GMT, was refuelled and took off for Manchester at 0406 hours GMT. The co-pilot was flying the aircraft from the right-hand seat and the flight was uneventful - between 0856 hours and 0900 hours the aircraft was descending for approach and landing and was being vectored towards the ILS localizer. At 0901:30 hours the flight was informed that it was 9 miles from touchdown and well left of the centre line and it was asked if it was receiving the ILS. The pilot-in-command replied that he was and would turn right a little. Shortly thereafter one engine, most probably No. 4, ceased to deliver power, followed some 15 seconds later by the other engine on the same side. The pilot-in-command took over the controls and just after 0903 hours the Controller told the flight that it was 6 miles from touchdown and asked if it was established on the ILS localizer. This message was not acknowledged by the flight and 7 seconds later the Controller asked if it was still receiving. The pilot-in-command then replied "Hotel Golf is overshooting, we've got a little bit of trouble with rpm". The aircraft's indicated air speed was then only 116 kt and its height 1 838 ft AMSL. The Controller then ordered the pilot-in-command to turn left on to 160'~ and climb to 2 500 ft QNH. He then asked the reason for overshooting and was told "We've a little bit of trouble with rpm, will advise you". At 0903:51 hours the pilot-in-command asked what the left turn was on to. The Controller noted that the aircraft had already turned through 25' to the right instead of to the left, so he ordered the pilot to continue turning right on to 020' and climb to 2 500 ft on QNH. This was acknowledged by the co-pilot. At 0904:41 hours the Controller asked the flight to advise when ready to recommence the approach. By this time the aircraft's IAS had dropped to 111 kt, its height to 1 287 ft ONH, and it had broken cloud and was seen by an eyewitness. Thereafter it flew below cloud in conditions of reasonable visibility. At 0905:26 hours the Controller told the flight that it was 7 miles from the airfield on a bearing of 040' and requested its height. The flight reported at 1 000 ft. This was the first indication to the Controller that the aircraft was faced with an emergency and after checking that the height given was correct he put full emergency procedure into operation at the airfield and ordered the aircraft to turn right on to 180 M, so that it would close the ILS localizer. At 0905:47 hoursthe Controller asked the flight if it could maintain height. The pilot-in-command now at 981 ft AMSL and only some 800 ft above the ground replied "just about". He was told he was 8 miles from touchdown and should continue his right turn on to 200% and maintain as much height as possible. At this point 341 ft of height were lost in 10 seconds after the IAS had fallen to 100 kt and the pilot-in-command said he was not able to maintain height at the moment. The Controller told him that he was 8 miles from touchdown and closing the ILS localizer from the right. At 0907:09 hours, the Controller informed the flight that radar contact had been lost due to the aircraft's low height and asked the pilot to adjust his heading on the ILS and report when established. The co-pilot replied that they had "the lights to our right'' and were at 800 ft, just maintaining height, and the pilot-in- command asked for the emergency to be laid on. At 0907:35 hours the pilot-in-command requested his position and was told 7; miles to run to touchdown. Half a minute later the Controller repeated that he had no radar contact, and cleared the flight for landing, the surface wind being 270°/12 kt. At this stage the PAR Controller, who had overheard that the Approach Controller had lost radar contact, saw a contact at the bottom of his elevation display, and told the flight that it was 6 miles from touchdown. The co-pilot then gave their altitude as being 500 ft. The terrain clearance was only 300 ft and the IAS was below 105 kt and falling. The aircraft was approximately on the line of the ILS localizer and heading for the very centre of the built up area of Stockport. A few seconds after 0909 hours the aircraft struck the ground more or less level in pitch, slightly right wing down, and slightly yawed to the right. From the evidence of two eyewitnesses who saw the aircraft just before the crash it was clear the pilot-in-command deliberately cut the power very shortly before impact and deliberately put the aircraft down on what was the only pocket handkerchief of relatively open space available, immediately before tall blocks of flats, the town hall, the police station, and Stockport Infirmary. Three crew members and 69 passengers were killed while 12 other occupants were injured.
Probable cause:
The immediate cause of the accident was loss of power of both engines on the starboard side resulting in control problems which prevented the pilot from maintaining height on the available power with one propeller windmilling. The loss of power of the first engine was due to fuel starvation due to inadvertent fuel transfer in flight. The loss of power of the second engine was due either to fuel starvation resulting from inadvertent fuel transfer in flight or to misidentification by the crew of which engine had failed followed by failure to restore power in time to the engine misidentified as having failed. Contributory causes of the accident were:
- The design of the fuel valves and location in the cockpit of their actuating levers, so that a failure by the pilot correctly to position the lever by an amount so small as to be easy to do and difficult to recognize would result in inadvertent fuel transfer on a scale sufficient to involve the risk after a long flight of a tank expected to contain sufficient fuel being in fact empty,
- Failure of those responsible for the design of the fuel system or the fuel valves to warn users that failure by a small amount to place the actuating levers in the proper position would result in inadvertent fuel transfer on a scale involving this risk after a long flight,
- Failure of British Midland's air crew or engineers to recognize the possibility of inadvertent fuel transfer in the air from the evidence available in previous incidents in flight and contained in the fuel logs,
- Failure of other operators of Argonauts who had learned by experience of the possibility of inadvertent fuel transfer in flight to inform the Air Registration Board, the Directorate of Flight Safety of the Board of Trade or its predecessors, or the United Kingdom Flight Safety Committee of the facts which they had learned so that these might be communicated to other operators of Argonauts and other aircraft equipped with similar systems and fuel cocks.
Final Report:

Crash of a Curtiss C-46 Commando in Seoul: 59 killed

Date & Time: Apr 8, 1967 at 1100 LT
Type of aircraft:
Operator:
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Seoul - Daegu
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
12
Pax fatalities:
Other fatalities:
Total fatalities:
59
Circumstances:
After takeoff from Yeouido AFB in Seoul, while climbing to Daegu in poor weather conditions, the captain informed ATC about the failure of the left engine and elected to return for an emergency landing. Shortly later, the airplane went out of control and crashed in a huge explosion in the district of Kum Ho-Dong. The aircraft disintegrated on impact and several houses and buildings were destroyed. All 15 occupants were killed as well as 44 people on the ground. 120 other people were injured, 23 of them seriously. At the time of the accident, weather conditions were poor with fog and drizzle.
Probable cause:
Failure (fire) of the left engine during initial climb for unknown reasons.

Crash of a Douglas DC-8-51 in New Orleans: 19 killed

Date & Time: Mar 30, 1967 at 0050 LT
Type of aircraft:
Operator:
Registration:
N802E
Flight Type:
Survivors:
No
Site:
Schedule:
New Orleans - New Orleans
MSN:
45409/19
YOM:
1959
Flight number:
DL9877
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
19
Captain / Total flying hours:
19008
Captain / Total hours on type:
475.00
Copilot / Total flying hours:
16929
Copilot / Total hours on type:
15
Aircraft flight hours:
23391
Circumstances:
Delta Air Lines DC-8-51 N802E was scheduled as Flight 9877, to provide crew training for a captain-trainee and a flight engineer-trainee. In addition the flight engineer-instructor was being given a routine proficiency check. At 23:14 a weather briefing was given to the instructor pilot, indicating, "... the only significant weather was a restriction in visibility which was expected to reduce to about two miles in fog and smoke near 0600...". The flight departed the ramp at 00:40 with the captain-trainee in the left seat and the check captain in the right seat. At 00:43 the crew advised the tower they were ready for takeoff and would "...like to circle and land on one (runway 1)." The tower controller then cleared them as requested. The aircraft was observed to make what appeared to be a normal takeoff and departure. At 00:47 the crew reported on base leg for runway 01, and the controller cleared the flight to land. A subsequent discussion revealed that they would execute a simulated two-engine out approach, execute a full stop landing and then takeoff on runway 19. The tower controller observed Flight 9877 in a shallow left turn on what appeared to be a normal final approach. The degree of bank increased to approximately 60° or greater when the aircraft hit the power lines approximately 2,300 feet short and 1,100 feet west of the runway threshold. The DC-8 crashed into a residential area, destroying several homes and the Hilton complex. All six crew members were killed as well as 13 people on the ground, clients and employees at Hilton Hotel. 18 other people were injured, some of them seriously. The aircraft was totally destroyed by impact forces and a post crash fire.
Probable cause:
Improper supervision by the instructor, and the improper use of flight and power controls by both instructor and the Captain-trainee during a simulated two-engine out landing approach, which resulted in a loss of control.
Final Report:

Crash of a Canadair CL-44D4-1 in Đà Nẵng: 111 killed

Date & Time: Dec 24, 1966 at 1915 LT
Type of aircraft:
Operator:
Registration:
N228SW
Flight Type:
Survivors:
No
Site:
Schedule:
Tachikawa – Đà Nẵng
MSN:
31
YOM:
1962
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
111
Circumstances:
The crew was completing a cargo flight from Tachikawa AFB to Đà Nẵng on a subcontract mission for the US Air Force, carrying various equipments and goods. On final approach to Đà Nẵng Airport by night, the crew encountered poor weather conditions with heavy rain falls and fog. In low visibility, the crew failed to realize his altitude was too low when the airplane struck an obstacle, stalled and crashed in flames in the district of Binh Thai located few dozen yards short of runway. The aircraft disintegrated on impact and several houses were destroyed. All four crew members were killed as well as 107 people on the ground. 50 others were injured, among them 19 seriously.
Probable cause:
It is believed that the crew continued the approach below the glide in below-minima weather conditions, probably in order to establish a visual contact with the ground. Poor weather conditions and low visibility were considered as contributing factors.
Final Report:

Crash of a Lockheed PV-2 Harpoon in Phoenix: 2 killed

Date & Time: Feb 3, 1966 at 1504 LT
Type of aircraft:
Operator:
Registration:
N7258C
Flight Type:
Survivors:
No
Site:
Schedule:
Phoenix - Phoenix
MSN:
15-1103
YOM:
1944
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
7000
Captain / Total hours on type:
250.00
Circumstances:
The crew was completing a local training flight at Phoenix-Sky Harbor Airport. While cruising in the vicinity of the airfield, the pilot informed ATC about an engine fire and elected to return for an emergency landing when control was lost. The airplane crash in flames into a residential area located near the airport. The airplane and three houses were destroyed. Both pilots were killed while no one on the ground was injured.
Probable cause:
Engine fire in flight for undetermined reason.
Final Report:

Crash of a Fairchild C-119C-25-FA Flying Boxcar in Scranton: 3 killed

Date & Time: Jan 8, 1966
Operator:
Registration:
51-2611
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Hartford – Binghamton
MSN:
10600
YOM:
1951
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
The crew was performing a flight from Hartford to Binghamton, carrying a load of various equipments. En route, one of the engine failed and the pilot was unable to maintain a safe altitude. At an altitude of 2,000 feet, the mechanic bailed out when the airplane dove into the ground and crashed onto a house located in Scranton. Both pilots were killed as well as a boy on the ground.
Probable cause:
Engine failure in flight.

Crash of a Vickers 701 Viscount in Liverpool: 4 killed

Date & Time: Jul 20, 1965 at 1710 LT
Type of aircraft:
Operator:
Registration:
G-AMOL
Flight Type:
Survivors:
No
Site:
Schedule:
Douglas - Liverpool
MSN:
25
YOM:
1953
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
4
Aircraft flight hours:
20694
Circumstances:
Viscount G-AMOL departed Ronaldsway at 16:49 for a flight to Liverpool. The flight was made at flight level 70 and at 17:08 hours the aircraft was identified by Liverpool radar over Wallasey and positioned for a PPI continuous descent radar approach to runway 26. Half a mile from touchdown the radar approach was completed and the aircraft was then seen (on radar) to be just discernibly to the right of the centreline. No radio messages were received from the aircraft after the start of the talk-down. At 550 metres from the threshold, it was estimated to be at a height between 30 and 60 metres and about 40 metres to the right of the centre line. At this point witnesses saw the aircraft bank and turn to the right. The fuselage was level and the aircraft was banked almost vertically for part of the turn. When heading in approximately the opposite direction to the runway it rolled on to its back and crashed into the roof of a factory about 365 metres to the right of the extended centre line of the runway and about 550 metres from the threshold. After penetrating the roof, the aircraft had struck a heavy steel girder which had caused it to tip "tail-over-nose". It had then come to rest the right way up on the floor of the workshop with the tail resting on the steel roof trusses. An intense fire broke out which consumed almost the whole structure of the fuselage. Both crew members and two employees of the factory were killed.
Probable cause:
The aircraft went out of control during the final stage of an approach to land but the reason for this has not been determined.