Crash of a Cessna 414 Chancellor in Bowie: 2 killed

Date & Time: Aug 15, 2014 at 1535 LT
Type of aircraft:
Registration:
N127BC
Flight Type:
Survivors:
No
Schedule:
La Porte - Bowie
MSN:
414-0519
YOM:
1974
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1200
Captain / Total hours on type:
15.00
Aircraft flight hours:
4256
Circumstances:
The twin engine aircraft, owned by Lawrence R. Liptack, crashed in flames in an open field located northeast of Bowie, Texas. The pilot and owner, aged 51, was killed with his son aged 10. The multi-engine airplane was about 500 ft above ground level (agl) and on a left base landing approach when a witness saw the airplane suddenly point straight down, begin spinning, and make three complete rotations before impacting terrain in a partially nose-down attitude. The airplane came to rest upright, and was mostly consumed by an immediate post impact fire. A post accident examination of the wreckage revealed no evidence of preimpact mechanical malfunctions or failures that would have precluded normal operation. A pilot operating another pipeline patrol airplane in the vicinity reported frequent severe-to-extreme turbulence about 1,000-2,000 ft above ground level. Data from an on-board GPS unit indicated that, while on the base leg of the airport traffic pattern for landing, the accident airplane's airspeed decayed 10 knots below the manufacturer's recommended approach speed for turbulent conditions. An autopsy performed on the pilot found significant existing atherosclerotic disease (60 to 80 percent) and described evidence of an acute, premortem, nonocclusive thrombosis of the left anterior descending coronary artery. The medical examiner's conclusion stated it "appears the decedent likely suffered an acute cardiac event while piloting his aircraft" and "died primarily due to hypertensive and atherosclerotic cardiovascular disease and that his multiple blunt force injuries likely contributed to his death." It is likely that the pilot was incapacitated due to the acute cardiac event and lost control of the airplane during the approach to land.
Probable cause:
The pilot's incapacitation in flight as the result of a an acute cardiac event, which resulted in a loss of control and collision with terrain.
Final Report:

Crash of a Cessna 560XLS Citation Excel in Santos: 7 killed

Date & Time: Aug 13, 2014 at 1003 LT
Operator:
Registration:
PR-AFA
Survivors:
No
Site:
Schedule:
Rio de Janeiro – Santos
MSN:
560-6066
YOM:
2011
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
6235
Captain / Total hours on type:
130.00
Copilot / Total flying hours:
5279
Copilot / Total hours on type:
95
Aircraft flight hours:
434
Aircraft flight cycles:
392
Circumstances:
The aircraft took off from Santos Dumont Airport (SBRJ) at 12:21 UTC, on a transport flight bound for Santos Aerodrome (SBST), with two pilots and five passengers on board. During the enroute phase of the flight, the aircraft was under radar coverage of the approach control units of Rio de Janeiro and São Paulo (APP-RJ and APP-SP, respectively), and no abnormalities were observed. Upon being released by APP-SP for descent and approach toward SBST, the aircraft crew, already in radio contact with Santos Aerodrome Flight Information Service (Santos Radio), reported their intention to perform the IFR ECHO 1 RWY 35 NDB approach chart profile. After reporting final approach, the crew informed that they would make a go-around followed by a holding procedure, and call Santos Radio again. According to an observer that was on the ground awaiting the arrival of the aircraft at Santos Air Base (BAST) and to another observer at the Port of Santos, the aircraft was sighted flying over the aerodrome runway at low height, and then making a turn to the left after passing over the departure end of the runway, at which point the observers lost visual contact with the aircraft on account of the weather conditions. Moments later, the aircraft crashed into the ground. All seven occupants were killed.
Probable cause:
The following factors were identified:
- Considering the pronounced angle formed between the trajectory of the aircraft and the terrain, as well as the calculated speed (which by far exceeded the aircraft operating limit) moments before the impact, it is possible to infer that, from the moment the aircraft disappeared in the clouds, it could only have reached such speed and flown that trajectory if it had climbed considerably, to the point of being detected by the radar. Such condition presented by the aircraft may have been the result of an exaggerated application of controls.
- The making of an approach with a profile different from the one prescribed shows lack of adherence to procedures, which, in this case, may have been influenced by the self-confidence of the pilot on his piloting ability, given his prior experiences.
- Despite the lack of pressure on the part of the passengers to force compliance with the agenda, it is a known fact that this type of routine creates in the crew a self-pressure, most of the time unconscious, for accomplishing the flight schedule on account of the commitments undertaken by the candidate in campaign, and, therefore, the specific characteristics of this type of flight pose demands in terms of performance that may have influenced the pilots to operate with reduced safety margins.
- The meteorological conditions were close to the safety minimums for the approach and below the minimums for the circle-to-land procedure prescribed in the ECHO 1 approach. However, such conditions, by themselves, would not represent risk for the operation, if the profile of the ECHO 1 procedure was performed in accordance with the parameters established in the aeronautical publications and the flight parameters defined by the aircraft manufacturer. Upon verifying that the above mentioned parameters were not complied with, one observes that the meteorological conditions became a complicating factor for flying the aircraft, rendering it difficult to be stabilized on the final approach, and a go-around became necessary, as a result.
- In the scenario of the aircraft collision with the ground, there were aspects favorable to the occurrence of spatial disorientation, such as: reduction of the visibility on account of meteorological conditions, stress and workload increase due to the missed approach procedure, maneuvers with a G-load above 1.15G, and a possible loss of situational awareness. The large pitch-down angle, the high speed, and the power developed by the engines at the moment of impact are also evidence compatible with incapacitating disorientation, and point towards a contribution of this factor.
- The integration between the pilots may have been hindered by their little experience working together as one crew, and also by their different training background. In addition, the personal characteristics of the captain, as a more impositive and confident person, in contrast with the more passive posture of the copilot, may also have hampered the crew dynamics in the management of the flight.
- In the seven days preceding the day of the accident, the crew was in conformity with the Law 7183 of 5 April 1984 in relation to both duty time and rest periods. However, the analysis of copilot’s voice, speech, and language indicated compatibility with fatigue and somnolence, something that may have contributed to the degradation of the crew’s performance.
- Their lack of training of missed approach procedures in CE 560XLS+ aircraft may have demanded from the crew a higher cognitive effort in relation to the conditions required for the aircraft model, since they possibly did not have conditioned behaviors for controlling the flight and that could otherwise provide them with more agility with regard to the cockpit actions. Thus, they probably missed the skills, knowledge, and attitudes that would allow them to more adequately perform their activities in that operational context.
- Even though Santos Radio reported, in the first contact with the aircraft, that the aerodrome was operating IFR, the messages transmitted to the aircraft did not include the conditions of ceiling, visibility, and SIGMET information (ICA 100-37). This may have contributed to reducing the crew’s situational awareness, since the last information accessed by them was probably the 11:00 UTC SBST METAR, which reported VMC conditions for operation in the aerodrome. Thus, the pilots may have built a mental model of unreal SBST meteorological conditions more favorable to the operation.
- After coordination of the descent, the PR-AFA aircraft made a left turn and, for an unknown reason, deviated from the W6-airway profile, reporting six positions that were not compatible with the real flight path until the moment it started a final approach. This approach was different from the trajectory of the final approach defined for the ECHO 1 procedure, and was flown with speed parameters different from those recommended by the aircraft manufacturer. These aspects reduced the chances of the aircraft to align with the final approach in a stabilized manner. The fact that the aircraft made a low pass over the runway and then a left turn at low altitude in weather conditions below the minimum established in the circle-to-land procedure instead of performing the profile prescribed in the ECHO 1 approach chart also resulted in risks to the operation, and created conditions which were conducive to spatial disorientation.
- Since the captain had already conducted FMS visual approaches on other occasions, his acquired work-memory may have strengthened his confidence in performing the procedure again, even though in another scenario, on account of the human being tendency to rely on previous successful experiences.
- A poor perception on the part of the pilots relative to the real meteorological conditions on the approach may have compromised their level of situational awareness, thus leading the aircraft to a condition of operation below the safe minimums.
- The TAF/GAMET weather prognostics with validity up to 12:00 UTC, and available to the crew at the time the flight plan was filed at the AIS-RJ, indicated a possibility of degradation of the ceiling and visibility parameters on account of rain associated with mist, encompassing the duration of the aforementioned flight, especially in the area of SBST. The 11:00 UTC satellite image and the SIGMET valid from 10:30 UTC to 13:30 UTC, also showed an active cold front in the Southeast with stratiform cloud layers over SBST and a forecast of convective cells with northeasterly movement at an average speed of 12kt. Despite the availability of such information, the crew may not have made a more accurate analysis showing the swift deterioration of the weather conditions in the period between their takeoff from SBRJ and the approach to SBST, and thus may have failed to plan their conduct of the flight in accordance with the weather conditions forecast by the meteorological services.
- Despite having the C560 qualification required to operate the CE 560XLS+aircraft, the pilots were not checked by the employers as to their previous experience on this kind of equipment, or as to the need of transition training and/or specific formation to fly the PRAFA aircraft. The adoption of a formal process for the recruitment, selection, monitoring and evaluation of the performance of the professionals could have identified their training needs for that type of aircraft.
- Although the RBAC 61 requires pilots to undergo flight instruction and proficiency checks to switch between models of the CE 560XL family, the need of specific training was only clarified on 4 July 2014, with the publication of the ANAC Supplementary Instruction (IS 61-004, Revision A). Until that date, this need could only be determined by means of consultation of the FSB Report, made available only on the FAA website. In this context, the PR-AFA pilots would only be evaluated on the CE 560XLS+ aircraft on the occasion of their type revalidation, which would take place shortly before the expiration date of their C560 qualifications, which were valid until October 2014 (captain), and May 2015 (copilot). The fact that there was a qualification (C560) that was shared for the operation of C560 Citation V, C560 Encore, C560 Encore+, CE 560XL, CE 560XLS, or CE 560XLS + aircraft was not enough to make the DCERTA system refuse flight plans filed by pilots who lacked proper training to operate one of the aforementioned aircraft models. The RBAC 67 contained physical and mental health requirements which were not clear, inducing physicians to resort to other publications for guidance and support of their decisions and judgments relative to the civil aviation personnel. The absence of clear requirements to be adopted as the acceptable minimum for the exercise of the air activity, led the physicians responsible for judging the pilots’ health inspections’ to use their own discretion on the subject, opening gaps that could allow professionals not fully qualified to perform functions in flight below the minimum acceptable safety levels.
- Considering the possibility that the captain accumulated tasks as a result of a possible difficulty of the copilot in assisting him at the beginning of the missed approach procedure, such accumulation may have exceeded his ability to deal with the tasks, leading him to committing piloting errors and/or experiencing spatial disorientation.
Final Report:

Crash of a Piper PA-46-350P Malibu Mirage in Statesville

Date & Time: Aug 1, 2014 at 2100 LT
Operator:
Registration:
N472ST
Flight Type:
Survivors:
Yes
Schedule:
Manassas – Statesville
MSN:
46-36472
YOM:
2010
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2556
Captain / Total hours on type:
1200.00
Aircraft flight hours:
1656
Circumstances:
According to the pilot, she was flying an instrument landing system approach when she noted that the glide slope was out of service. She transitioned to a localizer-only approach and continued. Night, instrument meteorological conditions prevailed with a 400-foot ceiling. She noticed that the airplane was "high and fast" on final approach, so she used speed brakes and flaps to slow the airplane and descend to the minimum descent altitude. As the airplane descended below the ceiling, she observed runway lights and attempted to land on the runway. The airplane landed long, departed the runway at the departure end, and struck an embankment before coming to rest. An inspector from the Federal Aviation Administration examined the airplane and confirmed substantial damage to the fuselage, wings, and empennage. The pilot reported no pre-impact mechanical malfunctions or failures with the airplane that would have precluded normal operation.
Probable cause:
The pilot's failure to maintain a proper glide path and airspeed on final approach, which resulted in a long landing and runway excursion.
Final Report:

Crash of an ATR72-500 in Magong: 48 killed

Date & Time: Jul 23, 2014 at 1906 LT
Type of aircraft:
Operator:
Registration:
B-22810
Survivors:
Yes
Site:
Schedule:
Kaohsiung – Magong
MSN:
642
YOM:
2000
Flight number:
GE222
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
54
Pax fatalities:
Other fatalities:
Total fatalities:
48
Captain / Total flying hours:
22994
Captain / Total hours on type:
19069.00
Copilot / Total flying hours:
2392
Copilot / Total hours on type:
2083
Aircraft flight hours:
27039
Aircraft flight cycles:
40387
Circumstances:
The aircraft was being operated on an instrument flight rules (IFR) regular public transport service from Kaohsiung to Magong in the Penghu archipelago. At 1906 Taipei Local Time, the aircraft impacted terrain approximately 850 meters northeast of the threshold of runway 20 at Magong Airport and then collided with a residential area on the outskirts of Xixi village approximately 200 meters to the southeast of the initial impact zone. At the time of the occurrence, the crew was conducting a very high frequency omni-directional radio range (VOR) non-precision approach to runway 20. The aircraft was destroyed by impact forces and a post-impact fire. Ten passengers survived the occurrence and five residents on the ground sustained minor injuries. The occurrence was the result of controlled flight into terrain, that is, an airworthy aircraft under the control of the flight crew was flown unintentionally into terrain with limited awareness by the crew of the aircraft’s proximity to terrain. The crew continued the approach below the minimum descent altitude (MDA) when they were not visual with the runway environment contrary to standard operating procedures. The investigation report identified a range of contributing and other safety factors relating to the flight crew of the aircraft, TransAsia’s flight operations and safety management processes, the communication of weather information to the flight crew, coordination issues at civil/military joint-use airport, and the regulatory oversight of TransAsia by the Civil Aeronautics Administration (CAA).
Probable cause:
- The flight crew did not comply with the published runway 20 VOR non-precision instrument approach procedures at Magong Airport with respect to the minimum descent altitude (MDA). The captain, as the pilot flying, intentionally descended the aircraft below the published MDA of 330 feet in the instrument meteorological conditions (IMC) without obtaining the required visual references.
- The aircraft maintained an altitude between 168 and 192 feet before and just after overflying the missed approach point (MAPt). Both pilots spent about 13 seconds attempting to visually locate the runway environment, rather than commencing a missed approach at or prior to the MAPt as required by the published procedures.
- As the aircraft descended below the minimum descent altitude (MDA), it diverted to the left of the inbound instrument approach track and its rate of descent increased as a result of the flying pilot’s control inputs and meteorological conditions. The aircraft’s hazardous flight path was not detected and corrected by the crew in due time to avoid the collision with the terrain, suggesting that the crew lost situational awareness about the aircraft’s position during the latter stages of the approach.
- During the final approach, the heavy rain and associated thunderstorm activity intensified producing a maximum rainfall of 1.8 mm per minute. The runway visual range (RVR) subsequently reduced to approximately 500 meters. The degraded visibility significantly reduced the likelihood that the flight crew could have acquired the visual references to the runway environment during the approach.
- Flight crew coordination, communication, and threat and error management were less than effective. That compromised the safety of the flight. The first officer did not comment about or challenge the fact that the captain had intentionally descended the aircraft below the published minimum descent altitude (MDA). Rather, the first officer collaborated with the captain’s intentional descent below the MDA. In addition, the first officer did not detect the aircraft had deviated from the published inbound instrument approach track or identify that those factors increased the risk of a controlled flight into terrain (CFIT) event.
- None of the flight crew recognized the need for a missed approach until the aircraft reached the point (72 feet, 0.5 nautical mile beyond the missed approach point) where collision with the terrain became unavoidable.
- The aircraft was under the control of the flight crew when it collided with foliage 850 meters northeast of the runway 20 threshold, two seconds after the go around decision had been made. The aircraft sustained significant damage and subsequently collided with buildings in a residential area. Due to the high impact forces and post-impact fire, the crew and most passengers perished.
- According to the flight recorders data, non-compliance with standard operating procedures (SOP's) was a repeated practice during the occurrence flight. The crew’s recurring non-compliance with SOP's constituted an operating culture in which high risk practices were routine and considered normal.
- The non-compliance with standard operating procedures (SOP's) breached the obstacle clearances of the published procedure, bypassed the safety criteria and risk controls considered in the design of the published procedures, and increased the risk of a controlled flight into terrain (CFIT) event.
Final Report:

Crash of a Lockheed C-130J Hercules in Herat

Date & Time: Jul 22, 2014
Type of aircraft:
Operator:
Registration:
MM62190
Flight Type:
Survivors:
Yes
Schedule:
Abu Dhabi - Herat
MSN:
5530
YOM:
2003
Location:
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was conducting a daily supply mission to Herat for the troops stationed in the area. For undetermined reason, the four engine aircraft landed hard and the right main gear sank on touchdown and went through the wheels bay. The airplane went out of control and veered off runway to the right before coming to rest. All four occupants were uninjured while the aircraft was damaged beyond repair. The exact cause of the heavy landing remains unknown.

Crash of an ATR72-212 in Cox's Bazar

Date & Time: Jul 20, 2014 at 1745 LT
Type of aircraft:
Operator:
Registration:
S2-AFN
Survivors:
Yes
Schedule:
Dhaka - Cox's Bazar
MSN:
379
YOM:
1993
Flight number:
4H501
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
43
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Following an uneventful flight from Dhaka, the crew initiated the approach to Cox's Bazar in poor weather conditions due to heavy rain falls. After touchdown, the nose gear collapsed. The airplane slid on its nose for few dozen metres before coming to rest in the middle of the runway that was blocked for almost 22 hours. All 48 occupants evacuated safely while the aircraft was damaged beyond repair.

Crash of a PAC-750XTOL in Golgubip

Date & Time: Jul 19, 2014 at 1143 LT
Operator:
Registration:
P2-RNB
Survivors:
Yes
Schedule:
Kiunga – Golgubip
MSN:
190
YOM:
2013
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2930
Captain / Total hours on type:
1900.00
Aircraft flight hours:
143
Circumstances:
A Pacific Aerospace PAC P-750 XTOL single engine aircraft was chartered to transport store goods and six passengers from Kiunga to Golgubip. Although Golgubip is in mountainous terrain and the weather in the area is often poor, the pilot was tasked to fly there without ever having been to Golgubip before. The terrain to the north north east of Golgubip rises gradually behind the airstrip. Visual illusions which may affect the pilot’s perception of height and distance can be associated with airstrips situated in terrain of this kind. On arrival at Golgubip, the pilot orbited and positioned the aircraft for landing. During the final approach he decided to discontinue the approach and to initiate a go-around procedure. The aircraft impacted terrain approximately 500 metres northwest of the airstrip and was substantially damaged. The six passengers were unhurt while the pilot sustained serious injuries. The pilot was treated in Golgubip following the accident, and was airlifted the next day to Tabubil, where he was admitted to hospital. It was later reported that the GPWS alarm sounded on approach until the final impact.
Probable cause:
Loss of control on final approach, maybe following visual illusions.
Final Report:

Crash of a BAe 125-800B in Moscow

Date & Time: Jul 7, 2014
Type of aircraft:
Operator:
Registration:
RA-02806
Flight Type:
Survivors:
Yes
Schedule:
Moscow – Makhatchkala
MSN:
258106
YOM:
1987
Flight number:
CIG9661
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The twin engine aircraft departed Moscow-Vnukovo Airport on a positioning flight to Makhatchkala, carrying a crew of three. On approach to Makhatchkala Airport, the crew was unable to lower the gear that remained stuck in their wheel well. Despite several attempts, the crew was unable to lower the gear manually and eventually decided to return to Moscow-Vnukovo for an emergency landing. The aircraft belly landed on a foam covered runway and slid for few dozen metres before coming to rest. All three crew members escaped uninjured and the aircraft was damaged beyond repair.

Crash of a Britten Norman BN-2A-26 Islander in Monkey Mountain

Date & Time: Jul 6, 2014 at 0950 LT
Type of aircraft:
Registration:
8R-GGY
Survivors:
Yes
Schedule:
Ogle – Omai – Mahdia – Monkey Mountain
MSN:
470
YOM:
1975
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The Authority said the aircraft left the Ogle International Airport earlier in the day and made stops at Omai and Mahdia before heading at Monkey Mountain Airfield with several goods on board. On approach to Monkey Mountain, the plane circled the airstrip several times before landing. Shortly after setting down, it was claimed the aircraft veered off the runway, hit few obstacles and came to rest. While both occupants were uninjured, the aircraft was damaged beyond repair. It appears that weather was poor at the time of the accident with rain and winds and low clouds.
Probable cause:
Guyana Civil Aviation Authority (GCAA) Director General Zulficar Mohamed disclosed that an initial investigation revealed that the Pilot involved in the Monkey Mountain mishap landed short of the runway. As a result, the landing gear of the plane was damaged and from there on, it was difficult to control the 10-seater Islander aircraft. The aircraft subsequently veered off the airstrip causing extensive damage. Mr. Mohamed further stated that the wrecked aircraft is beyond repair, but he was unsure if the operators will attempt to salvage what is left. The aircraft, owned by Domestic Airways, was piloted by Captain Orlando Charles.

Crash of a Cessna 414 Chancellor in Creve Coeur

Date & Time: Jun 26, 2014 at 0457 LT
Type of aircraft:
Registration:
N1552T
Flight Type:
Survivors:
Yes
Schedule:
Creve Cœur – Hopkinsville
MSN:
414-0267
YOM:
1972
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
775
Captain / Total hours on type:
90.00
Aircraft flight hours:
7626
Circumstances:
The pilot reported that, shortly after takeoff, the twin-engine airplane's left front baggage door opened. He attempted to return to the airport, but the left engine lost engine power while the airplane was on the downwind leg of the traffic pattern. The airplane subsequently impacted power lines and terrain. An explosion occurred during the impact sequence, and a fire ensued that almost completely consumed the airframe. Tear down examination of the right engine revealed no anomalies. A test run of the left engine revealed no anomalies; however, due to impact and fire damage, it was not possible to fully test or examine the left engine's fuel system. The reason for the left engine’s loss of power could not
be determined.
Probable cause:
The loss of left engine power for reasons that could not be determined due to impact and fire damage.
Final Report: