Crash of a Cessna 208B Super Cargomaster in Manteo: 1 killed

Date & Time: Dec 25, 2002 at 0100 LT
Type of aircraft:
Operator:
Registration:
N1122Y
Flight Type:
Survivors:
No
Schedule:
Elizabeth City - Manteo
MSN:
208B-0392
YOM:
1994
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
19091
Captain / Total hours on type:
500.00
Aircraft flight hours:
5229
Circumstances:
At 0029, the pilot contacted Norfolk Approach and stated he was ready for takeoff on runway 01 at Elizabeth City. The controller instructed the pilot to fly runway heading and climb to 3,000 feet. At 0032, the controller advised the pilot that the flight was radar contact and for the pilot to fly heading 160 degrees. At 0034, the Norfolk Approach controller instructed the pilot to contact the FAA Washington Air Route Traffic Control Center. At 0034, the pilot of N1122Y contacted the controller at Washington Center, stating he was coming up on 3,000 feet. The controller acknowledged, and the pilot requested the non-directional beacon (NDB) approach to runway 5 at Dare County Airport, Manteo. At 0036, the controller instructed the pilot to fly heading 145 degrees for Manteo and fly direct to the NDB when he receives the signal. The pilot acknowledged and the controller also asked the pilot if he had the current weather for Manteo. The pilot responded that he did have the current weather. At 0043, the controller cleared the pilot for the NDB runway 5 approach at Manteo and to maintain 2,000 feet until the flight crossed the beacon outbound. The pilot acknowledged. At 0046, the controller informed the pilot that radar contact with the flight was lost and for the pilot to report a cancellation or a downtime on his radio frequency. The pilot acknowledged. At 0057:21, the controller called the pilot and the pilot responded by reporting the flight was procedure turn inbound. No further transmissions were received from the pilot. When the pilot did not report that he was on the ground, and further radio contact could not be established, controllers initiated search and rescue efforts. The wreckage of the airplane was located in the waters of Croatan Sound, about 1.5 miles west of the Dare County Regional Airport about 1000. The pilot was not located in the airplane. The body of the pilot was located in the waters of Croatan Sound on February 11, 2003. Post crash examination of the airplane, flight controls, and engine showed no evidence of precrash failure or malfunction. The propeller separated from the airplane and was not located after the accident. Damage to the mounting bolts for the propeller was consistent with the propeller separating due to impact with the water. Postmortem examination of the pilot showed no findings which could be considered causal to the accident.
Probable cause:
The pilot's continued descent below the minimum descent altitude, for undetermined reasons, while performing a NDB approach, resulting in the airplane crashing into water 1.5 miles from the airport. A factor in the accident was a cloud ceiling below the minimum descent altitude and low visibility.
Final Report:

Crash of an Antonov AN-140-100 near Isfahan: 44 killed

Date & Time: Dec 23, 2002 at 1929 LT
Type of aircraft:
Operator:
Registration:
UR-14003
Survivors:
No
Site:
Schedule:
Kharkov - Trabzon - Isfahan
MSN:
253 02 008
YOM:
2002
Flight number:
AHW2137
Location:
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
38
Pax fatalities:
Other fatalities:
Total fatalities:
44
Aircraft flight hours:
70
Circumstances:
The aircraft departed Kharkiv Airport on a charter flight to Isfahan, Iran, with an intermediate stop in Trabzon, carrying 38 passengers and six crew members. All the occupants were engineers working for Antonov and flying to Isfahan to conduct test flights on the first Iran-140, a prototype built under licence by HESA Company. While descending to Isfahan Airport by night and marginal weather conditions, the aircraft struck the slope of a mountain located 30 km from the airport. The aircraft was totally destroyed and all 44 occupants were killed.
Probable cause:
Controlled flight into terrain after the pilots failed to use properly the GPS system installed in the cockpit.

Crash of a Cessna 208B Super Cargomaster in Rockford: 1 killed

Date & Time: Dec 17, 2002 at 2251 LT
Type of aircraft:
Operator:
Registration:
N277PM
Flight Type:
Survivors:
No
Schedule:
Decatur – Rockford
MSN:
208B-0143
YOM:
1988
Flight number:
PMS1627
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1872
Captain / Total hours on type:
1525.00
Aircraft flight hours:
10120
Circumstances:
The airplane collided with trees and terrain following a loss of control during an Instrument Landing System (ILS) approach at night. The impact occurred approximately 2.1 miles from the approach end of the runway. A witness reported hearing the airplane at "mid-throttle" as it flew over. He then heard the power increase followed by the impact. The witness stated there was no precipitation at the time of the accident and there were "severe winds, mostly from the south, shifting volatile directly from the east." He also stated the visibility was "extremely poor." Statements were received from five pilots who landed in transport category airplanes around the time of the accident. Three of these pilots reported experiencing a crosswind that varied from 15 to 50 knots during the approach. Four of the pilots reported airspeed fluctuations that varied between +/- 8 knots to +/- 10 knots during the approach. Three of the pilots reported breaking out of the clouds between 200 and 300 feet agl. Radar data indicates the airplane was high on the glideslope until it entered a rapid descent from an altitude of about 2,300 feet. Examination of the airframe, engine, and propeller governors failed to reveal any failures/malfunctions that would have resulted in the loss of control.
Probable cause:
The pilot's failure to maintain control of the airplane during the ILS approach. Factors associated with the accident were the low ceilings, high winds, crosswind, and wind shear conditions that existed.
Final Report:

Crash of a Cessna 414A Chancellor in Hahn: 2 killed

Date & Time: Dec 17, 2002 at 1353 LT
Type of aircraft:
Registration:
D-IAFL
Survivors:
No
Schedule:
Egelsbach - Hahn
MSN:
414A-0256
YOM:
1979
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3233
Captain / Total hours on type:
550.00
Circumstances:
While descending to Hahn Airport, the pilot encountered marginal weather conditions with limited visibility due to clouds down to 500 feet. On approach, the twin engine aircraft collided with trees and crashed about 11 km from the runway 03 threshold. The aircraft was destroyed and both occupants were killed.
Probable cause:
Collision with trees on approach after the pilot continued under VFR mode in IMC conditions. Poor flight planning on part of the pilot who failed to take into consideration the poor visibility at destination due to low clouds. Insufficient and ambiguous communication between pilot and ATC was considered as a contributing factor.
Final Report:

Crash of a GAF Nomad N.22A off Zamboanga

Date & Time: Dec 17, 2002
Type of aircraft:
Operator:
Registration:
53
Flight Type:
Survivors:
Yes
Schedule:
Sanga-Sanga - Zamboanga
MSN:
053
YOM:
1977
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
13
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Following an uneventful flight from Sanga-Sanga Airport (Tawi-Tawi Island), the pilot started the descent to Zamboanga Airport. On final approach, the twin engine aircraft lost height and crashed in the sea 300 metres offshore. All 14 occupants were rescued while the aircraft sank.

Crash of a BAe 125-1A-731 in Seattle

Date & Time: Dec 16, 2002 at 1907 LT
Type of aircraft:
Registration:
N55RF
Survivors:
Yes
Schedule:
Sacramento – Seattle
MSN:
25020
YOM:
1964
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
13497
Captain / Total hours on type:
1713.00
Aircraft flight hours:
14162
Circumstances:
The Co-Pilot was the flying pilot with the Captain giving directions throughout the approach phase. The Captain stated that he extended the flaps and the landing gear. When the aircraft touched down, the landing gear was not extended. The Co-Pilot reported that she did look down at the landing gear lever and at "three green lights" on the approach. The CVR was read out which indicated that the Co-Pilot directed the Captain to call inbound. The Captain acknowledged this and stated "fifteen flaps." The Co-Pilot then stated "fifteen flaps, before landing." The Captain did not respond to the Co-Pilot but instead made a radio transmission. The Captain shortly thereafter, stated that he was extending the flaps to 25 degrees. The Captain made another radio transmission to the tower when the Co-Pilot stated "final, sync, ignitions." The Captain responded "ignitions on." Full flaps were then extended. The Captain gave the Co-Pilot continued directions while on the approach for heading, speed and altitude. At approximately 300 feet, the Captain stated, "yaw damper's off, air valves are off, ready to land." The Captain reported that it was obvious that touchdown was on the flaps and keel. The Captain stated that he raised the flaps, shutdown the engines, and confirmed that the landing gear handle was down. During the gear swing test the landing gear cycled several times with no difficulties. All red and green lights illuminated at the proper positions. During the test, it was found that the gear not extended horn did not function with the gear retracted, the flaps fully extended and the power levers at idle. Later a bad set of contacts to the relay was found. When the relay was jumped, the horn sounded. Inspection of the damage to the aircraft revealed that the outer rims of both outer tires displayed scrape marks around the circumference of the rim. The outer surface of the gear door fairings were scraped and the flap hinge fairings was ground down.
Probable cause:
The landing gear down and locked was not verified prior to landing. The checklist was not followed, and an inoperative landing gear warning horn were factors.
Final Report:

Crash of a Douglas DC-8-62F in Singapore

Date & Time: Dec 13, 2002 at 1743 LT
Type of aircraft:
Operator:
Registration:
N1804
Flight Type:
Survivors:
Yes
Schedule:
Yokota - Singapore
MSN:
45896/303
YOM:
1967
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
11800
Captain / Total hours on type:
7200.00
Copilot / Total flying hours:
6200
Copilot / Total hours on type:
1900
Aircraft flight hours:
73500
Aircraft flight cycles:
29900
Circumstances:
The crew started their duty for the flight from Yokota, near Tokyo, Japan to Singapore at 1000 hours local time (0900 hours Singapore time) on 13 December 2002. The aircraft departed Yokota at 1125 hours local time (1025 hours Singapore time). The FO was the handling pilot for the flight. The expected flight time was about 7 hours. The departure and en route segments of the flight proceeded normally. The crew was aware of Changi Airport’s ATIS ‘Y’ weather information provided at about 1640 hours through Changi Airport’s there were thunderstorm activity, low level windshear and heavy rain in Singapore. The aircraft was given clearance to land on Runway 20R. The FO briefed the other crew members on landing on 20R. At about 7 miles from the airport, Changi Tower advised the aircraft that the wind was from 350 degrees at 5 knots, that the runway surface was wet, that the visibility from the Tower was about 1,000 metres and that landing traffic had reported the braking action at the end of Runway 20R to be from medium to poor. The approach and landing was carried out in heavy rain. The approach was stabilized and normal. Approach speed was about 148 knots. Flaps 35 were used. At about 300 feet above ground, the PIC reported having the approach lights and runway lights in sight while the FO still could not see the lights as the rain removal for the windshield on the FO’s side was not effective. According to the FO, he felt the PIC was putting his hands on the controls of the aircraft. The PIC noticed that the aircraft had drifted slightly left of the runway centreline and told the FO to make the correction back to the centerline. Although the FO made the correction, he was still unable to see the approach lights clearly at about 200 feet. The FO indicated he felt the PIC was in control of the aircraft and making corrections and so he let go of the controls. The CVR recording suggested that the PIC was aware the aircraft was floating down the runway and that the PIC informed the crew that “We are floating way down the runway.” The PIC subsequently moved the control column forward to make a positive landing. The aircraft landed at 1743 hours. The aircraft was observed by an air traffic controller to have touched down on the runway at a point roughly abeam the Control Tower and just before the turn-off for Taxiway W6, which was about 1,500 metres from the end of the runway. Two Airport Emergency Service officers of the Civil Aviation Authority of Singapore also observed that while most aircraft landing on Runway 20R would touch down at a point between the turn-offs for Taxiways W3 and W4, the Arrow Air aircraft floated way beyond the normal touchdown zone. The aircraft’s speed at the time of touchdown was estimated from flight data recorder data to be about 135 knots. Upon touchdown, the PIC deployed spoilers and thrust reversers. The thrust reversers for Engines Nos. 1, 2 and 3 deployed almost immediately while that of Engine No. 4 was reportedly slow in deployment. The PIC and FO also pushed hard on the brake pedals, but they felt that there was no braking response. The aircraft did not stop before reaching the end of the runway. It veered slightly to the right as it exited the runway. The speed of the aircraft when it left the runway was about 60 knots. The aircraft rolled in mud during the overrun. The nose landing gear broke off half way during the overrun and the aircraft came to rest in a grass and soggy area at about 300 metres from the end of the runway. There was no fire. After the aircraft had come to a complete stop, the PIC stowed the thrust reversers. The crew completed the evacuation checklist and exited the aircraft from Door L1 with the assistance of the Airport Emergency Service personnel who had already arrived by then.
Probable cause:
The following significant factors were identified:
- The FO, the pilot flying the approach and landing, did not elect to go around even though he did not have the runway lights and approach lights in sight at 300 feet above ground.
- The PIC could have taken over control from the FO when the latter still could not see the approach lights and runway lights at 300 feet above ground.
- The crew landed long by about 1,300 metres on the runway.
- The crew had not made a determination of the landing distance required for the landing on Runway 20R. They had just verified using the Runway Analysis Manual that the aircraft landing weight was within limit for the landing.
Final Report:

Crash of an Embraer EMB-110P Bandeirante in Havana

Date & Time: Dec 6, 2002
Operator:
Registration:
CU-T1110
Survivors:
Yes
Schedule:
Holguin - Havana
MSN:
110-098
YOM:
1976
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On final approach to Havana-José Marti-Rancho Boyeros Airport by night, the crew encountered poor weather conditions with heavy rain falls. In limited visibility, the aircraft descended too low when it impacted the ground and crashed in a wasteland located less than one km from the runway threshold. All 10 occupants were injured and the aircraft was destroyed.

Crash of a Cessna 500 Citation I in Marília

Date & Time: Dec 1, 2002 at 2310 LT
Type of aircraft:
Registration:
PT-LIY
Survivors:
Yes
Schedule:
Goiânia – Marília
MSN:
500-0219
YOM:
1975
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2200
Captain / Total hours on type:
1200.00
Copilot / Total flying hours:
1300
Copilot / Total hours on type:
200
Circumstances:
Following an uneventful flight from Goiânia-Santa Genoveva Airport, the crew started the descent to Marília Airport by night. Poor weather conditions at destination forced the crew to make a direct approach to runway 03. After landing, the aircraft was unable to stop within the remaining distance, overran, lost its undercarriage and came to rest in bushes 143 metres past the runway end. All seven occupants were rescued, among them four were injured. The aircraft was damaged beyond repair.
Probable cause:
Poor approach configuration on part of the crew who landed the aircraft 750 metres past the runway threshold, reducing the landing distance available. The following contributing factors were identified:
- The crew completed an unstabilized approach,
- Poor approach planning,
- Limited visibility due to the night and poor weather conditions,
- The braking action was low because the runway surface was wet,
- The crew failed to initiate a go-around procedure.
Final Report:

Crash of a Let L-410UVP-E20 in Olkiombo: 1 killed

Date & Time: Nov 28, 2002 at 1330 LT
Type of aircraft:
Registration:
5Y-ONT
Survivors:
Yes
Schedule:
Musiara – Mombasa
MSN:
87 18 12
YOM:
1987
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
18
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
After takeoff from Musiara Airport, during initial climb, the crew raised the landing gear and flaps. About 45 seconds after liftoff, the left engine failed. The crew elected to restart it but without success and decided to divert to Olkiombo Airport located 18 km from their position. On approach to runway 09, the aircraft stalled and crashed in an open field. The copilot was killed while 19 other occupants were injured, some seriously. The aircraft was destroyed.
Probable cause:
Failure of the left engine during initial climb for unknown reasons.