Crash of a De Havilland DHC-6 Twin Otter 300 off Værøy: 5 killed

Date & Time: Apr 12, 1990 at 1444 LT
Operator:
Registration:
LN-BNS
Flight Phase:
Survivors:
No
Schedule:
Værøy – Bodø
MSN:
536
YOM:
1977
Flight number:
WF839
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
5534
Captain / Total hours on type:
1269.00
Copilot / Total flying hours:
1370
Copilot / Total hours on type:
354
Aircraft flight hours:
27304
Aircraft flight cycles:
58709
Circumstances:
Less than two minutes after takeoff from Værøy Airport runway 25, while climbing in marginal weather conditions, the aircraft banked left then entered an uncontrolled descent and crashed in the sea in a near vertical attitude about 1,8 km from the airport. The aircraft was destroyed and all five occupants were killed. When the crew started to roll at the airport, the wind was gusting to 57 knots which was 7 knots above the maximum allowable limit for ground operations. After takeoff, the aircraft encountered wind gusting to 34 knots which was 14 knots above the maximum allowable limit for flight operations. Excessive wind component caused the stabilizers/elevator to fail, causing the aircraft to enter an uncontrolled descent and to crash in the sea.
Probable cause:
The cause of the accident was that the plane during departure came into the wind that exceeded the aircraft's design criteria. Thus there was a break in the horizontal stabilizer / elevator which meant that the plane could no longer be controlled.
Final Report:

Crash of a De Havilland DHC-6 Twin Otter 300 off Utila

Date & Time: Apr 4, 1990
Operator:
Registration:
HR-ALH
Survivors:
Yes
Schedule:
La Ceiba – Útila
MSN:
180
YOM:
1968
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
18
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On final approach to Útila Airport runway 25, the crew was blinded by the low sun position and failed to realize his altitude was insufficient. The aircraft struck the water surface and crashed in the sea about 50 meters offshore and less than 300 meters short of runway 25 threshold. All 20 occupants were evacuated safely while the aircraft was damaged beyond repair.

Crash of a De Havilland DHC-6 Twin Otter 300 in Labuan Bajo

Date & Time: Apr 3, 1990
Operator:
Registration:
PK-NUQ
Flight Phase:
Survivors:
Yes
Schedule:
Labuan Bajo – Denpasar
MSN:
488
YOM:
1976
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
14
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
After liftoff from Labuan Bajo-Mutiara Airport, while in initial climb, the left engine oversped. The crew elected to make an emergency landing when the aircraft struck rocks then crashed in a ravine. All 17 occupants were injured.
Probable cause:
Loss of control during initial climb after the left engine oversped for unknown reasons.

Crash of a Fairchild-Hiller FH-227B in Lagos

Date & Time: Apr 1, 1990 at 1155 LT
Type of aircraft:
Registration:
5N-ATL
Flight Phase:
Survivors:
Yes
Schedule:
Lagos - Port Harcourt
MSN:
534
YOM:
1967
Country:
Region:
Crew on board:
7
Crew fatalities:
Pax on board:
45
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
20925
Circumstances:
During the takeoff roll on runway 19L, at a speed of about 100 knots, the aircraft deviated from the centerline to the right. The pilot-in-command corrected with rudder but finally, the aircraft struck the right shoulder of the runway then veered off runway. It rolled in a grassy area and came to rest few dozen meters further. All 52 occupants evacuated safely while the aircraft was damaged beyond repair due to structural damages to the fuselage.
Probable cause:
It was determined that the right engine was not running properly during the takeoff roll, creating an asymmetric thrust and the aircraft to deviate from the centerline to the right. Investigations reported that the aircraft was subject to maintenance the days prior to the accident and modification were made to the fuel pump but nothing was entered in the airplane logbook. It was determined that the fuel pump overspeed governor had been set too low and a low power output at high TGT.

Crash of a PZL-Mielec AN-2R in Chumikan

Date & Time: Mar 24, 1990
Type of aircraft:
Operator:
Registration:
CCCP-17977
Flight Phase:
Survivors:
Yes
MSN:
1G210-01
YOM:
1984
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed following an engine failure. There were no casualties.
Probable cause:
Engine failure for unknown reasons.

Crash of a PZL-Mielec AN-2R near Kirensk

Date & Time: Mar 24, 1990
Type of aircraft:
Operator:
Registration:
CCCP-40679
Flight Phase:
Survivors:
Yes
MSN:
1G214-37
YOM:
1985
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
En route, the fuel pressure dropped and the engine lost power. The crew decided to return to his departure point when the engine failed. The crew attempted an emergency landing when the aircraft crashed in the taïga near Kirensk. Both pilots were injured.
Probable cause:
It is believed that the engine failed due to ignition problems.

Crash of an Antonov AN-26 in Santiago de Cuba: 4 killed

Date & Time: Mar 23, 1990
Type of aircraft:
Operator:
Registration:
CU-T1436
Flight Phase:
Survivors:
Yes
Schedule:
Santiago de Cuba - Havana
MSN:
87307406
YOM:
1978
Flight number:
CU7406
Country:
Crew on board:
5
Crew fatalities:
Pax on board:
41
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
During the takeoff roll, at V1 speed, the captain decided to abandon the takeoff procedure for unknown reasons. He reduced engine power and initiated an emergency braking maneuver. At a distance of 150 meters from the runway end, he realized he could not stop the airplane in time so he veered off runway to the left. The aircraft went into a grassy area, rolled for few dozen meters then plunges in a ravine, bursting into flames. Four passengers were killed while 17 other occupants were injured.

Crash of a Hawker-Siddeley HS.121 Trident 2E in Guilin

Date & Time: Mar 22, 1990
Operator:
Registration:
B-2208
Survivors:
Yes
Schedule:
Shanghai - Guilin
MSN:
2165
YOM:
1974
Location:
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
102
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Following a wrong approach configuration at Guilin Airport, the three engine aircraft landed too far down the runway. Unable to stop within the remaining distance, the aircraft overran, lost its right main gear and came to rest in a grassy area. All 107 occupants evacuated safely while the aircraft was damaged beyond repair. Weather conditions were poor at the time of the accident with rain showers and limited visibility. Thus, the runway surface was wet and the braking action was limited.

Crash of a Douglas C-47A-75-DL in Roatan: 7 killed

Date & Time: Mar 18, 1990 at 0620 LT
Operator:
Registration:
HR-SAZ
Survivors:
Yes
Schedule:
Guanaja - Roatán - San Pedro Sula
MSN:
19495
YOM:
1944
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
29
Pax fatalities:
Other fatalities:
Total fatalities:
7
Circumstances:
The aircraft was completing a flight from Guanaja to San Pedro Sula with an intermediate stop in Roatán. After landing, the crew encountered strong crosswinds when the aircraft veered off runway and crashed in the Caribbean Sea. A crew member and six passengers were killed while 25 other occupants were injured.
Probable cause:
Loss of control after touchdown due to strong crosswinds.

Crash of a PZL-Mielec AN-2R in Amgu

Date & Time: Feb 24, 1990
Type of aircraft:
Operator:
Registration:
CCCP-33544
Survivors:
Yes
MSN:
1G229-36
YOM:
1988
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
After touchdown, the single engine aircraft went out of control, veered off runway and came to rest. There were no casualties.