Crash of a Mitsubishi MU-2B-60 Marquise near Burlington: 1 killed

Date & Time: Apr 19, 1984 at 2022 LT
Type of aircraft:
Registration:
N466MA
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Burlington - Windsor Locks
MSN:
1540
YOM:
1981
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
5700
Captain / Total hours on type:
3200.00
Aircraft flight hours:
7890
Circumstances:
The aircraft was flown earlier in the day for a sales demonstration. On the return flight, when the landing gear were lowered, the pilot thought he heard a noise emitting from the gear, although cockpit indications were normal. The aircraft landed at Johnny Cake Airport and was refueled for a flight to Bradley Field where it is hangared. The pilot stated he intended to make the 22 miles flight with the gear down as a precaution. He also stated his intention to fly below the overcast because of delays of up to 45 minutes in obtaining IFR clearances. Moments after takeoff the aircraft collided with trees east of the airport. About one mile east of the airport is a north-south ridge. Another pilot, who departed 15-20 mins earlier, reported entering the overcast between 400 and 700 feet agl. Ground witnesses one mile southeast of the airport who heard the crash described the weather as heavy fog and mist. One witness estimated the ceiling as 100 feet agl. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: in flight encounter with weather
Phase of operation: cruise
Findings
1. (f) weather condition - low ceiling
2. (c) VFR flight into imc - initiated - pilot in command
----------
Occurrence #2: in flight collision with object
Phase of operation: cruise
Findings
3. (f) object - tree(s)
4. (c) altitude - inadequate - pilot in command
5. (f) light condition - dark night
Final Report:

Crash of a De Havilland DH.114 Heron 2B in Scottsdale

Date & Time: Apr 5, 1984 at 1715 LT
Type of aircraft:
Operator:
Registration:
N81962
Flight Type:
Survivors:
Yes
Schedule:
Albuquerque – Scottsdale
MSN:
14053
YOM:
1954
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5682
Captain / Total hours on type:
37.00
Aircraft flight hours:
20652
Circumstances:
For undetermined reasons the pilot experienced a power loss on both left engines while turning from left base to final for landing. The pilot was unable to maintain directional control and elected to reduce power on the right engines. During the forced landing roll the aircraft collided with three ditches as well as small trees. As the aircraft touched down both left engines resumed full power. The pilot, sole on board, was uninjured.
Probable cause:
Occurrence #1: loss of engine power
Phase of operation: approach - VFR pattern - base turn
Findings
1. (c) reason for occurrence undetermined
----------
Occurrence #2: forced landing
Phase of operation: descent - emergency
----------
Occurrence #3: on ground/water encounter with terrain/water
Phase of operation: landing - roll
Findings
2. Terrain condition - ditch
----------
Occurrence #4: on ground/water collision with object
Phase of operation: landing - roll
Findings
3. Object - tree(s)
Final Report:

Crash of a Beechcraft 65 Queen Air in Jennings: 1 killed

Date & Time: Apr 5, 1984 at 1045 LT
Type of aircraft:
Operator:
Registration:
N6RG
Flight Type:
Survivors:
No
Schedule:
New Roads - Mesa
MSN:
LC-199
YOM:
1966
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
A popping or backfiring sound was heard by several people who later observed the aircraft flying at low altitude on what appeared to be a final approach to runway 13 at Jennings Airport (located about 75 miles southwest of the departure point.) No radios were onboard the aircraft so no distress calls were made. Because of the wind this would have been a downwind landing. The aircraft then aborted the approach due to an aircraft landing from the opposite direction and appeared to start a left turn onto abase leg when it stalled, pitched nose down and impacted the ground with its landing gear and flaps extended. Wreckage examination revealed that all 3 blades of the right prop were bent smoothly and symmetrically rearward. However, no preimpact failure or malfunction of the right engine was found. There were no entries in the aircraft's logbook from 7/1/78 until 4/3/84 when the aircraft was inspected for the ferry flight. The pilot was not multi-engine rated and had not flown this type aircraft in about 10 years. The pilot's commercial certificate was revoked on 11/21/81. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: loss of engine power
Phase of operation: unknown
Findings
1. (c) reason for occurrence undetermined
----------
Occurrence #2: loss of control - in flight
Phase of operation: approach - VFR pattern - base turn
Findings
2. Procedures/directives - not followed - pilot in command
3. (f) qualification - pilot in command
4. (f) overconfidence in personal ability - pilot in command
5. Precautionary landing - initiated - pilot in command
6. Go-around - performed - pilot in command
7. (c) airspeed (VMC) - not maintained - pilot in command
8. (c) stall - inadvertent - pilot in command
9. (c) inadequate transition/upgrade training - pilot in command
10. (f) lack of recent experience - pilot in command
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: approach - VFR pattern - base turn
Final Report:

Crash of a De Havilland DHC-2 Beaver off Port McNeill: 1 killed

Date & Time: Dec 30, 1983
Type of aircraft:
Operator:
Registration:
C-FRQW
Flight Phase:
Flight Type:
Survivors:
No
MSN:
618
YOM:
1954
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
Crashed into the sea shortly after takeoff from Port McNeill, Vancouver island, BC. The pilot, sole on board, was killed.

Crash of a Rockwell Aero Commander 520 in Clines Corners: 2 killed

Date & Time: Nov 8, 1983 at 2018 LT
Registration:
N4116B
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Bartlesville - Tucumcari - Ontario
MSN:
520-20
YOM:
1952
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
625
Captain / Total hours on type:
95.00
Circumstances:
The non-instrument rated pilot was on ferry flight from Bartlesville, OK to Ontario, CA. An en route stop was made at Tucumcari, NM, where the aircraft was refueled and 14 qts of oil was added to the left engine. The line boy who serviced the aircraft saw no visible oil leaks or spillage around the engine. While on the next leg of the flight, the aircraft crashed near interstate highway 40. Two witnesses that saw the crash stated rain was falling, the wind was blowing very strong and there were low ceilings. Reportedly, a squall line was moving thru the area and there was moderate to severe turbulence. An exam of the wreckage revealed the aircraft had crashed in a steep nose down attitude, with 20° to 30° left bank and at high speed. No preimpact, mechanical failures were found and both engines had evidence that they were operating during impact. The weather briefer said the pilot indicated he would fly around the area of precipitation and remain VFR. Radar info showed the pilot had been following the interstate highway and varying his alt between 7,900 and 6,300 feet msl. Both occupants were killed.
Probable cause:
Occurrence #1: in flight encounter with weather
Phase of operation: cruise - normal
Findings
1. (f) flight into known adverse weather - initiated - pilot in command
2. (f) light condition - dark night
3. (f) weather condition - low ceiling
4. (f) weather condition - high wind
5. (f) weather condition - rain
6. (c) VFR flight into IMC - continued - pilot in command
----------
Occurrence #2: loss of control - in flight
Phase of operation: cruise
Findings
7. (c) aircraft handling - not maintained - pilot in command
8. (c) spatial disorientation - pilot in command
9. (f) lack of total instrument time - pilot in command
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of a Beechcraft C90 King Air in Fort Wayne: 1 killed

Date & Time: Oct 24, 1983 at 1615 LT
Type of aircraft:
Registration:
N4TS
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Fort Wayne - Tulsa
MSN:
LJ-541
YOM:
1972
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
18980
Aircraft flight hours:
3821
Circumstances:
At 1604 est, the aircraft departed Fort Wayne on a ferry flight. IFR conditions prevailed and the pilot had filed an IFR flight plan. While climbing after takeoff, the pilot passed his assigned altitude of 2,500 feet msl and flew to 4,200 feet. Also, he failed to turn to his initial assigned heading of 130°. He had problems contacting departure control as he was not on the assigned frequency. He reported problems with his heading indicator and his 'gyro'. Shortly after his last transmission, the aircraft left 4,200 feet msl and crashed in a steep dive. Before takeoff, the atp pilot reported he had flown all King Air aircraft and was currently flying the Beech 200. A review of his last log book revealed over 2,000 hours in the Beech 200, but showed no time in the Beech C90. A witness that reviewed the aircraft with the pilot before the flight believed he (the pilot) was very familiar with the aircraft systems. During an inspection of the wreckage, no evidence was found to verify a pre-impact malfunction or failure of the aircraft or engines. All instruments were destroyed. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: climb
Findings
1. (c) reason for occurrence undetermined
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of a Learjet 25B in Wilmington

Date & Time: Aug 17, 1983 at 0724 LT
Type of aircraft:
Operator:
Registration:
N108PA
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Wilmington - Danville
MSN:
25-195
YOM:
1975
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4304
Captain / Total hours on type:
1420.00
Aircraft flight hours:
4758
Circumstances:
After lift-off a flock of birds approached from left to right at about 400 feet. The pilot maneuvered the aircraft behind and above the birds in an attempt to avoid them. Both engines flamed out and the aircraft made a forced landing on a road. Ground witnesses described the climbout as '...very steep...' and '...a steep angle, between 40° 45°.' There was some bird residue on the engines. Both pilots escaped uninjured.
Probable cause:
Occurrence #1: loss of engine power (total) - non mechanical
Phase of operation: takeoff - initial climb
Findings
1. (f) maneuver - performed - pilot in command
2. (c) aircraft performance, climb capability - exceeded
3. (c) aircraft handling - improper - pilot in command
----------
Occurrence #2: forced landing
Phase of operation: maneuvering - turn to landing area (emergency)
Findings
4. (f) aircraft performance, two or more engines - inoperative
----------
Occurrence #3: in flight collision with object
Phase of operation: maneuvering - turn to landing area (emergency)
Findings
5. Object - bird(s)
----------
Occurrence #4: in flight collision with terrain/water
Phase of operation: landing - flare/touchdown
----------
Occurrence #5: main gear collapsed
Phase of operation: landing - roll
Findings
6. Landing gear, main gear - overload
Final Report:

Crash of a Rockwell Grand Commander 680 in Bayport: 2 killed

Date & Time: Jul 28, 1983 at 1515 LT
Operator:
Registration:
N6878S
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Bayport - Islip
MSN:
680-409-85
YOM:
1956
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
4000
Aircraft flight hours:
4967
Circumstances:
At about 60 feet agl black smoke was observed coming from the left engine. The aircraft continued a climb in a nose high attitude and the nose pitched down and the aircraft rolled inverted. Engine teardown revealed extensive damage to the supercharger assembly. The impeller shaft was bent and its associated bearing damaged. The aircraft had not flown for about 14 years. Engine service instructions describe pre-oiling of the supercharger drive shaft bearing after any prolonged period of inactivity. The owner, a paraplegic, was seated in the left seat. The pilot seated in the right seat had a history of heart and pulmonary disease. The gear and flaps were in the down position. Prior to departure, a witness asked the owner 'are you doing the elevators and ailerons and is he your rudders.' the owner responded with 'we have an arrangement'. Both occupants were killed.
Probable cause:
Occurrence #1: loss of engine power(total) - mechanical failure/malfunction
Phase of operation: takeoff - initial climb
Findings
1. (c) maintenance, service bulletin/letter - not followed - company maintenance personnel
2. (c) engine assembly, blower/impeller/integral supercharger - failure, total
3. (c) maintenance, lubrication - not performed - company maintenance personnel
----------
Occurrence #2: loss of control - in flight
Phase of operation: takeoff - initial climb
Findings
4. (c) aircraft handling - uncontrolled - pilot in command
5. (c) incapacitation (other cardiovascular) - pilot in command
6. (c) airspeed (VMC) - not possible - unqualified person
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: takeoff - initial climb
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in the Pacific Ocean: 2 killed

Date & Time: Dec 9, 1982 at 0228 LT
Registration:
N74957
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Oakland - Honolulu
MSN:
31-7305106
YOM:
1973
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
6000
Captain / Total hours on type:
100.00
Aircraft flight hours:
5093
Circumstances:
The aircraft departed Oakland, CA at 1733 PST on a night flight to Honolulu, HI. The flight proceeded without incident until approximately 0050 PST when the pilot advised that the left engine was slowly losing oil pressure. At that time, the aircraft was at an altitude of 6,000 feet. At 0205, the pilot reported he shut down the engine and was unable to maintain 6000 feet. A descent was started. In his last transmission at 0228 PST, the pilot reported that he was at 500 feet, barely maintaining altitude. Radio contact was lost when the aircraft was approximately 500 miles east of Honolulu. At 1559, the crew of a search aircraft sighted floating debris and one body floating in that area. A marker buoy was deployed, but no recovery was accomplish. The aircraft was presumed to have been destroyed and both occupants were presumed to have been fatally injured. The aircraft crashed in moderate sea conditions with waves heights estimated at three to five feet.
Probable cause:
Occurrence #1: loss of engine power
Phase of operation: cruise
Findings
1. (c) reason for occurrence undetermined
2. (f) fluid,oil - pressure too low
3. Propeller feathering - intentional - pilot in command
----------
Occurrence #2: ditching
Phase of operation: landing
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: landing - flare/touchdown
Findings
4. (f) light condition - night
5. (f) terrain condition - water,rough
Final Report:

Crash of a Rockwell Aero Commander 560E in Livingston: 2 killed

Date & Time: Nov 20, 1982 at 1614 LT
Operator:
Registration:
N3827C
Flight Type:
Survivors:
No
Schedule:
Blairstown - Teterboro
MSN:
560-0744
YOM:
1959
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
730
Circumstances:
Aero Commander 560E, N3827C (27C) was returning from Blairstown where it had been flown for minor maintenance. The pilot was on an IFR flight plan, cleared by New York tracon to proceed at 2,000 feet msl on a radar vector of 170° for an ILS approach to the Teterboro Airport. The aircraft was equipped with an altitude encoding transponder that was being used. The pilot was advised of numerous targets at his 12 o'clock position. At approximately the same time, Cessna 182Q, N96402 (402), was on a flight from the Kupper Airport to Ramapo Airport. A direct route between these airports would have intersected the nw edge of the New York TCA where positive control began between 1,800 and 7,000 feet msl. The pilot was proceeding VFR with no flight plan and was not in radio communication with any ATC facility. 402 was equipped with a transponder that was operating, but had no altitude encoding capability. As the aircraft converged, 402 was on a northeasterly heading. The planes collided about 1 mile inside the TCA. Then impacted the ground approximately 1,500 feet apart. A map was found in 402 with a line drawn between the airports and intersecting the TCA. All three occupants in both aircraft were killed.
Probable cause:
Occurrence #1: midair collision
Phase of operation: approach
Findings
1. (f) air/ground communications - not attained - pilot of other aircraft
2. (f) procedures/directives - not followed - pilot of other aircraft
3. (f) traffic advisory - not obtained - pilot of other aircraft
4. (f) unsafe/hazardous condition - not identified - ATC personnel (dep/apch)
5. (c) visual lookout - inadequate - pilot in command
6. (c) visual lookout - inadequate - pilot of other aircraft
Final Report: