Ground accident of a Boeing 747-306M in Cairo

Date & Time: Jul 17, 2010 at 0730 LT
Type of aircraft:
Operator:
Registration:
HS-VAC
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Cairo - Jeddah
MSN:
23056/587
YOM:
1983
Flight number:
SV9302
Country:
Region:
Crew on board:
22
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was completing a positioning flight from Cairo to Jeddah. During the takeoff roll, the engine n°4 experienced an uncontained failure. The takeoff procedure was rejected and the aircraft came to a halt and later transferred to a hangar. All 22 crew members escaped uninjured while the aircraft was considered as damaged beyond repair.
Probable cause:
Failure of the n°4 engine during takeoff following the failure of the high pressure compressor.

Crash of a Cessna 550 Citation Bravo in Brač

Date & Time: Jul 15, 2010 at 1646 LT
Type of aircraft:
Operator:
Registration:
YU-BSG
Survivors:
Yes
Schedule:
Tirana – Brač
MSN:
550-1049
YOM:
2003
Location:
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
3427
Aircraft flight cycles:
2661
Circumstances:
Following an uneventful flight from Tirana, the crew started the approach to Brač Airport in good weather conditions. After landing on runway 04, the crew started the braking procedure but the aircraft was unable to stop within the remaining distance. It overran, went through a fence, lost its undercarriage and came to rest in a rocky area, bursting into flames. All five occupants escaped uninjured while the aircraft was partially destroyed by a post crash fire.
Probable cause:
Wrong approach configuration on part of the crew who landed too far down the runway, reducing the landing distance available. The following contributing factors were identified:
- Excessive speed on approach (the IAS was 143 knots upon touchdown),
- The crew completed the approach in a too steep descent,
- Incorrect flare which caused the aircraft to land too dar down the runway,
- Insufficient landing distance available,
- The crew failed to initiate a go-around procedure.
Final Report:

Crash of a Cessna 421A Golden I Eagle in Tulsa: 3 killed

Date & Time: Jul 10, 2010 at 2205 LT
Type of aircraft:
Operator:
Registration:
N88DF
Flight Type:
Survivors:
No
Schedule:
Pontiac – Tulsa
MSN:
421A-0084
YOM:
1968
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
592
Captain / Total hours on type:
67.00
Aircraft flight hours:
640
Circumstances:
During the 3.5-hour flight preceding the accident flight, the airplane used about 156 gallons of the 196 gallons of usable fuel. After landing, the airplane was topped off with 156 gallons of fuel for the return flight. During the preflight inspection, a line serviceman at the fixed based operator observed the right main fuel tank sump become stuck in the open position. He estimated 5 to 6 gallons of fuel were lost before the sump seal was regained, but the exact amount of fuel lost could not be determined. The lost fuel was not replaced before the airplane departed. Data from an on board GPS unit indicate that the airplane flew the return leg at an altitude of about 4,500 feet mean sea level for about 4 hours. About 4 minutes after beginning the descent to the destination airport, the pilot requested to divert to a closer airport. The pilot was cleared for an approach to runway 18R at the new destination. While on approach to land, the pilot reported to the air traffic control tower controller, “we exhausted fuel.” The airplane descended and crashed into a forested area about 1/2 mile from the airport. Post accident examination of the right and left propellers noted no leading edge impact damage or signatures indicative of rotation at the time of impact. Examination of the airplane wreckage and engines found no malfunctions or failures that would have precluded normal operation. The pilot did not report any problems with the airplane or its fuel state before announcing the fuel was exhausted. His acceptance of the approach to runway 18R resulted in the airplane flying at least 1 mile further than if he had requested to land on runway 18L instead. If the pilot had declared an emergency and made an immediate approach to the closest runway when he realized the exhausted fuel state, he likely would have reached the airport. Toxicological testing revealed cyclobenzaprine and diphenhydramine in the pilot’s system at or above therapeutic levels. Both medications carry warnings that use may impair mental and/or physical abilities required for activities such as driving or operating heavy machinery. The airplane would have used about 186 gallons of fuel on the 4-hour return flight if the engines burned fuel at the same rate as the previous flight. The fuel lost during the preflight inspection and the additional 30 minutes of flight time on the return leg reduced the airplane’s usable fuel available to complete the planned flight, and the pilot likely did not recognize the low fuel state before the fuel was exhausted due to impairment by the medications he was taking.
Probable cause:
The pilot’s inadequate preflight fuel planning and management in-flight, which resulted in total loss of engine power due to fuel exhaustion. Contributing to the accident was the pilot’s use of performance-impairing medications.
Final Report:

Crash of a Gippsland GA-8 Airvan in Orange

Date & Time: Jul 6, 2010 at 1745 LT
Type of aircraft:
Operator:
Registration:
VH-YBH
Flight Type:
Survivors:
Yes
Schedule:
Parkes - Orange
MSN:
GA8-08-131
YOM:
2008
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The pilot was performing a cargo flight from Parkes to Orange, New South Wales. On final approach, the single engine aircraft was too low and impacted the roof of a metal hangar located near the runway threshold. The aircraft stalled and struck the runway surface. Upon impact, the nose gear was torn off. Out of control, the aircraft veered off runway and eventually collided with a metal hangar under construction. While the pilot was injured, the aircraft was destroyed.

Crash of a PZL-Mielec AN-2T in Tuzla: 12 killed

Date & Time: Jul 5, 2010 at 1740 LT
Type of aircraft:
Operator:
Registration:
53
Flight Phase:
Survivors:
Yes
Schedule:
Tuzla - Tuzla
MSN:
1G194-53
YOM:
1982
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
10
Pax fatalities:
Other fatalities:
Total fatalities:
12
Circumstances:
Shortly after takeoff from Tuzla Airport, the single engine aircraft stalled and crashed in an open field, bursting into flames. Two passengers survived while 12 other occupants were killed. The aircraft was carrying 4 crew and 10 members of the Romanian Navy engaged in a paratroopers mission.
Those killed were:
Cdr Nicolae Jianu,
Lt Cdr Cătălin Vicenţiu Antoche,
Lt Lavinia Guită,
Lt Răzvan Rîngheţ,
Lt Liviu Antim,
Florin Claudiu Cişmaşu,
Cătălin Rădoi,
Băduţ Papuc,
Vlăduţ Sărman,
Marius Cătălin Chioveanu,
Cosmin Furtună,
Cosmin Florescu.
The Captain Daniel Bâlsanu and the foreman Marius Nazare were injured.

Crash of a Cessna 421B Golden Eagle II in Alpine: 5 killed

Date & Time: Jul 4, 2010 at 0015 LT
Operator:
Registration:
N31AS
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Alpine - Odessa
MSN:
421B-0473
YOM:
1973
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
1650
Captain / Total hours on type:
160.00
Aircraft flight hours:
2302
Circumstances:
The airplane impacted terrain shortly after takeoff. The wreckage distribution was consistent with a high airspeed, low angle-of-attack impact. Examination of the ground scars and wreckage indicated that the landing gear was down, the flaps were down, and the engines were operating at a high power setting at the time of impact. An examination of the airframe, engines, and related systems revealed no mechanical malfunctions or failures. According to the owner’s manual for the airplane, the flaps should have been retracted and the landing gear should have been brought up as soon as a climb profile was established. Based upon the location of the wreckage, the direction of the impact, and the location of the airport, it is likely that the airplane crashed within one or two minutes after takeoff. The extended landing gear and flaps degraded the climb performance of the airplane. The pilot held an airline transport pilot certificate and had recent night flight experience. Toxicological results were positive for azacyclonol and ibuprofen but were not at levels that would have affected his performance. According to family members, the pilot normally slept from 2230 or 2300 to 0700; the accident occurred at 0015. Although the investigation was unable to determine how long the pilot had been awake before the accident or his sleep schedule in the three days prior to the accident, it is possible that the pilot was fatigued, as the accident occurred at a time when the pilot was normally asleep. The company did not have, and was not required to have guidance or a policy addressing fatigue management.
Probable cause:
The degraded performance of the airplane due to the pilot not properly setting the flaps and retracting the landing gear after takeoff. Contributing to the accident was the pilot’s fatigue.
Final Report:

Crash of a Beechcraft RC-12K Guardrail in Wiesbaden

Date & Time: Jun 30, 2010 at 1540 LT
Type of aircraft:
Operator:
Registration:
85-0155
Flight Type:
Survivors:
Yes
Schedule:
Wiesbaden - Wiesbaden
MSN:
FE-9
YOM:
1987
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew departed Wiesbaden-Erbenheim AFB on a local training flight. On approach, technical problem forced the crew to attempt an emergency landing in a cornfield 200 metres short of runway. Both pilots were slightly injured while the aircraft was damaged beyond repair.
Probable cause:

Crash of a Piper PA-31-350 Navajo Chieftain in Puerto Barrios: 2 killed

Date & Time: Jun 23, 2010 at 1050 LT
Registration:
N430LA
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Guatemala City – Rio Dulce
MSN:
31-7405446
YOM:
1974
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The twin engine departed Guatemala City-La Aurora Airport at 0930LT on a flight to Rio Dulce with two pilots on board. En roue, the crew contacted ATC, modified his flight plan and was cleared to continue direct to Puerto Barrios. Following few touch-and-go manoeuvres at Puerto Barrios Airport, the crew completed a new approach and landing on runway 12. The pilot-in-command increased engine power and took off when he lost control of the airplane that crashed on a road, coming to rest upside down. The aircraft was destroyed and both occupants were killed.
Probable cause:
Loss of control following an unstabilized approach. The failure of the crew to initiate a go-around procedure was considered as a contributing factor.
Final Report:

Crash of a Beechcraft A100 King Air in Québec: 7 killed

Date & Time: Jun 23, 2010 at 0559 LT
Type of aircraft:
Operator:
Registration:
C-FGIN
Flight Phase:
Survivors:
No
Schedule:
Québec - Seven Islands - Natashquan
MSN:
B-164
YOM:
1973
Flight number:
APO201
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
3046
Captain / Total hours on type:
372.00
Copilot / Total flying hours:
2335
Copilot / Total hours on type:
455
Aircraft flight hours:
19665
Aircraft flight cycles:
16800
Circumstances:
Aircraft was making an instrument flight rules flight from Québec to Sept-Îles, Quebec. At 0557 Eastern Daylight Time, the crew started its take-off run on Runway 30 at the Québec/Jean Lesage International Airport; 68 seconds later, the co-pilot informed the airport controller that there was a problem with the right engine and that they would be returning to land on Runway 30. Shortly thereafter, the co-pilot requested aircraft rescue and fire-fighting (ARFF) services and informed the tower that the aircraft could no longer climb. A few seconds later, the aircraft struck the ground 1.5 nautical miles from the end of Runway 30. The aircraft continued its travel for 115 feet before striking a berm. The aircraft broke up and caught fire, coming to rest on its back 58 feet further on. The 2 crew members and 5 passengers died in the accident. No signal was received from the emergency locator transmitter (ELT).
Probable cause:
Findings as to Causes and Contributing Factors:
1. After the take-off at reduced power, the aircraft performance during the initial climb was lower than that established at certification.
2. The right engine experienced a problem in flight that led to a substantial loss of thrust.
3. The right propeller was not feathered; therefore, the rate of climb was compromised by excessive drag.
4. The absence of written directives specifying which pilot was to perform which tasks may have led to errors in execution, omissions, and confusion in the cockpit.
5. Although the crew had the training required by regulation, they were not prepared to manage the emergency in a coordinated, effective manner.
6. The priority given to ATC communications indicates that the crew did not fully understand the situation and were not coordinating their tasks effectively.
7. The impact with the berm caused worse damage to the aircraft.
8. The aircraft’s upside-down position and the damage it sustained prevented the occupants from evacuating, causing them to succumb to the smoke and the rapid, intense fire.
9. The poor safety culture at Aéropro contributed to the acceptance of unsafe practices.
10. The significant measures taken by TC did not have the expected results to ensure compliance with the regulations, and consequently unsafe practices persisted.
Findings as to Risk:
1. Deactivating the flight low pitch stop system warning light or any other warning system contravenes the regulations and poses significant risks to flight safety.
2. The maintenance procedures and operating practices did not permit the determination of whether the engines could produce the maximum power of 1628 ft-lb required at take-off and during emergency procedures, posing major risks to flight safety.
3. Besides being a breach of regulations, a lack of rigour in documenting maintenance work makes it impossible to determine the exact condition of the aircraft and poses major risks to flight safety.
4. The non-compliant practice of not recording all defects in the aircraft journey log poses a safety risk because crews are unable to determine the actual condition of the aircraft at all times, and as a result could be deprived of information that may be critical in an emergency.
5. The lack of an in-depth review by TC of SOPs and checklists of 703 operators poses a safety risk because deviations from aircraft manuals are not detected.
6. Conditions of employment, such as flight hours–based remuneration, can influence pilots’ decisions, creating a safety risk.
7. The absence of an effective non-punitive and confidential voluntary reporting system means that hazards in the transportation system may not be identified.
8. The lack of recorded information significantly impedes the TSB’s ability to investigate accidents in a timely manner, which may prevent or delay the identification and communication of safety deficiencies intended to advance transportation safety.
Final Report:

Crash of a McDonnell Douglas MD-82 in Kinshasa

Date & Time: Jun 21, 2010 at 1200 LT
Type of aircraft:
Operator:
Registration:
9Q-COQ
Survivors:
Yes
Schedule:
Kinshasa – Lubumbashi
MSN:
49178/1122
YOM:
1983
Flight number:
EO601
Region:
Crew on board:
7
Crew fatalities:
Pax on board:
103
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
During the takeoff roll at Kinshasa-N'Djili Airport, a tyre burst on the left main gear. After liftoff, while in initial climb, the crew was forced to shut down the left engine while the hydraulic system failed. The crew declared an emergency and was cleared for an immediate return. On approach, he was unable to lower the nose gear due to the malfunction of the hydraulic system. After touchdown on runway 06, the aircraft rolled for a distance of 1,000 metres then veered off runway to the right, slid on a grassy area and came to rest 500 metres further. All 110 occupants evacuated safely while the aircraft was damaged beyond repair.
Probable cause:
A tyre burst on the left main gear during the takeoff procedure. Debris damaged hydraulic lines and were ingested in the left engine that should be shut down.