Crash of a Beechcraft 100 King Air near Valera: 6 killed

Date & Time: Mar 1, 2009 at 1153 LT
Type of aircraft:
Registration:
YV2129
Survivors:
No
Site:
Schedule:
Charallave – Valera
MSN:
B-83
YOM:
1971
Location:
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
The twin engine aircraft departed Charallave-Óscar Machado Zuloaga Airport on a charter flight to Valera, carrying four passengers and two pilots. While descending to Valera-Carvajal Airport in IMC conditions, at an altitude of 9,650 feet, the aircraft impacted the slope of Mt Piedra Gorda located 35 km from the airport. The wreckage was found the following day at the end of the afternoon. The aircraft disintegrated on impact and all 6 occupants were killed.
Probable cause:
Controlled flight into terrain after the crew started the descent prematurely. The lack of visibility was considered as a contributing factor.

Crash of a PZL-Mielec AN-2SX in Bishkek

Date & Time: Feb 22, 2009 at 1249 LT
Type of aircraft:
Operator:
Registration:
EX-68039
Flight Phase:
Survivors:
Yes
Schedule:
Bishkek - Bukhara
MSN:
1G193-11
YOM:
1981
Flight number:
GRA4571
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8215
Captain / Total hours on type:
7362.00
Copilot / Total flying hours:
7613
Copilot / Total hours on type:
4985
Aircraft flight hours:
6132
Circumstances:
The single engine aircraft departed from a small airstrip in Bishkek on a charter service (flight GRA4571) to Bukhara with two passengers and two pilots on board. About a minute after takeoff, while in initial climb, the engine lost power. The crew informed ATC about the situation and was cleared for an immediate return. Shortly later, the engine failed and the crew attempted an emergency landing in an open field located near the aerodrome. Upon landing, the aircraft collided with a small drainage ditch, lost its left main gear and both left wings before coming to rest. All four occupants escaped with minor injuries and the aircraft was damaged beyond repair.
Probable cause:
The reason for the loss of engine power in flight, most likely, was a reduction in the filing of the gasoline due to clogging of fuel filters. The appearance, structure and nature of the impurities found in the fuel on the aircraft were not characteristic of impurities accumulated in the fuel supply system in normal operating conditions. The source of the impurities in aircraft fuel system could not be found.
Final Report:

Crash of an Embraer EMB-110P1 Bandeirante off Santo Antônio: 24 killed

Date & Time: Feb 7, 2009 at 1324 LT
Operator:
Registration:
PT-SEA
Survivors:
Yes
Schedule:
Coari - Manaus
MSN:
110-352
YOM:
1981
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
26
Pax fatalities:
Other fatalities:
Total fatalities:
24
Captain / Total flying hours:
18870
Captain / Total hours on type:
7795.00
Copilot / Total flying hours:
1011
Copilot / Total hours on type:
635
Aircraft flight hours:
12686
Circumstances:
The twin engine aircraft departed Coari Airport at 1240LT on a charter flight to Manaus-Eduardo Gomes Airport, carrying 26 passengers and two pilots. About 30 minutes into the flight, while cruising at FL115, the crew informed ATC that the left engine failed and elected to divert to the unused Manacapuru Airfield. While approaching runway 08, the aircraft rolled to the left to an angle of 30° then crashed in the Rio Manacapuru. 24 people were killed while 4 passengers were slightly injured.
Probable cause:
The following factors were identified:
- At takeoff from Coari Airport, the total weight of the aircraft was 6,414 kg, which means 744 kg over the MTOW,
- On board were 26 passengers including 8 children while the aircraft was certified for 19 passengers,
- The left engine fuel pump was completely burnt during the accident but it could not be determined if it failed during the flight or not,
- The crew was not sufficiently trained for emergency situations,
- Poor work organisation,
- Lack of supervision from the operator concerning crew's decisions before and during flights,
- Poor crew coordination,
- Lack of crew communication,
- Non compliance with management techniques,
- Incomplete execution of the actions provided by the emergency checklist.
Final Report:

Crash of a Piper PA-31 Navajo Chieftain in Darwin

Date & Time: Feb 6, 2009 at 0840 LT
Operator:
Registration:
VH-TFX
Flight Phase:
Survivors:
Yes
Schedule:
Darwin – Maningrida
MSN:
31-8152143
YOM:
1981
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Shortly after takeoff from Darwin Airport, while in initial climb, one of the engine failed. The pilot declared an emergency and elected to return but eventually attempted to ditch the aircraft that came to rest in shallow water about 200 metres offshore. All six occupants escaped uninjured while the aircraft was damaged beyond repair.

Crash of a De Havilland DHC-6 Twin Otter 100 in La Ronge

Date & Time: Feb 4, 2009 at 0915 LT
Operator:
Registration:
C-FCCE
Flight Phase:
Survivors:
Yes
Schedule:
La Ronge – Deschambeault Lake
MSN:
8
YOM:
1966
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
14000
Captain / Total hours on type:
11000.00
Copilot / Total flying hours:
625
Copilot / Total hours on type:
425
Circumstances:
The aircraft was taking off from a ski strip east of and parallel to Runway 36 at La Ronge. After the nose ski cleared the snow, the left wing rose and the aircraft veered to the right and the captain, who was the pilot flying, continued the take-off. The right ski, however, was still in contact with the snow. The aircraft became airborne briefly as it cleared a deep gully to the right of the runway. The aircraft remained in a steep right bank and the right wing contacted the snow-covered ground. The aircraft flew through a chain link fence and crashed into trees surrounding the airport. The five passengers and two crewmembers evacuated the aircraft with minor injuries. There was a small fire near the right engine exhaust that was immediately extinguished by the crew.
Probable cause:
Findings as to Causes and Contributing Factors:
1. Contamination on the wings of the aircraft was not fully removed before take-off. It is likely that asymmetric contamination of the wings created a lift differential and a loss of lateral control.
2. Although the operator was not authorized for short take-off and landing (STOL) take-off on this aircraft, the crew conducted a STOL take-off, which reduced the aircraft’s safety margin relative to its stalling speed and minimum control speed.
3. As a result of the loss of lateral control, the slow STOL take-off speed, and the manipulation of the flaps, the aircraft did not remain airborne and veered right, colliding with obstacles beside the ski strip.
Findings as to Risk:
1. The out of phase task requirements regarding the engine vibration isolator assembly, as listed in the operator’s maintenance schedule approval, results in a less than thorough inspection requirement, increasing the likelihood of fatigue cracks remaining undetected.
2. The right engine inboard and top engine mounts had pre-existing fatigue cracks, increasing the risk of catastrophic failure.
Other Findings:
1. The cockpit voice recorder (CVR) contained audio of a previous flight and was not in operation during the occurrence flight. Minimum equipment list (MEL) procedures for logbook entries and placarding were not followed.
2. The Transwest Air Limited safety management system (SMS) did not identify deviations from standard operating procedures.
Final Report:

Crash of a Beechcraft F90-1 King Air in Mamuno

Date & Time: Jan 21, 2009
Type of aircraft:
Operator:
Registration:
A2-AHV
Survivors:
Yes
MSN:
LA-212
YOM:
1983
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On approach to Mamuno Airstrip, the pilot decided to initiate a go-around procedure. After the undercarriage were raised, the twin engine aircraft continued to descent and hit the runway surface. It slid for few dozen metres then veered off runway to the left and came to rest in a grassy area. The high engine temperature set the grass on fire and the aircraft was destroyed by fire. There were no injuries among the occupants.

Crash of a Gulfstream G200 in Oradea

Date & Time: Jan 16, 2009 at 1535 LT
Type of aircraft:
Operator:
Registration:
YR-TIG
Survivors:
Yes
Schedule:
Bucharest - Oradea
MSN:
012
YOM:
1999
Flight number:
TIH101
Location:
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
10
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
13000
Captain / Total hours on type:
2000.00
Copilot / Total flying hours:
1600
Copilot / Total hours on type:
465
Circumstances:
Following an uneventful flight from Bucharest-Otopeni Airport, the crew started the approach to Oradea Airport in marginal weather conditions. On final approach, the pilot-in-command established a visual contact with the runway 19 and continued the descent. The aircraft landed 761 metres past the runway threshold. After touchdown, it was unable to stop within the remaining distance, overran and came to rest in a drainage ditch located 420 metres short of runway 01 threshold. All 13 occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
The contrast between the area covered with snow and the snow-cleared area (the runway) induced the pilots visual sensation about the runway threshold. This caused the crew to miscalculate the touchdown point, causing the aircraft to land too far down the runway.
Final Report:

Crash of a Cessna 550 in Wilmington

Date & Time: Jan 4, 2009 at 0209 LT
Type of aircraft:
Operator:
Registration:
N815MA
Survivors:
Yes
Schedule:
La Isabela - Wilmington
MSN:
550-0406
YOM:
1982
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6914
Captain / Total hours on type:
1400.00
Copilot / Total flying hours:
1717
Aircraft flight hours:
11123
Circumstances:
During a night, northbound, international over water flight that paralleled the east coast of the southeast United States, the airplane encountered headwinds. Upon arrival at the intended destination, the weather was below forecasted conditions, resulting in multiple instrument approach attempts. After the first missed approach, the controller advised the crew that there was an airport 36 miles to the north with "much better" weather, but the crew declined, citing a need to clear customs. During the third missed approach, the left engine lost power, and while the airplane was being vectored for a fourth approach, the right engine lost power. Utilizing the global positioning system, the captain pointed the airplane toward the intersection of the airport's two runways. Approximately 50 feet above the ground, he saw runway lights, and landed. The captain attempted to lower the landing gear prior to the landing, but it would not extend due to a lack of hydraulic pressure from the loss of engine power, and the alternate gear extension would not have been completed in time. The gear up landing resulted in damage to the underside of the fuselage and punctures of the pressure vessel. The captain stated that the airplane arrived in the vicinity of the destination with about 1,000 pounds of fuel on board or 55 minutes of fuel remaining. However, air traffic and cockpit voice recordings revealed that the right engine lost power about 14 minutes after arrival, and the left engine, about 20 minutes after arrival. Federal air regulations require, for an instrument flight rules flight plan, that an airplane carry enough fuel to complete the flight to the first airport of landing, fly from that airport to an alternate, and fly after that for 45 minutes at normal cruising speed. The loss of engine power was due to fuel exhaustion, with no preaccident mechanical anomalies noted to the airplane.
Probable cause:
A loss of engine power due to the crew's inadequate in-flight fuel monitoring.
Final Report:

Crash of a Britten-Norman BN-2A Trislander off Providenciales: 12 killed

Date & Time: Dec 15, 2008 at 1645 LT
Type of aircraft:
Registration:
N650LP
Flight Phase:
Survivors:
No
Schedule:
Santiago de los Caballeros – Mayaguana – New York
MSN:
1029
YOM:
1976
Crew on board:
1
Crew fatalities:
Pax on board:
11
Pax fatalities:
Other fatalities:
Total fatalities:
12
Circumstances:
The aircraft was making a charter flight from Santiago de los Caballeros to New York with an intermediate stop at Mayaguana, Bahamas. The flight departed Santiago-Cibao Airport, Dominican Republic, at 1605LT. Thirty-five minutes later, while cruising off the Turks & Caicos Islands, the pilot sent a brief mayday message and the aircraft crashed 25 km off Providenciales. SAR teams and US Coast Guards did not find any trace of the aircraft nor the 12 occupants. A spokesman from the Dominican Pilots Association later reported that the pilot's licence had been suspended in October 2006.

Crash of a Dornier DO228-202 in Cambridge Bay

Date & Time: Dec 13, 2008 at 0143 LT
Type of aircraft:
Operator:
Registration:
C-FYEV
Survivors:
Yes
Schedule:
Resolute Bay - Cambridge Bay
MSN:
8133
YOM:
1987
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
12
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
13400
Captain / Total hours on type:
802.00
Copilot / Total flying hours:
850
Copilot / Total hours on type:
470
Circumstances:
The Summit Air Charters Dornier 228-202 was on a charter flight from Resolute Bay to Cambridge Bay, Nunavut, under instrument flight rules. While on final approach to Runway 31 True, the aircraft collided with the ground approximately 1.5 nautical miles from the threshold at 0143 mountain standard time. Of the 2 pilots and 12 passengers on board, 2 persons received serious injuries. The aircraft was substantially damaged. The emergency locator transmitter activated, and the crew notified the Cambridge Bay Airport radio operator of the accident via the aircraft radio. Local ground search efforts found the aircraft within 30 minutes, and all occupants were removed from the site within two hours.
Probable cause:
Findings as to Causes and Contributing Factors:
1. An abbreviated visual approach was conducted at night in instrument meteorological conditions, which resulted in the flight crew’s inability to obtain sufficient visual reference to judge their height above the ground.
2. The flight crew did not monitor pressure altimeter readings or reference the minimum altitude requirements in relation to aircraft position on the approach, resulting in controlled flight into terrain.
3. The pilots had not received training and performance checks for the installed global positioning system (GPS) equipment, and were not fully competent in its use. The attempts at adjusting the settings likely distracted the pilots from maintaining the required track and ground clearance during the final approach.
Findings as to Risk:
1. The precision approach path indicator systems (PAPI) at Cambridge Bay had not been inspected in accordance with the Airport Safety Program Manual. Although calibration of the equipment did not have a bearing on this occurrence, there was an increased risk of aircraft misalignment from the proper glide path, especially during night and reduced visibility conditions.
2. The flight crew’s cross-check of barometric altimeter performance was not sufficient to detect which instrument was inaccurate. As a result, reference was made to a defective altimeter, which increased the risk of controlled flight into terrain.
3. Operators’ maintenance organizations normally do not have access to the troubleshooting information contained in Component Maintenance Instruction Manuals for the Intercontinental Dynamics Corporation altimeters. Therefore, aircraft could be dispatched with damaged instruments with the potential for developing a loss of calibration during flight.
4. The flight was conducted during a period in which the crew’s circadian rhythm cycle could result in cognitive and physical performance degradation unless recognized and managed.
Final Report: