Country

Crash of an ATR72-500 in Capela: 62 killed

Date & Time: Aug 9, 2024 at 1322 LT
Type of aircraft:
Operator:
Registration:
PS-VPB
Flight Phase:
Survivors:
No
Site:
Schedule:
Cascavel – São Paulo
MSN:
908
YOM:
2010
Flight number:
PTB2283
Country:
Crew on board:
4
Crew fatalities:
Pax on board:
58
Pax fatalities:
Total fatalities:
62
Circumstances:
The airplane departed Cascavel Airport at 1158LT on a schedule service (flight PTB2283) to São Paulo-Guarulhos Airport, carrying 58 passengers and a crew of four. While flying at FL170, the airplane entered an uncontrolled descent and crashed in a relative flat attitude in a private garden, nearby a villa located in the city of Capela, west of Vinhedo, some 69 km northwest of Guarulhos Airport. A fire erupted after the crash. All 62 occupants have been killed. Significant variations were noted with the aircraft' speed during the entire flight, while the altitude remained stable until the loss of control. Severe icing conditions were reported between FL120 and FL210.

Crash of an ATR72-500 in Pokhara: 72 killed

Date & Time: Jan 15, 2023 at 1057 LT
Type of aircraft:
Operator:
Registration:
9N-ANC
Survivors:
No
Schedule:
Kathmandu - Pokhara
MSN:
754
YOM:
2007
Flight number:
YT691
Location:
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
68
Pax fatalities:
Other fatalities:
Total fatalities:
72
Captain / Total flying hours:
21901
Captain / Total hours on type:
3300.00
Copilot / Total flying hours:
6396
Copilot / Total hours on type:
186
Aircraft flight hours:
28731
Aircraft flight cycles:
30104
Circumstances:
On 15 January 2023, an ATR 72-212A version 500 was operating scheduled flights between Kathmandu (VNKT) and Pokhara International Airport (VNPR). The same flight crew operated two sectors between VNKT to VNPR and VNPR to VNKT earlier in the morning. For first sector, the aircraft landed on runway 30 of VNPR and thereafter departed from VNPR using runway 12. The accident occurred during a visual approach for runway 12 at VNPR. This was the third flight by the crew members on that day. As per the CVR recordings it was understood that the flight was operated by two Captains, one Captain was in the process of obtaining aerodrome familiarization for operating into VNPR and the other Captain was an instructor pilot. The Captain being familiarized, who was occupying the left-hand seat, was the Pilot Flying (PF) and the instructor pilot, occupying the right-hand seat, was the Pilot Monitoring (PM). The take-off, climb, cruise and descent to VNPR was normal. The weather was compatible with VMC enroute to the destination airport. During the first contact with VNPR tower, the Air Traffic Controller (ATC) assigned runway 30 for the aircraft to land. But during the later phases of flight the flight crew, without mentioning any reason for changing the allocated runway, requested and received clearance from ATC to change runway 30 to 12 for landing. At 10:51:36, the aircraft descended from 6,500 feet at fifteen miles away from VNPR and joined the downwind track for Runway 12 to the north of the runway. The aircraft was visually identified by ATC during the approach. At 10:56:12, the pilots extended the flaps to the 15 degrees position and 46 seconds later they selected the landing gears lever to the down position. At 10:56:27, the PF disengaged the Autopilot System (AP) at an altitude of 721 feet Above Ground Level (AGL). The PF then called for “FLAPS 30” at 10:56:32, and the PM replied, “Flaps 30 and continue descent. The flight data recorder (FDR) data did not record any flap surface movement at that time. Instead, the propeller rotation speed (Np) of both engines decreased simultaneously to less than 25% and the torque (Tq) started decreasing to 0%, which is consistent with both propellers going into the feathered condition . The feather condition is not recorded in the FDR parameters. On the cockpit voice recorder (CVR) area microphone recording, a single Master Caution chime was recorded at 10:56:36. As per CVR readout, the flight crew then carried out the “Before Landing Checklist” without identifying the flaps were not to the 300 position, before starting the left turn onto the base leg. During that time, the power lever angle increased from 41% to 44%. At that point, Np of both propellers was recorded as Non-Computed Data (NCD) in the FDR and the torque (Tq) of both engines was at 0%. When propellers are in feather, they are not producing thrust. When both propellers were feathered both engines of 9N-ANC were running in flight idle condition during the event flight as per design to prevent overtorque. As per the FDR data, the engine turbo machine were functioning as expected considering the propeller were feathered. At 10:56:50 when the radio altitude callout for five hundred feet was annunciated, another “click” sound was heard . The aircraft turned to the left and reached a maximum bank angle of 30 degrees. The recorded Np and Tq data remained non-computed, in line with propellers being in feather condition. The yaw damper was disconnected four seconds later. The PF consulted the PM on whether to continue the left turn and the PM replied to continue the turn. Subsequently, the PF asked the PM on whether to continue descend and the PM responded it was not necessary and instructed to apply a little power. At 10:56:54, another click was heard, followed by the flaps moving to the 30 degrees position. When ATC gave the clearance for landing at 10:57:07, the crew did not respond to the tower, the PF mentioned twice that there was no power coming from the engines. The FDR data shows that at 10:57:11, the power levers were advanced first to 62 degrees then to the maximum power position in 2 seconds. It was followed by a “click” sound at 10:57:16. One second after the “click” sound, the aircraft was at the initiation of its last left turn at 368 feet AGL, the highpressure turbine speed (Nh) of both engines increased from 73% to 77%. It is noted that at 10:57:18, in the very last stage of flight, the PF handed over control of the aircraft to the PM. At 10:57:20, the PM (who was previously the PF) repeated again that there was no power from the engines. At 10:57:24 when the aircraft was at 311 feet AGL, the stick shaker5 was activated warning the crew that the aircraft Angle of Attack (AoA) increased up to the stick shaker threshold. At 10:57:26, a second sequence of stick shaker warning was activated when the aircraft banked towards the left abruptly. Three seconds later, the radio altitude alert for two hundred feet was annunciated, and the cricket sound and stick shaker ceased. At 10:57:32, sound of impact was heard in the CVR. The FDR and CVR stopped recording at 10:57:33 and 10:57:35 respectively. The airplane was totally destroyed and all 72 occupants were killed.
Probable cause:
The most probable cause of the accident is determined to be the inadvertent movement of both condition levers to the feathered position in flight, which resulted in feathering of both propellers and subsequent loss of thrust, leading to an aerodynamic stall and collision with terrain.
The following contributing factors were identified:
- High workload due to operating into a new airport with surrounding terrain and the crew missing the associated flight deck and engine indications that both propellers had been feathered;
- Human factor issues such as high workload and stress that appears to have resulted in the misidentification and selection of the propellers to the feathered position;
- The proximity of terrain requiring a tight circuit to land on runway 12. This tight circuit was not the usual visual circuit pattern and contributed to the high workload. This tight pattern also meant that the approach did not meet the stabilized visual approach criteria;
- Use of visual approach circuit for RWY 12 without any evaluation, validation and resolution of its threats which were highlighted by the SRM team of CAAN and advices proposed in flight procedures design report conducted by the consultant and without the development and approval of the chart by the operator and regulator respectively;
- Lack of appropriate technical and skill based training (including simulator) to the crew and proper classroom briefings (for that flight) for the safe operation of flight at new airport for visual approach to runway 12;
- Non-compliance with SOPs, ineffective CRM and lack of sterile cockpit discipline.
Final Report:

Ground collision with an ATR72-500 in Medan

Date & Time: Aug 3, 2017 at 1100 LT
Type of aircraft:
Operator:
Registration:
PK-WFF
Flight Phase:
Survivors:
Yes
Schedule:
Medan – Meulaboh
MSN:
869
YOM:
2009
Flight number:
IW1252
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
67
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
13006
Captain / Total hours on type:
624.00
Copilot / Total flying hours:
263
Copilot / Total hours on type:
109
Aircraft flight hours:
14321
Aircraft flight cycles:
16132
Circumstances:
On 3 August 2017, a Boeing 737-900 ER aircraft, operated by PT. Lion Mentari Airlines (Lion Air) as a scheduled passenger flight from Sultan Iskandar Muda International Airport, Banda Aceh (WITT) to Kualanamu International Airport, Medan (WIMM) as flight number JT 197. JT197 departed at 1010 LT (0310 UTC) in daylight condition, with 151 persons on board. Meanwhile, an ATR 72-500 aircraft, operated by PT. Wings Abadi Airlines (Wings Air) as scheduled passenger flight from Medan with intended destination to Cut Nyak Dien Airport, Meulaboh (WITC) as flight number IW1252. On board IW1252 were two pilots, one observer pilot, two flight attendants and 67 passengers. At 0356 UTC, the IW1252 pilot requested taxi clearance to runway 23 from the Medan Ground controller and was instructed to follow U2 taxi route, the IW1252 pilot requested to depart via intersection taxiway D which was approved by Medan Tower controller. At 0357 UTC, JT197 was on landing approach and received landing clearance. At 04:00:01 UTC, the Medan Tower controller issued conditional clearance to the IW1252 pilot, to enter the runway after the JT197 had landed. This conditional clearance was combined with the air traffic control route clearance. IW1252 continued to taxi and entered the runway. At 04:00:50 UTC, JT197 touched down on runway 23 and a few second later impacted with the IW1252. There were no injuries during this occurrence, but both aircraft were substantially damaged. After impact, debris from the impact aircraft remained on the runway. Prior to the runway inspection, one aircraft departed and one aircraft landed.
Probable cause:
The communication misunderstanding of the conditional clearance to enter runway while the IW1252 pilots did not aware of JT197 had received landing clearance and the unobserved IW1252 aircraft movement made the IW1252 aircraft entered the runway.
Final Report: