Crash of a De Havilland DHC-6 Twin Otter 300 near Port Moresby: 4 killed

Date & Time: Sep 20, 2014 at 0935 LT
Operator:
Registration:
P2-KSF
Survivors:
Yes
Site:
Schedule:
Woitape - Port Moresby
MSN:
528
YOM:
1977
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
19290
Captain / Total hours on type:
5980.00
Copilot / Total flying hours:
432
Copilot / Total hours on type:
172
Aircraft flight hours:
34327
Aircraft flight cycles:
46302
Circumstances:
A DHC-6 Twin Otter aircraft was returning from Woitape, Central Province, to Jacksons Airport, Port Moresby on the morning of 20 September 2014 on a charter flight under the instrument flight rules (IFR). The weather at Woitape was reported to have been clear, but at Port Moresby the reported weather was low cloud and rain. Witnesses reported that the summit of Mt Lawes (1,700 ft above mean sea level (AMSL)) was in cloud all morning on the day of the accident. When the aircraft was 36 nm (67 km) from Port Moresby, air traffic control gave the flight crew a clearance to descend maintaining visual separation from terrain and to track to a left base position for runway 14 right (14R) at Jacksons Airport, Port Moresby. The clearance was accepted by the crew. When the aircraft was within 9.5 nm (17.5 km) of the airport, the pilot in command (PIC) contacted the control tower and said that they were “running into a bit of cloud” and that they “might as well pick up the ILS [instrument landing system] if it’s OK”. The flight crew could not have conducted an ILS approach from that position. They could have discontinued their visual approach and requested radar vectoring for an ILS approach. However, they did not do so. The Port Moresby Aerodrome Terminal Information Service (ATIS), current while the aircraft was approaching Port Moresby had been received by the flight crew. It required aircraft arriving at Port Moresby to conduct an ILS approach. The PIC’s last ILS proficiency check was almost 11 months before the accident flight. A 3-monthly currency on a particular instrument approach is required under PNG Civil Aviation Rule 61.807. It is likely the reason the PIC did not request a clearance to intercept the ILS from 30 nm (55.5 km) was that he did not meet the currency requirements and therefore was not authorized to fly an ILS approach. During the descent, although the PIC said to the copilot ‘we know where we are, keep it coming down’, it was evident from the recorded information that his assessment of their position was incorrect and that the descent should not have been continued. The PIC and copilot appeared to have lost situational awareness. The aircraft impacted terrain near the summit of Mt Lawes and was substantially damaged by impact forces. Both pilots and one passenger were fatally injured in the impact, and one passenger died on the day after the accident from injuries sustained during the accident. Of the five passengers who survived the accident, three were seriously injured and two received minor injuries. One of the fatally injured passengers was not wearing a seat belt.
Probable cause:
The following contributing factors were identified:
- The flight crew continued the descent in instrument meteorological conditions without confirming their position.
- The flight crew’s assessment of their position was incorrect and they had lost situational awareness
- The flight crew deprived themselves of the “Caution” and “Warning” alerts that would have sounded about 20 sec and about 10 sec respectively before the collision, by not deactivating the EGPWS Terrain Inhibit prior to departure from Woitape.
Final Report:

Crash of a Beechcraft 300LW Super King Air in Nordelta: 2 killed

Date & Time: Sep 14, 2014 at 1515 LT
Operator:
Registration:
LV-WLT
Flight Type:
Survivors:
No
Site:
Schedule:
Lincoln – Buenos Aires
MSN:
FA-221
YOM:
1992
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
14004
Captain / Total hours on type:
2000.00
Aircraft flight hours:
2630
Aircraft flight cycles:
2419
Circumstances:
The twin engine aircraft departed Lincoln-Estancia La Nueva Airport on a private flight to Buenos Aires, carrying one passenger and one pilot. While descending to Buenos Aires-Aeroparque-Jorge Newbury Airport, the pilot was unable to intercept the ILS for runway 13 because of an excessive speed of 260 knots and a too high angle of descent. In such conditions, he could not configure the aircraft for approach and landing (flaps) in accordance with the information in the BE 300 flight manual. He completed a left turn at a speed of 228 knots and descended below the glide before initiating a second turn to the right when control was lost. The aircraft entered a dive and crashed onto two houses located in Nordelta, about 26 km northwest of the airport. The aircraft and two houses were destroyed and both occupants were killed, among them Gustavo Andres Deutsch aged 78 who was the former owner of the defunct airline LAPA.
Probable cause:
The accident resulted from the combination of immediate triggers and failures in the aeronautical system's defenses, including:
- Prevailing weather conditions at the scene of the accident;
- Pilot-in-command experienced difficulties in managing aircraft control and flight path during an instrument approach;
- The probability of overload of work of the pilot in command as a result of the operational demands presented by the situation;
- The execution of the operation by a single pilot (single pilot operation), taking into account the age of the pilot; and
- Deficiencies in pilot-in-command certification denying the value of CE-6 as a defense barrier for the aeronautical system (CE-6 is a Critical Element of ICAO Annex 19 regarding responsibilities in issuing licenses).
Final Report:

Crash of a Piper PA-61 Aerostar (Ted Smith 601P) in Austin: 1 killed

Date & Time: Sep 10, 2014 at 1326 LT
Operator:
Registration:
N711YM
Flight Type:
Survivors:
No
Schedule:
Dallas – Austin
MSN:
61-0215-023
YOM:
1975
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
525
Captain / Total hours on type:
37.00
Aircraft flight hours:
3438
Circumstances:
Witnesses reported observing the airplane flying slowly toward the airport at a low altitude. The left engine was at a low rpm; "sputtering," "knocking," or making a "banging" noise; and trailing black smoke. One witness said that, as the airplane passed over his location, he saw the tail "kick" horizontally to the right and the airplane bank slightly left. The airplane subsequently collided with trees and impacted a field 1/2 mile north of the airport. Disassembly of the right engine revealed no anomalies, and signatures on the right propeller blades were consistent with power and rotation on impact. The left propeller was found feathered. Disassembly of the left engine revealed that the spark plugs were black and heavily carbonized, consistent with a rich fuel-air mixture; the exhaust tubing also exhibited dark sooting. The rubber boot that connected the intercooler to the fuel injector servo was found dislodged and partially sucked in toward the servo. The clamp used to secure the hose was loose but remained around the servo, the safety wire on the clamp was in place, and the clamp was not impact damaged or bent. The condition of the boot and the clamp were consistent with improper installation. The time since the last overhaul of the left engine was about 1,050 hours. The last 100-hour inspection occurred 3 months before the accident, and the airplane had been flown only 0.8 hour since then. It could not be determined when the rubber boot was improperly installed. Although the left engine had failed, the pilot should have been able to fly the airplane and maintain altitude on the operable right engine, particularly since he had appropriately feathered the left engine.
Probable cause:
The pilot's failure to maintain sufficient clearance from trees during the single engine and landing approach. Contributing to the accident was the loss of power in the left engine due to an improperly installed rubber boot that became dislodged and was then partially sucked into the fuel injector servo, which caused an excessively rich fuel-air mixture that would not support combustion.
Final Report:

Crash of a Beechcraft 200C Super King Air in Nouméa

Date & Time: Sep 9, 2014 at 1150 LT
Operator:
Registration:
F-GRSO
Flight Type:
Survivors:
Yes
Schedule:
Lifou – Nouméa
MSN:
BL-11
YOM:
1980
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The twin engine airplane departed Lifou Airport on an ambulance flight to Nouméa-Magenta Airport, carrying two passengers and two pilots. On approach to Magenta Airport, the crew followed the checklist and lower the landing gears. As all three green light failed to came on the cockpit panel, the crew elected to lower the gears manually without success. The crew completed two low passes in front of the control tower and it was confirmed that the left main gear seems to be down but not locked. After a 45-minute flight to burn fuel, the crew completed the landing. Upon touchdown, both main landing gear collapsed while the nose gear remained extended. The aircraft slid for few dozen metres before coming to rest. All four occupants evacuated safely and the aircraft was damaged beyond repair.
Probable cause:
The rupture of two teeth of the sprocket of the control cylinder of the left main landing gear caused the cylinder to be locked and thus caused the mechanical system to extend the landing gear. This blockage prevented the complete extension and locking of the landing gear. This rupture and other damage to the two main landing gear actuators was probably the result of improper installation of the toothed gear and / or improper adjustment of the assembly.
Final Report:

Crash of a Fokker 50 in Mogadishu

Date & Time: Sep 6, 2014 at 1030 LT
Type of aircraft:
Operator:
Registration:
5Y-BYE
Survivors:
Yes
Schedule:
Galkayo - Mogadishu
MSN:
20204
YOM:
1990
Flight number:
6J715
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
21
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Upon landing on runway 05 at Mogadishu Airport, the right main gear failed. The aircraft veered off runway to the right then rolled for few dozen metres, collided with a concrete perimeter fence and came to rest. There was no fire. It appears the right wing and the right engine suffered severe damage (the right broke in two). The nose of the aircraft was destroyed and the fuselage was bent on several areas. All 24 occupants evacuated safely. The aircraft was completing a domestic schedule flight on behalf of Jubba Airways.

Crash of a Piper PA-46-350P Malibu Mirage in Cortez

Date & Time: Sep 3, 2014 at 1238 LT
Registration:
N747TH
Flight Type:
Survivors:
Yes
Schedule:
Cortez - Cortez
MSN:
46-36200
YOM:
1999
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4000
Captain / Total hours on type:
2050.00
Copilot / Total flying hours:
4184
Copilot / Total hours on type:
1648
Aircraft flight hours:
2900
Circumstances:
The accident occurred during a local instructional flight to satisfy the commercial pilot's annual insurance currency requirements in the accident airplane. The flight instructor reported that the pilot was demonstrating a simulated loss of engine power during initial climb and return for a downwind landing. During initial climb, upon reaching 1,200 ft above ground level (agl), the flight instructor reduced engine power to flight idle and feathered the propeller. In response, the pilot reduced airplane pitch and entered a left, 45-degree-bank turn back toward the airport. The flight instructor stated that, upon rolling wings level, the airplane appeared to be lower than he had expected as it glided toward the runway; however, he believed there was sufficient altitude remaining to safely land on the runway and told the pilot to continue without increasing the engine power. The flight instructor ultimately decided to abort the maneuver as the airplane crossed over the runway threshold at 40 ft agl. The flight instructor advanced the engine power lever to the full-forward position and increased airplane pitch to arrest the descent; however, he did not perceive an increase in engine thrust. Without an increase in engine thrust and with the increased pitch, the airplane's airspeed decreased rapidly, and the airplane entered an aerodynamic stall about 30 ft above the runway. The airplane impacted the runway before sliding into a grassy area. The flight instructor reported that he did not recall advancing the propeller control when he decided to abort the maneuver, and, as such, the perceived lack of engine thrust was likely because the propeller remained feathered after he increased engine power. Additionally, the flight instructor postulated that the airplane's landing gear had not been retracted after takeoff, which resulted in a reduced climb gradient, and, as such, the airplane entered the maneuver farther away from the airport than anticipated. Further, with the landing gear extended, the airplane experienced a reduction in glide performance during the simulated forced landing. The flight instructor reported that the accident could have been prevented if he had maintained a safe flying airspeed after he took control of the airplane. Additionally, he believed that his delayed decision to abort the maneuver resulted in an insufficient margin of safety.
Probable cause:
The flight instructor's delayed decision to abort the simulated engine out maneuver, his failure to unfeather the propeller before restoring engine power, and his inadequate airspeed management, which led to an aerodynamic stall at low altitude.
Final Report:

Crash of a Piper PA-46-350P Malibu Mirage in Erie: 5 killed

Date & Time: Aug 31, 2014 at 1150 LT
Registration:
N228LL
Flight Type:
Survivors:
No
Schedule:
Denver - Erie
MSN:
46-22164
YOM:
1994
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
1300
Aircraft flight hours:
2910
Circumstances:
The private pilot was inbound to the airport, attempting to conduct a straight-in approach to runway 33. Due to the prevailing wind, traffic flow at the time of the pilot's arrival was on runway 15. Another airplane was departing the airport in the opposite direction and crossed in close proximity to the accident airplane. The departing traffic altered his course to the right to avoid the accident airplane while the accident airplane stayed on his final approach course. The two aircraft were in radio communication on the airport common traffic advisory frequency and were exercising see-and-avoid rules as required. Witnesses reported that as the airplane continued down runway 33 for landing, they heard the power increase and observed the airplane make a left-hand turn to depart the runway in an attempted go-around. The airplane entered a left bank with a nose-high attitude, failed to gain altitude, and subsequently stalled and impacted terrain. It is likely the pilot did not maintain the necessary airspeed during the attempted go-around and exceeded the airplane's critical angle of attack. The investigation did not reveal why the pilot chose to conduct the approach with opposing traffic or why he attempted a landing with a tailwind, but this likely increased the pilot's workload during a critical phase of flight.
Probable cause:
The pilot's failure to maintain adequate airspeed and exceedance of the critical angle of attack during a go-around with a tailwind condition, which resulted in an aerodynamic stall. A contributing factor to the accident was the pilot's decision to continue the approach with opposing traffic.
Final Report:

Crash of a Cessna 340A off Freeport: 4 killed

Date & Time: Aug 18, 2014 at 1002 LT
Type of aircraft:
Registration:
N340MM
Flight Type:
Survivors:
No
Schedule:
Ormond Beach - Freeport
MSN:
340A-0635
YOM:
1978
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Aircraft flight hours:
5572
Circumstances:
On 18 August, 2014 at 10:02am local time (1402Z) UTC a fixed wing, twin-engine, Cessna 3 4 0 A aircraft, United States registration N340MM, serial number 340A0635, crashed into waters while on a left base to runway 06 at Grand Bahama International Airport (MYGF) Freeport, Grand Bahama, Bahamas. The aircraft departed Ormond Beach Municipal Airport (KOMN) at 8:51am local time (1251Z) for Grand Bahama International Airport (MYGF) on an Instrument Flight Rules (IFR) flight plan with the pilot and three passengers aboard. Sometime after 9:00am (1300Z) an IFR inbound flight plan on N340MM was received by Freeport Approach Control from Miami Center. Upon initial contact with Freeport Approach Control the pilot was given weather advisory, re-cleared to Freeport VOR and told to maintain four thousand feet and report at JAKEL intersection. He was also advised to expect an RNAV runway six approach. After the pilot’s acknowledgement of the information he later acknowledged his position crossing JAKEL. Freeport Approach then instructed the aircraft to descend to two thousand feet and cleared him direct to JENIB intersection for the RNAV runway six (6) approach. After descending to two thousand feet the pilot indicated to Freeport Approach that he had the field in sight and was able to make a visual approach. Freeport Approach re-cleared the aircraft for a visual approach and instructed the pilot to contact Freeport Control Tower on frequency 118.5. At 9:57am (1357Z) N340MM established contact with Freeport Tower and was cleared for the visual approach to runway six; he was told to join the left base and report at five (5) DME. At 10:01am (1401Z) the pilot reported being out of fuel and his intention was to dead stick the aircraft into the airport from seven miles out at an altitude of one thousand five hundred feet. A minute later the pilot radioed ATC to indicate they “were going down and expected to be in the water about five miles north of the airport.” Freeport Tower tried to get confirmation of the last transmission but was unable to. Several more calls went out from Freeport Tower to N340MM but communication was never reestablished. Freeport Control Tower then made request of aircrafts departing and arriving to assist in locating the lost aircraft by over flying the vicinity of the last reported position to see if visual contact could be made. An inbound aircraft reported seeing an aircraft down five miles from the airport on the 300 degree radial of the ZFP VOR. Calls were made to all the relevant agencies and search and rescue initiated. The aircraft was located at GPS coordinates 26˚ 35.708’N and 078˚ 47. 431 W. The aircraft received substantial damage as a result of the impact and crash sequence. There were no survivors.
Probable cause:
The probable cause of this accident has been determined as a lack of situational awareness resulting in a stalled condition and loss of control while attempting to remedy a fuel exhaustion condition at a very low altitude.
Contributing factors:
- The pilot’s incorrect fuel calculations which resulted in fuel exhaustion to both engines.
- Stalled aircraft.
- Loss of situational awareness.
Final Report:

Crash of a Piper PA-31-325 Navajo in Grand Manan Island: 2 killed

Date & Time: Aug 16, 2014 at 0512 LT
Type of aircraft:
Operator:
Registration:
C-GKWE
Flight Type:
Survivors:
Yes
Schedule:
Saint John - Grand Manan Island
MSN:
31-7812037
YOM:
1978
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
17400
Copilot / Total flying hours:
304
Copilot / Total hours on type:
67
Circumstances:
The Atlantic Charters Piper PA-31aircraft had carried out a MEDEVAC flight from Grand Manan, New Brunswick, to Saint John, New Brunswick. At 0436 Atlantic Daylight Time, the aircraft departed Saint John for the return flight to Grand Manan with 2 pilots and 2 passengers. Following an attempt to land on Runway 24 at Grand Manan Airport, the captain carried out a go-around. During the second approach, with the landing gear extended, the aircraft contacted a road perpendicular to the runway, approximately 1500 feet before the threshold. The aircraft continued straight through 100 feet of brush before briefly becoming airborne. At about 0512, the aircraft struck the ground left of the runway centreline, approximately 1000 feet before the threshold. The captain and 1 passenger sustained fatal injuries. The other pilot and the second passenger sustained serious injuries. The aircraft was destroyed; an emergency locator transmitter signal was received. The accident occurred during the hours of darkness.
Probable cause:
Findings as to causes and contributing factors:
1. The captain commenced the flight with only a single headset on board, thereby preventing a shared situational awareness among the crew.
2. It is likely that the weather at the time of both approaches was such that the captain could not see the required visual references to ensure a safe landing.
3. The first officer was focused on locating the runway and was unaware of the captain’s actions during the descent.
4. For undetermined reasons, the captain initiated a steep descent 0.56 nautical mile from the threshold, which went uncorrected until a point from which it was too late to recover.
5. The aircraft contacted a road 0.25 nautical mile short of the runway and struck terrain.
6. The paramedic was not wearing a seatbelt and was not restrained during the impact sequence.
Findings as to risk:
1. If cockpit data recordings are not available to an investigation, then the identification and communication of safety deficiencies to advance transportation safety may be precluded.
2. If crew members are unable to communicate effectively, then they are less likely to anticipate and coordinate their actions, which could jeopardize the safety of flight.
3. If crew resource management training is not provided, used and continuously fostered, then there is a risk that pilots will be unprepared to avoid or mitigate crew errors encountered during flight.
4. If an actual weight and balance cannot be determined, then the aircraft may be operating outside of its approved limits, which could affect the aircraft’s performance characteristics.
5. If pre-computed weight and balance forms do not include standard items, then it increases the likelihood of omissions in weight and balance calculations, which increases the risk of inadvertently overloading or incorrectly loading the aircraft.
6. If organizations carry out a maintenance task that they consider to be elementary work and the task is not approved as an elementary work task, then there is a risk that the aircraft will not conform to its type design, which could jeopardize the safety of flight.
7. If individuals are performing maintenance tasks for which they have not received approved training, then there is a risk that the task will not be performed in accordance with the manufacturer’s instructions.
8. If components are not installed in accordance with the manufacturer’s instructions, then occupants are at a greater risk of injury or death during an incident or accident if these components are not properly secured.
9. If organizations do not record when maintenance is carried out, then the proper completion of tasks cannot be confirmed, and there is a risk that the aircraft will not conform to its type design, which could jeopardize the safety of flight.
10. If an aircraft is modified without regulatory approval and without supporting documentation, then the aircraft is not in compliance with all applicable standards of airworthiness, which could jeopardize the safety of flight.
11. If an operator undertakes unapproved changes to a supplemental type certificate, then there is a risk that the aircraft will not be airworthy, which could jeopardize the safety of flight.
12. If organizations do not use modern safety management practices, then there is an increased risk that hazards will not be identified and risks mitigated.
13. If Transport Canada does not adopt a balanced approach that combines thorough inspections for compliance with audits of safety management processes, unsafe operating practices may not be identified, thereby increasing the risk of accidents.
14. If organizations contract aviation companies to provide a service with which the organizations are not familiar, then there is an increased risk that safety deficiencies will go unnoticed, which could jeopardize the safety of the organizations’ employees.
15. If passengers are not provided with a regular safety briefing, then there is an increased risk that they will not use the available safety equipment or be able to perform necessary emergency functions in a timely manner to avoid injury or death.
16. If passengers are not properly restrained, then there is an increased risk of injuries and death to those passengers and the other occupants in the event of an accident.
17. If carry-on baggage, equipment or cargo is not restrained, then occupants are at a greater risk of injury or death if these items become projectiles in a crash.
18. If carry-on baggage, equipment or cargo is not restrained, then there is an increased risk that the occupants’ access to normal and emergency exits, and to safety equipment, will be completely or partially blocked.
19. If pilots continue an approach below published minimum descent altitudes without seeing the required visual references, then there is a risk of collision with terrain and/or obstacles.
20. If current charts and databases are not used, then navigational accuracy and obstacle avoidance cannot be assured.
21. If GPS (global positioning system) approaches are conducted without the approved Operations Specification, then there is a risk that the pilot’s training and knowledge will be inadequate to safely conduct the approach.
22. If medical symptoms/conditions are not reported to Transport Canada, then it negates some of the safety benefit of examinations and increases the risk that pilots will continue to fly with a medical condition that poses a risk to safety.
Other findings:
1. The pilot who installed the air ambulance system did not have approved training, nor was the pilot approved to carry out elementary work.
2. Atlantic Charters was not approved to install the air ambulance system as an elementary work task.
3. Atlantic Charters’ pre-computed weight and balance form did not include a line item to indicate nacelle fuel.
4. The semi-annual safety training offered to paramedics in lieu of safety briefings prior to flights did not meet regulatory requirements.
Final Report:

Crash of a BAe 3102 Jetstream 31 in Doncaster

Date & Time: Aug 15, 2014 at 1936 LT
Type of aircraft:
Operator:
Registration:
G-GAVA
Survivors:
Yes
Schedule:
Belfast – Doncaster
MSN:
785
YOM:
1987
Flight number:
LNQ207
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8740
Captain / Total hours on type:
3263.00
Circumstances:
G-GAVA took off from Belfast City Airport at 1745 hrs operating a scheduled air service to Doncaster Sheffield Airport with one passenger and a crew of two pilots on board. The commander was the Pilot Flying (PF) and the co-pilot was the Pilot Monitoring (PM). The departure, cruise and approach to Doncaster Sheffield were uneventful. The 1820 hrs ATIS for the airport stated that the wind was from 260° at 5 kt, varying between 220° and 280°. Visibility was greater than 10 km, there were few clouds at 3,000 ft aal, the temperature was 17°C and the QNH was 1,019 hPa. Although Runway 02 was the active runway, the crew requested radar vectors for a visual final approach to Runway 20, a request which was approved by ATC. The load sheet recorded that the aircraft’s mass at landing was expected to be 5,059 kg which required a target threshold indicated airspeed (IAS) of 101 kt. The aircraft touched down at 1836 hrs with an IAS of 102 kt and a peak normal acceleration of 1.3 g, and the commander moved the power levers aft to ground idle and then to reverse. As the aircraft decelerated, the commander moved the power levers forward to ground idle and asked the co-pilot to move the RPM levers to taxi. At an IAS of 65 kt, eight seconds after touchdown, the left wing dropped suddenly, the aircraft began to yaw to the left and the commander was unable to maintain directional control with either the rudder or the nosewheel steering tiller. The aircraft ran off the left side of the runway and stopped on the grass having turned through approximately 90°. The left landing gear had collapsed and the aircraft had come to a halt resting on its baggage pannier, right landing gear and left wing. The commander pulled both feather levers, to ensure that both engines were shut down, and switched the Electrics Master switch to emergency off. The co-pilot transmitted “tower……[callsign]” and the controller replied “[callsign] copied, emergency services on their way”. The commander instructed the co-pilot to evacuate the aircraft. The co-pilot moved into the main cabin where he found that the passenger appeared to be uninjured. He considered evacuating the aircraft through the emergency exit on the right side but judged that the main exit on the left side at the rear of the cabin would be the best option. The left side cabin door released normally but would not open completely because the sill of the doorway was at ground level (Figure 1) but, all occupants were able to evacuate the aircraft. The Aerodrome Controller in the ATC tower activated the Crash Alarm at 1836 hrs while the aircraft was still on the paved surface of the runway. Two Rescue and Fire Fighting Service vehicles arrived on scene at 1838 hrs by which time the occupants were clear of the aircraft.
Probable cause:
The aircraft’s left main landing gear failed as a result of stress corrosion cracking in the forward pintle housing, at the top of the left landing gear cylinder. The landing gear material is known to be susceptible to stress corrosion cracking. The investigation determined that a design solution implemented by the aircraft manufacturer following the 2012 accident, which was intended to prevent stress corrosion cracking, had not met its original design intent.
Final Report: